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Manby H1L15 Breaker Incident - July 5, 2010 - IESO

Manby H1L15 Breaker Incident - July 5, 2010 - IESO

Manby H1L15 Breaker Incident - July 5, 2010 - IESO

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<strong>Manby</strong> <strong>H1L15</strong> <strong>Breaker</strong> <strong>Incident</strong> - <strong>July</strong> 5, <strong>2010</strong>5. System Impact5.4 Impact on GenerationOntario Power Generation and Bruce Power both reported terminal voltage swings at thePickering and Bruce nuclear generating stations, respectively. All units remained stablefollowing each fault experienced at <strong>Manby</strong>.In order for ACE return to normal, a combination of hydro-electric and coal-fired generatorswere verbally dispatched down at 15:41 EST to compensate for the temporary load loss. By16:00 EST, <strong>IESO</strong> software was re-configured to account for the load profile change and allgenerators were returned to automated dispatch.As discussed earlier, the availability of the Portlands Energy Centre allowed for an expeditedload restoration once load transfers were initiated from <strong>Manby</strong> to Leaside supply. More loadwas available for transfer as the Leaside 230 to 115 kV autotransformers were not asthermally restrictive as they would have been if Portlands was unavailable.- End of Section -October 20, <strong>2010</strong> Public 15

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