Florentines Patisserie - Sustainable Business Network
Florentines Patisserie - Sustainable Business Network
Florentines Patisserie - Sustainable Business Network
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Introduction of Lean Manufacturing<br />
Management recognised early on that it was important for the company to consolidate its position after 3 years of<br />
aggressive sales growth and concentrate on the internal robustness of the business. In February 2010, Lean<br />
Manufacturing i was implemented into the business to cope with system issues faced by having a larger range and<br />
production facility.<br />
<strong>Florentines</strong> was clear that they wanted to survive the difficult change from a small batch producer to a larger<br />
manufacturer and the productivity improvement project was implemented throughout the company. Lean<br />
manufacturing has been a large part of helping <strong>Florentines</strong> to scale up and re-design almost all facets of the business.<br />
The company has implemented change across the entire company from the business structure, production processes,<br />
warehouse systems, finished products inventory, new products, accounting practices, and sales and marketing. This<br />
helped give a clear focus and strategy to help the company improve its profitability.<br />
Staff Training<br />
<strong>Florentines</strong> realised early on in the Lean process that productivity was going to be a large factor in helping the company<br />
survive and prosper. Most of the products are hand-made and without the correct flow and procedures, competing in<br />
the marketplace would be difficult if not impossible.<br />
A considerable amount of time was spent on staff training around continuous improvement. In less than a year, over<br />
150 continuous improvement ideas were suggested and almost all of these were implemented.<br />
Creation of New Roles<br />
An existing staff member, experienced in production planning and lean processes, was re-stationed into the production<br />
planning role with a view to improving the production processes and systems. Significant improvements were made in<br />
this area. Another person was employed to take over many of the production planning tasks so that the experienced<br />
staffer could further develop the productivity programme that has been set up. These are both new roles and huge<br />
resources have been allocated to this programme of continuous improvement.<br />
Change Management<br />
<strong>Florentines</strong> realised early on that the change couldn’t be imposed upon the staff but rather they needed to buy into the<br />
change and lean process. Although not initially easy, it was supported by the management team’s determination and<br />
patience. To better facilitate this change process, and so that the managing director could spend the considerable time<br />
required with the staff, a person was employed to take on his role in the sales and marketing department.<br />
After a large amount of staff awareness training and knowledge building, <strong>Florentines</strong> worked hard on aligning the aims<br />
and values of the business with the needs of staff. Again, much of this was done with staff consultation. Although still in<br />
the early stages of this change process, the business believes in continuous learning and incremental improvement.<br />
<strong>Florentines</strong> is now in the process of breaking down its strategic vision into smaller measurable KPI’s and performance<br />
measures.<br />
Sustainability Measures<br />
• Moved from plastic milk bottles to bags even though they are more expensive. This saved one large rubbish bin<br />
and pick-up per week.<br />
• Implemented a recycle bin for all cardboard products.<br />
• Changed to a new supplier that used recycled cardboard for all cake packaging.<br />
• Purchased new freezer equipment that has reduced power bill from $1.01 per square foot to $0.32 per square<br />
foot.<br />
• Moved from having four colour printers throughout the business to one more efficient colour printer which has<br />
saved 30% in costs over the last three months.<br />
• Any waste food products is now given to pig farmers instead of dumping.<br />
• All staff are encouraged to turn off all computers etc. prior to leaving for home.