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Wheelspin July 2012 - Sporting Car Club of SA

Wheelspin July 2012 - Sporting Car Club of SA

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The wedding was on Saturday the 26th <strong>of</strong> March 2011. The<br />

Mustang was finished being assembled the previous weekend.<br />

Still a lot to do during the week to get it wedding ready! Leanne<br />

and I took the car out on the Thursday before the wedding to<br />

Hahndorf. It rained all <strong>of</strong> the way there and back. We suspected<br />

that it was burning a lot <strong>of</strong> oil but we needed to be at the wedding<br />

on Saturday.<br />

The Wedding Ceremony was held at the Botanic Gardens at Mt.<br />

L<strong>of</strong>ty. The Mustang took the groomsmen to the ceremony, the<br />

groom travelled up in a 1989 Porsche Speedster. The bride and<br />

her accompaniment arrived in a pair <strong>of</strong> 1970’s Minis.<br />

The comment from the driver <strong>of</strong> the Porsche was that the Mustang<br />

was blowing a fair bit <strong>of</strong> smoke. We made it back to the reception<br />

and took the Mustang home. Under the bonnet everything looked<br />

ok the breather was hooked up properly, the vacuum lines all in<br />

place. Much head scratching?<br />

A few weeks later, our eldest son Chris was racing his Group N<br />

Mini at Mallala at the Easter Nationals. We took the Mustang to<br />

Mallala to get some miles on it to see if we could bed in the rings<br />

and stop it from smoking. Marion to Mallala and return, 40 litres<br />

<strong>of</strong> petrol and 2 litres <strong>of</strong> oil, we may as well <strong>of</strong> bought a Zeta!<br />

Only one way to fix this, pull the motor out and strip it down, this<br />

is what we did. At first glance all looked good. The pistons and<br />

bores looked ok with some funny marks at the top and bottom<br />

<strong>of</strong> the stroke. All <strong>of</strong> the pistons had large carbon deposits on the<br />

top <strong>of</strong> them. Some <strong>of</strong> the exhaust valves were not seating correctly<br />

due to the carbon build-up in that small number <strong>of</strong> miles driven.<br />

On closer inspection, the rings supplied by the machine shop<br />

were too narrow for the ring grooves in the pistons that they had<br />

supplied. This caused the rings to flutter and flex at the top and<br />

bottom <strong>of</strong> each stroke, hence the marks! We noticed some<br />

strange (for the mileage) wear marks on the main bearings. I<br />

went back and complained to them. They said it was my fault for<br />

not checking the parts and not checking their work. They supplied<br />

new rings but refused to re-hone the bores or <strong>of</strong>fer any<br />

compensation. They advised just re-assemble it. It will be fine.<br />

I took the block, crank, rods and Pistons to Chris Milton Engine<br />

Developments. Sam was very helpful. He diagnosed some other<br />

serious errors made in the machining process. The tunnel bore<br />

thru the main bearings was out <strong>of</strong> tolerance, Pistons assembled<br />

onto con-rods incorrectly, Bores at +20 not bored to specifically<br />

suit the pistons.<br />

I re-lapped the valves in the heads and checked them with<br />

kerosene in a leak down test. (I still think that this is a more<br />

thorough method than applying vacuum to the port).<br />

Reassembly <strong>of</strong> the motor went smoothly. All measurements<br />

checked, all surfaces and components cleaned and checked.<br />

New rings, gaskets, bearings, the extra machining just an extra<br />

$1000.00.<br />

The installation <strong>of</strong> the motor back into the body turned out to be<br />

tricky. The previous installation, went smoothly. This time no<br />

such luck! Exhaust pipes fowling on the chassis rails and on the<br />

steering box. Lift it out, Change the angle <strong>of</strong> approach. Still<br />

fowling! Lift it out again. Same again. Eventually after what<br />

should have been a few minutes dropping the motor in we<br />

managed to have it sitting on its mounts waiting for bolts.<br />

Simple assembly followed. Use up all <strong>of</strong> the parts, use up all <strong>of</strong><br />

the nuts bolts and washers when there are no parts left on the<br />

bench you must be finished! Put fuel in the tank, connect the<br />

battery and crank it over. Oil pressure showing on the gauge,<br />

that’s a good thing, hook up the distributor and try to start it.<br />

The engine fires but doesn’t want to keep running. Lots <strong>of</strong> black<br />

smoke coming from the exhaust. We check the carburettor only<br />

to find that fuel is running out <strong>of</strong> the float bowl straight into the<br />

manifold. This should be easy to fix. A rebuild kit for the Holley<br />

carby is installed. Apparently an easy job made more difficult<br />

because the kit has 7 different gaskets to suit the different models<br />

<strong>of</strong> carby! The gaskets all look the same so unknowingly we<br />

installed the wrong gaskets only to find that the leaking in to the<br />

manifold was now worse than ever.<br />

This is now January 3rd and it looks like the Mustang isn’t going<br />

to make it to Meeting On The Move on Friday. We made a<br />

couple <strong>of</strong> phone calls and found a Holley <strong>Car</strong>by to borrow. The<br />

borrowed item was a different model, hadn’t been on a car in<br />

years but it did show some potential. Stripped threads on the<br />

fuel inlets, more fuel leaking (good thing it’s cheap). Swap some<br />

parts between the two carby’s and try again. This time, success!<br />

The Mustang starts and runs. No black smoke, no blue smoke,<br />

excellent oil pressure, no water leaks, even the troublesome<br />

rear main seal isn’t leaking.<br />

We drive around the block just to be sure that all is ok. We drive<br />

as far as Henley Beach to Chris’s house. It runs fine the engine<br />

temperature is good everything seems fine. The borrowed<br />

carburettor is OK but not quite set correctly. On Wednesday we<br />

took my carby to Allan at Auto <strong>Car</strong>burettor services on Norfolk<br />

Rd at Marion. He did a quick fiddle, checked the unit over, put<br />

in the right gaskets, he called me a goose for getting it all so<br />

wrong!<br />

On Thursday, Chris refitted the correct carby and drove the<br />

Mustang in to Willshire Motor Trimmers as I had returned to<br />

work after what seemed a very short Christmas New Year break.<br />

No excuses now. We had to take the car to Meeting On The<br />

Move.<br />

Home from work on Thursday after work, who would have thought<br />

that a car could get so dirty just sitting in the shed doing almost<br />

nothing? A quick wash and a chamois over and it looks almost<br />

presentable.<br />

to page 17

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