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44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 1<br />

DIESEL HYDROTREATERS REVAMP A WAY FOR<br />

INCREASING PRODUCTION OF NEAR ZERO SULPHUR<br />

DIESEL AND IMPROVING THE ENERGY EFFICIENCY<br />

Dicho Stratiev, Iliya Vergov, Todor Tzingov, Ivelina Shishkova<br />

Lukoil Neftochim Bourgas- R&D Department, 8104 Bourgas, Bulgaria,<br />

e-mail: stratiev.dicho@neftochim.bg<br />

KEY WORDS: near zero sulphur <strong>diesel</strong> ,energy efficiency, hydrotreater <strong>revamp</strong><br />

ABSTACT<br />

The progress of catalyst technologies allowed the <strong>diesel</strong> hydrotreating<br />

units designed <strong>for</strong> <strong>production</strong> of <strong>diesel</strong> with sulphur content of 3 000 ppm to<br />

accommodate <strong>production</strong> of automotive <strong>diesel</strong> with sulphur content of 500,<br />

350, and 50 ppm without need of reconstruction. Even the 10 ppm sulphur<br />

<strong>diesel</strong> was possible to produce only by a reduction of the content of the<br />

refractory sulphur species boiling above 340 0 C from 30 to 15% in the <strong>diesel</strong><br />

hydrotreater feed. However, the <strong>diesel</strong>ization of Europe requires higher volume<br />

of automotive <strong>diesel</strong> <strong>production</strong>. To meet this challenge the Lukoil Neftochim<br />

Bourgas has made a <strong>revamp</strong> of two of its four middle distillate <strong>hydrotreaters</strong><br />

which process heavy <strong>diesel</strong> fractions. The <strong>revamp</strong> consisted of a reduction of<br />

the liquid hourly space velocity (LHSV) from 2.0 and 1.7 to 1.17 and 0.90 h -1 by<br />

adding additional catalyst volume. In order to prevent the possibility of<br />

leakage, observed two years ago, the heat exchangers utilizing the reactor<br />

product heat were replaced. The unit <strong>revamp</strong> was per<strong>for</strong>med within 20 days<br />

and the project was executed (from the start of the basic design preparation to<br />

the final unit reconstruction) within a year. The critical equipment – new<br />

reactors were prepared within less than one year. The per<strong>for</strong>mance test<br />

showed that the <strong>revamp</strong>ed <strong>hydrotreaters</strong> produce 8 ppm sulphur <strong>diesel</strong> at 10 0 C<br />

lower than the design weight average bed temperature (WABT) from a<br />

feedstock that contained 30% fraction boiling above 340 0 C. The saturation of<br />

poly- to mono - nuclear aromatics was increased from 40 to 50% leading to<br />

increase of hydrogen consumption by about 11%. The installation of the new<br />

heat exchangers has resulted in 50% fuel savings.<br />

INTRODUCTION<br />

The near zero sulphur <strong>diesel</strong>(NZSD) had to be available at the petrol<br />

station pump as from 01.01.2009 in the whole European union according to<br />

Directive 2003/17/EC. The preparation <strong>for</strong> <strong>production</strong> of NZSD started in the<br />

Lukoil Neftchim Bulgaria (LNB) refinery much earlier than the mandate date<br />

[1]. However, the achieved improvement in the operation of the existing<br />

middle distillate <strong>hydrotreaters</strong> was not enough to provide 100% <strong>production</strong> of<br />

NZSD. The mandate date of 01.01.2009 was very close and a reconstruction<br />

of the LNB heavy middle distillate <strong>hydrotreaters</strong> HDS-2 and HDS-3 seemed<br />

difficult to implement starting in late 2007. Due to the higher load of the most<br />

manifacturers of special equipment in 2008 the duration of manufacturing of<br />

hydrotreating reactors would not be shorter than 18 months. This meant not<br />

complying with the deadline <strong>for</strong> <strong>production</strong> of NZSD in the LNB. In order to


44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 2<br />

find a solution in this tough situation the technological department and the<br />

research laboratory made estimation about the required catalyst volume<br />

increase necessary to achieve <strong>production</strong> of NZSD in the hydrotreating units<br />

HDS-2 and HDS-3 running on a mixture of heavy straight run gas oil and light<br />

vacuum gas oil from Ural crude. This estimation showed that the liquid hourly<br />

space velocity (LHSV) should be approximately 1.0h -1 if the mixture of heavy<br />

straight run gas oil and light vacuum gas oil from Ural crude is hydrotreated at<br />

a pressure of 35 kg/cm 2 on the Topsoe TK-576 Brim catalyst. This catalyst<br />

proved to be among the best per<strong>for</strong>mers in the ultra low hydrodesulphurization<br />

[1,2]. The LHSV of about 1.0h -1 was possible to achieve if reactors with<br />

dimensions of the LNB FCC feed hydrotreating reactors were installed in the<br />

HDS-2 and HDS-3 units. Drawings of these reactors were available and this<br />

gave the opportunity to shorten the time <strong>for</strong> their manufacture. The LNB<br />

signed a contract with the Haldor Topsoe (HTAS) <strong>for</strong> basic engineering of<br />

reactor section <strong>for</strong> reconstruction of the LNB HDS-2 and HDS-3 units in<br />

November 2007. In late November 2007 HTAS assured LNB that the LNB<br />

FCC feed hydrotreating reactors fit the reconstruction of the HDS-2 and HDS-<br />

3 units and LNB signed a contract <strong>for</strong> manifacturing of the hydrotreating<br />

reactors <strong>for</strong> a period of less than 12 months with the Russian company OOO<br />

Energomash-Atomash. Having the bitter experience with appearance of<br />

leakage in the heat exchangers LNB was aware that the <strong>production</strong> of NZSD<br />

could fail if the older heat exchangers were used [3]. That is why a contract<br />

with the Ukrain company OOO Mashzavod was signed <strong>for</strong> manufacturing of<br />

shell and tube heat exchangers <strong>for</strong> utilization of the energy of the reactor<br />

product stream effluent. The delivery term <strong>for</strong> the heat exchangers was lower<br />

than 12 months. With this tight schedule the HDS-3 was reconstructed and<br />

successfully started up operation in late December 2008.The HDS-2 unit was<br />

reconstructed and successfully started up operation in early March 2009. The<br />

aim of this work is to discuss the achieved operation of the reconstructed LNB<br />

heavy middle distillate hydrotreating HDS-2 and HDS-3 units.<br />

EXPERIMENTAL<br />

The per<strong>for</strong>mance test of the reconstructed LNB HDS-3 was carried out in<br />

December 2008 at following conditions:<br />

- Feedstock properties<br />

Density at 15 °C, kg/m3 851.6-853.5<br />

Distillation, ASTM D 86, o C<br />

- IBP 208-220<br />

- 10% vol% 257-265<br />

- 50% vol% 294-300<br />

- 90% vol% 330-340<br />

- 95% vol% 338-349<br />

- EBP 355-360<br />

Sulfur , wt% 0.66-0.875<br />

Bromine number, g Br2/100 g 0.9-2.8<br />

Total aromatics,% 27.4-29.2<br />

Polynuclear aromatics , % 8.8-9.7


44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 3<br />

- Unit operating conditions:<br />

LHSV, h -1<br />

0.90<br />

First reactor inlet temperature, ºC 350<br />

First reactor outlet temperature, ºC 362<br />

Second reactor inlet temperature, ºC 360<br />

Second reactor inlet temperature, ºC 362<br />

Hydrogen/Oil ratio, Nm 3 /m 3 230<br />

Hydrogen make-up, Nm 3 /m 3 66<br />

Hydrogen content in the make up gas, mole% ≥ 80<br />

The per<strong>for</strong>mance test of the reconstructed LNB HDS-2 was carried out in<br />

March 2009 at following conditions:<br />

- Feedstock properties<br />

Density at 15 °C, kg/m3 854,6-860,9<br />

Distillation, ASTM D 86, o C<br />

- IBP 179-219<br />

- 10% vol% 233-252<br />

- 50% vol% 294-302<br />

- 90% vol% 340-349<br />

- 95% vol% 351-360<br />

- EBP 360<br />

Sulfur , wt% 0.983-1.12<br />

Nitrogen , mg/kg 164 -266<br />

Bromine number, g Br2/100 g 3.35 - 5.68<br />

Total aromatics,% 29.6<br />

Polynuclear aromatics , % 11.1<br />

- Unit operating conditions:<br />

LHSV, h -1<br />

1.17<br />

First reactor inlet temperature, ºC 349<br />

First reactor outlet temperature, ºC 374<br />

Second reactor inlet temperature, ºC 372<br />

Second reactor inlet temperature, ºC 374<br />

Hydrogen/Oil ratio, Nm 3 /m 3 284<br />

Hydrogen make-up, Nm 3 /m 3 76<br />

Quench, Nm 3 /m 3 10<br />

Hydrogen content in the make up gas, mole% 79.5-86


44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 4<br />

RESULTS AND DISCUSSION<br />

During the per<strong>for</strong>mance test of the HDS-3 unit the product (stable<br />

hydrogenate) properties were as follows:<br />

- Product properties<br />

Sulphur , wt ppm ≤ 5<br />

Density at 15 °C, kg/m 3 840.5-843.6<br />

Polynuclear aromatics , % 4.6-5.8<br />

These data indicate that the increase of the catalyst volume by a factor<br />

of 1.9 (decreasing the LHSV from 1.7 to 0.90h -1 ) allowed the LNB heavy<br />

middle distillate hydrotreater HDS-3 to produce NZSD. The hydrogen<br />

consumption was found to be 28.3 Nm 3 /m 3 oil which was 8% higher than that<br />

recorded be<strong>for</strong>e the reconstruction (26.3 Nm 3 /m 3 oil).<br />

During the per<strong>for</strong>mance test of the HDS-2 unit the product (stable<br />

hydrogenate) properties were as follows:<br />

- Product properties<br />

Sulphur , wt ppm ≤ 5<br />

Density at 15 °C, kg/m 3 844-845<br />

Polynuclear aromatics , % 4.6-5.8<br />

These data indicate that the increase of the catalyst volume by a factor<br />

of 1.7 (decreasing the LHSV from 2.0 to 1.17h -1 ) allowed the LNB heavy<br />

middle distillate hydrotreater HDS-2 to produce NZSD. The hydrogen<br />

consumption was found to be 34.2 Nm 3 /m 3 oil which was 14% higher than that<br />

recorded be<strong>for</strong>e the reconstruction (30.1 Nm 3 /m 3 oil).<br />

Figures 1 and 2 present the deactivation of the catalyst TK-576 Brim in<br />

the LNB HDS-3 and HDS-2 heavy middle distillate <strong>hydrotreaters</strong>. It is evident<br />

from these data that the catalyst in HDS-2 unit has exhibited higher<br />

deactivation rate of 3.4 0 C/month, than HDS-3 catalyst whose deactivation rate<br />

is 3.0 0 C/month. With a start of run temperature (SORT) of 350 0 C and end of<br />

run temperature (EORT) of 390 0 C a cycle length of 13 months is obtained <strong>for</strong><br />

HDS-3. With a start of run temperature (SORT) of 349 0 C and end of run<br />

temperature (EORT) of 390 0 C also a cycle length of 12 months is obtained <strong>for</strong><br />

HDS-2. The replacement of the older heat exchangers in both units not only<br />

improved reliability but also improved the unit energy efficiency. The cost <strong>for</strong><br />

fuel gas was reduced by a factor of two.


O C<br />

400<br />

395<br />

390<br />

385<br />

380<br />

375<br />

370<br />

365<br />

360<br />

355<br />

350<br />

345<br />

340<br />

335<br />

330<br />

325<br />

320<br />

315<br />

310<br />

305<br />

300<br />

44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 5<br />

WABTreal WABTnorm Product suphur<br />

0 10 20 30 40 50 60 70 80 90 100 110 120 130 140 150 160 170 180 190 200 210 220 230 240 250<br />

Days of Run<br />

Figure 1 Deactivation of the catalyst TK-576 Brim in the LNB HDS-3 unit<br />

Deactivation rate - 3.0 o C/month<br />

50<br />

45<br />

40<br />

35<br />

30<br />

25<br />

20<br />

15<br />

10<br />

5<br />

0<br />

Product sulphur, ppm


О С<br />

400<br />

395<br />

390<br />

385<br />

380<br />

375<br />

370<br />

365<br />

360<br />

355<br />

350<br />

345<br />

340<br />

335<br />

330<br />

325<br />

320<br />

315<br />

310<br />

305<br />

44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 6<br />

WABT real WABT norm Product sulphur<br />

300<br />

0<br />

0 10 20 30 40 50 60 70 80 90 100 110 120 130 140 150 160 170 180<br />

Days of Run<br />

Figure 2 Deactivation of the catalyst TK-576 Brim in the LNB HDS-2 unit<br />

Deactivation Rate - 3.4 o C/month<br />

50<br />

45<br />

40<br />

35<br />

30<br />

25<br />

20<br />

15<br />

10<br />

5<br />

Product sulphur, ppm


44th International Petroleum Conference, Bratislava, Slovak Republic, September 21-22, 2009 7<br />

CONCLUSIONS<br />

The design and construction of the <strong>revamp</strong> of the LNB heavy middle<br />

distillate hydrotreating units HDS-2 and HDS-3 was implemented <strong>for</strong> a record<br />

short time of 12 months due to the well organized and coordinated work<br />

between the Lukoil Chief engineer department, the licensor of technology<br />

Haldor Topsoe and the manufacturer of reactors and heat exchangers the<br />

Russian company OOO Energomash-Atomash and the Ukrain company OOO<br />

Mashzavod. The units were put on stream according to the planned schedule<br />

and demonstrated stable operation with an expected catalyst cycle length of<br />

12-13 months.<br />

REFERENCE<br />

[1] I. Vergov, I. Shishkova, “Catalyst advances promote <strong>production</strong> of near<br />

zero sulphur <strong>diesel</strong>”, Petroleum & Coal, 51 (2), pp. 136-139, 2009.<br />

[2] D. Stratiev, V. Galkin, K. Stanulov, “Study: Most-active catalyst<br />

improves ULSD economics”, Oil&Gas Journal, Aug.14, pp. 53-56, 2006.<br />

[3] D. Dobrev, D. Stratiev, T. Tzingov, G. Argirov, V. Dyakov, P. Petkov,<br />

“Effect of unreliable <strong>diesel</strong> hydrodesulphurization unit equipment operation<br />

on the <strong>production</strong> of ultra low sulphur <strong>diesel</strong>”, Proc. 43 th International<br />

Petroleum Conference, 2007, Bratislava, Slovac Republic.

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