atw - International Journal for Nuclear Power | 05.2019
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<strong>atw</strong> Vol. 64 (2019) | Issue 5 ı May<br />
296<br />
Brokdorf<br />
REPORT<br />
Operating sequence in 2018<br />
100<br />
90<br />
80<br />
70<br />
60<br />
50<br />
40<br />
30<br />
20<br />
10<br />
Electrical output in %<br />
January February March April May June July August September October November December<br />
In the year 2018 nuclear power plant Brokdorf (KBR) was on the grid<br />
with an availability factor of 84.70 % in total 7,937 operating hours.<br />
Gross generation <strong>for</strong> the year under review amounted to<br />
80 10,376,751 MWh. Also in 2018, the thermal reactor power was limited<br />
to a maximum of 95 % with a coolant temperature reduced by 3 K<br />
60 of nominal power due to the specifications of ME 02/2017 “Increased<br />
oxide layer thickness on fuel rod cladding tubes of fuel assemblies”.<br />
40<br />
Due to high summer temperatures, temporary reductions in output<br />
were necessary in the months of July to September in order to<br />
20<br />
comply with the water law permit.<br />
100<br />
0<br />
Planned shutdowns<br />
On 1 April 2018 the plant was shutdown <strong>for</strong> the 30 th refuelling and<br />
annual major revision:<br />
The revision included the following priorities:<br />
80<br />
pp<br />
Reactor<br />
Offload of the reactor pressure vessel.<br />
Oxide layer measurement and<br />
60<br />
visual inspection of fuel elements.<br />
40<br />
Inspection of control elements.<br />
Ultrasonic test, reactor pressure vessel,<br />
20<br />
bottom part.<br />
pp<br />
Main coolant pump YD40 Ring exchange of e-motor.<br />
0<br />
Inspection of the axial bearing.<br />
Replacement mechanical shaft seal.<br />
pp<br />
Feed water system Pressure testing.<br />
pp<br />
Coolant<br />
Works on pump stationary head VE30/40.<br />
Works on main coolant water<br />
Positionierung: channel VA10-30.<br />
pp<br />
Turbine Bezug, links, Standard untenservice.<br />
Inspection primary water cooler<br />
of generator.<br />
pp<br />
Trans<strong>for</strong>mers VGB: HKS6K Exchange 30 % of trans<strong>for</strong>mers<br />
<strong>atw</strong>: 100 60 CS12, 0 0 CS21, CT31.<br />
pp<br />
Batteries Exchange, redundancy 1<br />
100<br />
X = 20,475 Y = 95,25 B = 173,5 H = 38,2<br />
Unplanned shutdowns and reactor/turbine trip<br />
On 2 May 2018, the generator was disconnected from the grid and<br />
shut down to remove a seal leakage at a non-return flap of the steam<br />
generator blowdown system. On 5 May 2018, after completion of the<br />
repair, a malfunction in the turbine control at one of two electrohydraulic<br />
converters (EHU) occurred during start-up of the plant.<br />
After clearing of the failure the main synchronisation took place on<br />
6 May 2018.<br />
On 12 August 2018 the plant was disconnected from the grid <strong>for</strong><br />
repairing the speed monitor selection circuit of the turbine protection<br />
system.<br />
<strong>Power</strong> reductions above 10 % and longer than <strong>for</strong> 24 h<br />
In the period from 12 to 13 October 2018, power reduction was carried<br />
out <strong>for</strong> the inspection and repair of a connecting slide valve between<br />
a <strong>for</strong>ce-locking basin and a pump antechamber of the secured<br />
secondary cooling water system as well as <strong>for</strong> the detection and removal<br />
of a condenser pipe leakage in the turbine condenser.<br />
In addition, load reductions were carried out in order to implement<br />
the grid-supporting power control in accordance with the specifications<br />
of the mission control centre.<br />
Delivery of fuel elements<br />
During the reporting year 28 fuel elements were delivered.<br />
Waste management status<br />
By the end of the year 2018 33 loaded CASTOR © cask were located at<br />
the on-site intermediate storage Brokdorf.<br />
Report<br />
Operating Results 2018