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Methanol Plant Capacity Enhancement By: Mr. C D ... - Fibre2fashion

Methanol Plant Capacity Enhancement By: Mr. C D ... - Fibre2fashion

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Two catalyst charging nozzles were used with hoppers and 2 ½” dia flexible hoses for charging the catalyst -<br />

SACK WISE under the supervision of Linde. A table was prepared to log the number of bags charged per<br />

round and the subsequent dip achieved, which showed the packing uniformity. This proved to be a very<br />

successful method of charging with good packing density with less than 20 mm of variation in the final height<br />

adjustment. A flat and heavy plumb with strong cotton thread was used for taking the dip.<br />

Approximately equal quantities of 20 kg balls/catalyst were filled in HDPE sacks before the start of loading.<br />

About 5.2 m 3 alumina balls were filled first in four rounds of sack charging. The catalyst bed was leveled so<br />

that the balls were just inside the tube coiled bundle. The first dip of catalyst was taken after charging<br />

almost half of the catalyst. Thereafter, while monitoring the height, charging continued to completion over<br />

approximately two (2) days.<br />

Commissioning activities<br />

The synthesis loop was made available earlier than the distillation loop (6 ½ days) while the total shutdown<br />

period was compressed to 8 days by effective identification of the priority of each job. The effectiveness of<br />

the pre-commissioning activities was evident during post-commissioning. There were no plugged strainers,<br />

control valves by-passing, nor false signals during or after the startup of the plant. Re-commissioning of the<br />

plant was completed in less than 4 days time. While, the distillation section modifications were being<br />

completed, the synthesis loop pre-commissioning activities were completed. While the catalyst heat up and<br />

reduction was proceeding, crude methanol production was coming online.<br />

Peak production levels for the plant were achieved while testing the plant at different feed gas mixtures. The<br />

plant has met all process guarantees. Of particular interest has been an improved yield of methanol due to a<br />

higher conversion rate and stable reaction conditions. Less by-product formation has led to a reduction of<br />

loading in the distillation section.<br />

Conclusion<br />

From this experience, we see that the plant capacity can be increased by understanding the basic principles<br />

of reaction kinetics and unit operations. Through integration of technology and the use of improved catalyst,<br />

this little plant had been transformed into a giant producer. Proper planning of critical activities like catalyst<br />

charging, pre-commissioning of loops, commissioning and guarantee test runs can ensure success.<br />

About the Authors:<br />

The authors are associated with GNFC Ltd.<br />

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