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Evaluation of Lime Kiln Dust as a Mineral Filler in Stone Matrix Asphalt

Evaluation of Lime Kiln Dust as a Mineral Filler in Stone Matrix Asphalt

Evaluation of Lime Kiln Dust as a Mineral Filler in Stone Matrix Asphalt

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West and James 3<br />

<strong>in</strong>clud<strong>in</strong>g soil condition<strong>in</strong>g and stabilization, <strong>in</strong>dustrial w<strong>as</strong>te stabilization, Portland cement<br />

production, and agricultural uses. Unused LKD is usually stockpiled near the lime plant but can<br />

be disposed <strong>of</strong> <strong>in</strong> approved landfills.<br />

C<strong>as</strong>e Studies <strong>of</strong> the Use <strong>of</strong> <strong>Lime</strong> <strong>Kiln</strong> <strong>Dust</strong> <strong>as</strong> a <strong>M<strong>in</strong>eral</strong> <strong>Filler</strong> <strong>in</strong> SMA<br />

Alabama<br />

<strong>Lime</strong> kiln dust w<strong>as</strong> used <strong>in</strong> several SMA projects <strong>in</strong> Alabama between 2001 and 2002.<br />

Accord<strong>in</strong>g to the Alabama Department <strong>of</strong> Transportation, a number <strong>of</strong> these SMA projects<br />

exhibited discolored surfaces soon after construction. The discoloration w<strong>as</strong> generally observed<br />

<strong>as</strong> a blotchy grey color. One Alabama project with lime kiln dust did result <strong>in</strong> more significant<br />

pavement problems. This SMA project w<strong>as</strong> constructed on Highway 80 <strong>in</strong> Selma, Alabama <strong>in</strong><br />

the summer <strong>of</strong> 2002. This project w<strong>as</strong> <strong>in</strong>tended to correct significant rutt<strong>in</strong>g on this heavy<br />

trafficked section <strong>of</strong> roadway. The exist<strong>in</strong>g rutted pavement w<strong>as</strong> milled five <strong>in</strong>ches and two<br />

layers <strong>of</strong> SMA were placed to complete the reconstruction. The first layer w<strong>as</strong> a 1-½ <strong>in</strong>ch<br />

Maximum Aggregate Size (MAS) SMA which w<strong>as</strong> placed 3 to 3.5 <strong>in</strong>ches thick. The surface<br />

layer w<strong>as</strong> a ½ <strong>in</strong>ch MAS SMA that w<strong>as</strong> placed 1.5 to 2 <strong>in</strong>ches. The 1-½ <strong>in</strong>ch SMA mix<br />

conta<strong>in</strong>ed n<strong>in</strong>e percent lime kiln dust and the ½ <strong>in</strong>ch SMA mix conta<strong>in</strong>ed six percent lime kiln<br />

dust. In less than one year after construction, several are<strong>as</strong> <strong>of</strong> distress were observed. Flush<strong>in</strong>g<br />

<strong>of</strong> the surface w<strong>as</strong> observed, followed by rutt<strong>in</strong>g, shov<strong>in</strong>g, crack<strong>in</strong>g, and potholes. A light tan<br />

powder w<strong>as</strong> evident along the edge <strong>of</strong> pavement <strong>in</strong> the distressed are<strong>as</strong>. Cores taken from the<br />

pavement <strong>in</strong> the distressed are<strong>as</strong> found that the underly<strong>in</strong>g SMA layer w<strong>as</strong> severely stripped. It<br />

w<strong>as</strong> suspected that the lime kiln dust <strong>in</strong> the first layer <strong>of</strong> SMA conta<strong>in</strong>ed excessive amount <strong>of</strong><br />

available calcium oxide. The Alabama Department <strong>of</strong> Transportation subsequently disapproved<br />

LKD <strong>as</strong> a m<strong>in</strong>eral filler for SMA mixtures.<br />

Tex<strong>as</strong><br />

In August 2003, an SMA project w<strong>as</strong> started on SH-105 <strong>in</strong> Sour Lake, Tex<strong>as</strong>. Pav<strong>in</strong>g <strong>of</strong> the<br />

SMA began with a test section on the project located. The construction <strong>of</strong> the SMA test section<br />

w<strong>as</strong> cut short due to extended heavy ra<strong>in</strong>s <strong>in</strong> the area. A few days after the ra<strong>in</strong>, the entire<br />

surface <strong>of</strong> the SMA pavement had turned a grayish white color. The surface <strong>of</strong> the SMA w<strong>as</strong><br />

friable and the test section had to be removed and replaced. The <strong>in</strong>vestigation <strong>of</strong> the failure led<br />

to the m<strong>in</strong>eral filler which w<strong>as</strong> determ<strong>in</strong>ed to be a lime kiln dust. Subsequent tests on samples <strong>of</strong><br />

the LKD from the contractor’s m<strong>in</strong>eral filler silo <strong>in</strong>dicated the LKD conta<strong>in</strong>ed 54 percent<br />

available calcium oxide content, an unusually high amount. The SMA mix design and TSR tests,<br />

which had been conducted several months before, did not <strong>in</strong>dicate any problems. However, lab<br />

tests with the QC samples <strong>of</strong> the SMA did reveal that the mix w<strong>as</strong> reactive <strong>in</strong> water. It w<strong>as</strong><br />

apparent that the characteristics <strong>of</strong> the LKD m<strong>in</strong>eral filler had changed from the time the mix<br />

designs were performed and when the m<strong>in</strong>eral filler w<strong>as</strong> delivered to the contractor’s plant.<br />

Kentucky<br />

In September 2004, a project us<strong>in</strong>g lime kiln dust <strong>in</strong> SMA w<strong>as</strong> completed on AA highway near<br />

Bracken, Kentucky. The mix design conta<strong>in</strong>ed six percent lime kiln dust and the available lime<br />

TRB 2006 Annual Meet<strong>in</strong>g CD-ROM Orig<strong>in</strong>al paper submittal – not revised by author.<br />

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