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Summary Report for Conduct of Kozloduy NPP Stress Tests

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“<strong>Kozloduy</strong> <strong>NPP</strong>” PLC<br />

SUMMARY REPORT<br />

<strong>for</strong> <strong>Conduct</strong> <strong>of</strong> <strong>Kozloduy</strong> <strong>NPP</strong><br />

<strong>Stress</strong> <strong>Tests</strong><br />

Additional system <strong>for</strong> steam generator emergency makeup (ASSGEM-3) <strong>of</strong> unit 3 and<br />

ASSGEM-4 <strong>of</strong> unit 4, and Fire Pump Station 2 were designed and put into service be<strong>for</strong>e 1997 as a<br />

system <strong>of</strong> seismic category I and are designed <strong>for</strong> seismic effects <strong>of</strong> DBE level.<br />

The wind load calculated in the design basis (1.40 kN/m2) <strong>of</strong> the three buildings is greater<br />

than the extreme value (1.24 kN/m2) <strong>of</strong> these standards. The available margin is within 2.6%,<br />

taking into account the significance factor according to the current standards and elastic work <strong>of</strong> the<br />

structures.<br />

4.3.1.1.3 Rein<strong>for</strong>ced concrete ventilation pipes 1 and 2<br />

In 1999 a constructive investigation <strong>of</strong> "Energoproekt" LLC <strong>of</strong> the three rein<strong>for</strong>ced concrete<br />

pipes at the site was per<strong>for</strong>med identifying that the facilities are designed <strong>for</strong> the effects <strong>of</strong> wind<br />

with calculated load from 1,26 kN/m2 exceeding the extreme values <strong>of</strong> 1.24 kN/m2 <strong>of</strong> these norms.<br />

The facilities have the required carrying capacity to bear the normative and extreme wind<br />

load as the design value <strong>of</strong> the wind is 88% higher as compared against the normative value and<br />

1.6% against the extreme value the wind.<br />

4.3.1.1.4 Spray pools 3,4 unit<br />

Design basis <strong>of</strong> the three spray pools comply with their first class in seismic resistance and<br />

the calculated maximum wind speed <strong>of</strong> 45 m/s (load - 1.24 kN/m2) at probability P = 0.01% (once<br />

per 10 000 years), which meets the requirements <strong>of</strong> the regulations and specified extreme wind<br />

speeds.<br />

Losses <strong>of</strong> water treatment during extreme winds do not affect the per<strong>for</strong>mance <strong>of</strong> the system<br />

safety function (ultimate heat sink) as the system is open and has a continuous makeup from the<br />

advance chamber be<strong>for</strong>e CPS-2.<br />

4.3.1.2 Snowfalls<br />

4.3.1.2.1 Units 3 and 4 – Reactor compartment<br />

The design basis <strong>for</strong> the calculated extreme snow loads (2.52 kN/m2) exceed the standard<br />

calculated value <strong>of</strong> these standards (1.68 kN/m2).<br />

Facilities have the necessary carrying capacity to withstand standard and extreme snow<br />

loads as the design calculated value <strong>of</strong> snow load is higher than 50% as compared against the<br />

normative value and 57% as compared against the extreme values <strong>of</strong> snow load.<br />

4.3.1.2.2 ASSGEM 3 and 4, FPS 2, CPS 2 AND DGS 2<br />

The design snow load in the design basis (1.40 kN/m2) is less than the defined extreme (1.6<br />

kN/m2) and standard (1.68 kN/m2) value. In relatively heavy structures such as rein<strong>for</strong>ced concrete,<br />

with a high ratio <strong>of</strong> permanent loads to the snow loads, the impact <strong>of</strong> the increase <strong>of</strong> snow is<br />

minimal. The physical condition <strong>of</strong> structural elements and the influence <strong>of</strong> a constant load is rather<br />

130/202

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