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A <strong>DISCUSSION</strong> <strong>OF</strong> <strong>THE</strong> <strong>ADVANTAGES</strong> <strong>OF</strong> <strong>CO</strong>-<strong>THICKENING</strong> <strong>OF</strong><br />

PRIMARY AND SE<strong>CO</strong>NDARY SLUDGES IN DISSOLVED AIR FLOTATION THICKENERS<br />

Abstract<br />

Richard Butler, King County Department of Metropolitan Services (Metro)<br />

Richard E. Finger*, King County Department of Metropolitan Services<br />

East Division Reclamation Plant<br />

1200 Monster Rd. S.W.<br />

Renton, WA 98055-2962<br />

Phone (206) 684-2412<br />

Jim Pitts, King County Department of Metropolitan Services<br />

Barbara Strutynski, King County Department of Metropolitan Services<br />

Dissolved air flotation thickeners (DAFTS) are commonly used to thicken waste activated sludge;<br />

however, their use for co-thickening primary and waste activated sludges is not commonly practiced. This<br />

paper describes the results of a full-scale DAFT co-thickening operation. Soluble BOD reduction across<br />

the DAFTS is approximately 80% while soluble <strong>CO</strong>D reduction is approximately 60%. This represents a<br />

reduction in BOD loading to the activated sludge facilities of approximately 4%. In addition, substantial<br />

amounts of fine grit is removed from the primary sludge during the flotation process. Thus, DAFT cothickening<br />

of primary and secondary sludges can significantly reduce secondary organic loading while<br />

concurrently reducing the amount of grit being discharged to the digesters. It also eliminates the need to<br />

independently thicken primary sludge. These impacts lead to reductions in secondary operating costs as<br />

well as reduced operating costs associated with digester cleaning and thickening of primary sludge.<br />

Keywords<br />

Dissolved Air Flotation Thickening, Soluble BOD Removal, Solids Thickening, Grit Removal<br />

Introduction<br />

The East Division Reclamation Plant (EDRP) of King County’s Department of Metropolitan Services<br />

(Metro), which was formerly known as the Municipality of Metropolitan Seattle’s Renton Treatment<br />

Plant, is a secondary activated sludge treatment plant, which was originally constructed in the early<br />

1960’s. The original plant design, which was described by Uhte (1964), did not include solids<br />

processing; all EDRP solids were pumped to Metro’s West Point facility for treatment. The EDRP was<br />

expanded in 1972 to increase its liquid stream capacity from 1.05 m 3<br />

/s (24 mgd) to 1.58 m 3<br />

/s (36 mgd);<br />

however, solid stream processing was again not included. A second expansion, completed between 1985<br />

and 1988, doubled the secondary capacity to 3.15 m 3<br />

/s (72 mgd) and constructed solids handling facilities<br />

for the first time. The solid stream processing facilities included thickening, anaerobic digestion and belt<br />

filter press dewatering.<br />

<strong>576</strong>


As a part of the predesign work for the second expansion, pilot testing of dissolved air flotation<br />

thickening (DAFT) and gravity thickening was conducted. Before solids handling facilities were<br />

constructed at the EDRP, no attempts were made to thicken primary sludges in order to minimize<br />

residence time in the forcemain used to transport solids to West Point. As a result, the plant staff were<br />

interested in evaluating options which would allow the continued rapid withdrawal of primary sludge<br />

from the primary units. DAFT pilot testing therefore included an evaluation of co-thickening of primary<br />

and secondary sludges as well as thickening of secondary sludge alone. The results of that pilot testing<br />

were described by Anwar, Finger, Merrill and Uhte (1983).<br />

The results of the pilot testing suggested several advantages to co-thickening primary and secondary<br />

solids using DAFTS. First, the need for separate thickeners for primary and secondary sludges would be<br />

eliminated, thus reducing the number of operating thickeners and associated capital and operating costs.<br />

Second, DAFT co-thickened sludge produced a higher solids concentration than could be achieved using<br />

gravity thickeners for primary solids and DAFTS for secondary solids. Third, solids loading for cothickening<br />

was twice the normal design loading used for the thickening of secondary solids alone. Thus<br />

no increase in DAFT size was required over that needed for secondary thickening. Fourth, data<br />

suggested the potential for a reduced BOD concentration in the recycle stream, presumably due to the<br />

removal of soluble BOD in the DAFT. Fifth, the data suggested that there was the potential for<br />

coincidental degritting of the primary sludge.<br />

Pilot testing results indicated that DAFT co-thickening would result in the lowest overall operating<br />

costs and the lowest total present worth, even when the potential savings from improved degritting and<br />

BOD removal were ignored. As a result, it was decided to proceed with a design which included cothickening<br />

of primary and secondary sludges using DAFTS even though it was a new operational<br />

concept. The solid stream construction was completed in late 1987. Since solid stream operation was<br />

new to the plant staff, the first several years were spent learning the system operation. In addition, a<br />

number of operational, equipment and control strategy modifications were implemented to improve the<br />

thickening operation. These modifications and initial DAFT performance have been described by Finger,<br />

Grenet, Pitts and Uhte (1992). Since this work was reported, performance has continued to improve<br />

with float solids in the range of 6% or greater being achieved while polymer usage has dropped to the<br />

range of $2.98 per metric ton ($ 2.71 per ton) of solids treated. While efforts to optimize the DAFT<br />

performance are continuing, additional work has been directed towards verifying the results of the pilot<br />

testing with respect to BOD and grit removal. The results of this testing are discussed below.<br />

The design and operation of the DAFTS at the East Division Reclamation Plant has been thoroughly<br />

discussed by Finger, Grenet, Pitts and Uhte (1992); however, a summary is provided below for reference.<br />

Feed to the DAFTS, which is referred to as mixed sludge (MS), is a mixture of the primary and<br />

secondary waste activated sludges, filtrate from the belt filter presses and thickened bottom sludge return.<br />

The thickened bottom sludge return is the centrate from solids which had settled in the DAFTS and<br />

which had been centrifuged to separate the organic fraction from the inorganic fraction. The inorganic<br />

fraction is discharged along with the grit to a collection area from which it was hauled to landfill for<br />

disposal. MS is ground using in-line grinders and discharged to a distribution box which feeds four 17.8<br />

meter (55 foot) diameter circular DAFTS by gravity. Equal flow distribution is achieved using overflow<br />

weirs.


Each DAFT is provided with two float collection troughs located 180 degrees apart with float being<br />

continuously removed by 16 hinged flights which are supported by an eight armed carousel. Float level is<br />

automatically maintained by a level control algorithm which controls the rate at which the clarified liquid,<br />

which is called thickener overflow (TO), is removed. Both the level setpoint and the collector speed can<br />

be varied to help optimize unit operation. Each DAFT has two dedicated air dissolution systems, either<br />

or both of which can be used to maintain the desired air to solids ratio. Polymer is fed to each DAFT,<br />

with the rate controlled automatically based on the turbidity of the TO. TO turbidity is measured using a<br />

Hach surface scatter turbidimenter. Settled solids, which are called thickened bottom sludge (TBS), are<br />

transported to a central hopper by a scraper, which is coupled to the float collectors. The TBS is<br />

processed as described above. The capability to degrit the TBS was incorporated into the design as a<br />

result of the pilot testing, which showed a significant amount of grit in the solids which accumulated on<br />

the bottom of the test unit.<br />

Methodology<br />

Procedures to evaluate BOD and <strong>CO</strong>D removal are relatively easily documented as compared to grit<br />

removal, which depends as much on anecdotal as on quantitative data. The MS and TO samples were<br />

composited on a flow-paced basis. Mixed sludge feed to the DAFTS was sampled using an automatic<br />

solids sampler as described by Finger (1992). The MS sampling rate was proportional to the DAFT feed<br />

rate as measured by two 0.3-meter magnetic flow meters. TO, or clarified subnate, was collected using a<br />

dipper-type sampler which collected a fixed volume sample per volume of flow discharged.<br />

MS and TO were analyzed for total BOD, total <strong>CO</strong>D, soluble BOD and soluble <strong>CO</strong>D. BOD analyses<br />

were performed in accordance with Standard Methods. <strong>CO</strong>D analyses were performed using a modified<br />

version of that described in Standard Methods with digestion time reduced to 20 minutes. The lower<br />

digestion time was based on analytical data which indicated this time was adequate to ensure complete<br />

oxidation of the species present. Soluble portions were prepared by centrifugation and then filtration<br />

through 0.045 m μ membrane filters.<br />

Other analyses were performed on the solid stream processes as a routine part of the plant process<br />

monitoring and control program. Methodologies contained in Standard Methods were utilized in<br />

conducting these analyses. Once the analytical testing was completed, routine monitoring data was<br />

entered into a computerized laboratory data base which was developed by Metro staff. In addition to<br />

storing raw data, this system performed process calculations and provided data retrieval and report<br />

generation capabilities.<br />

Manual probing of the digester, which has been practiced since the digesters were placed in service,<br />

was used to indicate grit and solids carryover from the DAFTS. The probe consisted of a series of rod<br />

sections which could be screwed together to reach the bottom of the digester, which was about 10.7<br />

meters (35 feet) below the cover. The first rod section had a small disk on the end to produce a<br />

resistance as it encounters more dense layers. The rod was inserted into the digesters through access<br />

ports on the floating cover. After the initial resistance of the scum layer, the rod was lowered until a<br />

significant increase in resistance was encountered. The rod was then lowered until the bottom was<br />

reached. The distance between the digester bottom and the depth where resistance increased was defined<br />

as the thickness of the digester bottom sludge accumulation.


Results<br />

Soluble <strong>CO</strong>D and BOD removal across the DAFTS were evaluated over two periods: February 1 to<br />

June 23, 1994, and September 20 to October 24, 1993. These periods represent distinctly different<br />

seasonal periods which should provide some insight into whether organic uptake in the DAFTS is<br />

dependent on seasonal conditions. Only soluble <strong>CO</strong>D analyses were performed before April 17 (first half<br />

of Period One). Both soluble <strong>CO</strong>D and soluble BOD testing were conducted for the remainder of Period<br />

One and all of Period Two. Analyses were seven days per week except during the second part of Period<br />

One when analyses were limited to weekdays. The results of soluble <strong>CO</strong>D testing are summarized in<br />

Table I, while Table II summarizes the soluble <strong>CO</strong>D loading to the DAFTS for the two periods.<br />

Figure 1 presents data for both test periods including MS and TO soluble <strong>CO</strong>D concentrations and<br />

soluble <strong>CO</strong>D removal efficiencies.


.<br />

800<br />

700<br />

600<br />

500<br />

400<br />

300<br />

200<br />

100<br />

0<br />

The results of the soluble BOD testing are summarized in Table III, which includes concentration data<br />

for the two test periods. Table IV summarizes the soluble BOD loading data for the same periods.


solids buildup in the digesters as measured indirectly by probing and directly during digester cleanings,<br />

the comparative volatile content of the DAFT thickened sludge (digester feed) and the DAFT bottom<br />

sludge (TBS), and the primary sludge and TBS quality during extreme storm events.<br />

Manual probing of the digesters has been conducted on a monthly basis since the solids handling<br />

facilities came on-line in 1988. The intent of the probings was to measure solids accumulation in order to<br />

schedule digester cleanings without seriously impacting plant operations. Over the past six years, the<br />

probings have consistently indicated no appreciable solids accumulation in the digester.<br />

Although digester probings had proven “negative”, one digester was drained and cleaned in 1992 to<br />

test the digester cleaning system (which had not been tested since it was installed in 1988) and to verify<br />

the results of the digester probing. A significant accumulation of plastics and rags was found on the<br />

digester bottom. However, only a minor amount of grit was found amongst the accumulated solids. As a<br />

result of the significant amount of plastics and rags found during the first digester cleaning, digester<br />

cleanings have continued on a yearly basis. Two more digesters have subsequently been drained and<br />

cleaned (as a part of the annual digester cleaning routine) and found relatively free of accumulated grit,<br />

though plastics and rags accumulation are a recurring problem. Steps are in progress to address the issue<br />

of rags and plastics through an upgrade to the plant raw sewage screening system.<br />

The comparative volatile content of the THS and TBS is an another indication of the DAFTS<br />

effectiveness at separating grit. Grit settles in the DAFTS and is incorporated in the TBS. TBS is<br />

subsequently recycled through degritting classifiers prior to it’s return to the DAFTS as part of the MS.<br />

The average mass of TBS produced during the test periods was 18,695 kg/d (41,130 lb/d), and the<br />

volatile content of the THS and TBS averaged 80% and 75%, respectively. Assuming the difference in<br />

volatile content represents the amount of grit removed during the co-thickening process, daily grit<br />

removal in the DAFTS averaged approximately 935 kg (2057 lb). This represents about 9% of the total<br />

grit and screenings hauled from the plant on an average day. The grit being remove in the TBS has a<br />

generally fine sandy consistency based on a visual examination of the channel used to convey TBS from<br />

the sampling point to the plant drain. Flushing water is required to move the TBS to the drain and the<br />

resultant agitation results in the separation of the grit from the solids and subsequent settling in the drain<br />

channel.<br />

The effectiveness of the DAFTS to separate grit from primary sludge was demonstrated during an<br />

extreme storm event in November 1990. The EDRP collection system is primarily a separated system<br />

resulting in moderate storm flows. However, significant inflow and infiltration, a result of high water<br />

tables during Pacific Northwest winters, can produce significant peak flows. During a November 1990<br />

storm, which was rated a 100 year event, plant flow peaked at the plant’s maximum hydraulic capacity of<br />

10.5 m 3<br />

/s (240 mgd). These extreme flows significantly reduced the effectiveness of the plant’s aerated<br />

grit removal system. The resulting carryover of grit to the primary system caused a significant drop in the<br />

volatile content of the primary sludge; however, the THS from the DAFTS was not significantly affected.<br />

At the same time, there was a significant increase in the quantity of TBS produced in the DAFTS. It took<br />

several days to return to normal, during which time grit production remained elevated; however, digester<br />

operation was not affected because of the effectiveness of the DAFTS at removing the grit. During the<br />

day of the storm and the following day, the mass of TBS increased by over 27,262 kg (60,000 lbs) while


the volatile content dropped to approximately 60%. The system thus prevented approximately 10,910<br />

kg (24,000 lbs) of grit from reaching the digesters during that storm event alone.<br />

Discussion<br />

A significant reduction in soluble BOD and <strong>CO</strong>D occurred across the DAFTS. Soluble BOD removal<br />

averaged almost 80% or 1387 kg/d (3051 lb/d) during the test period. This removal represents a 3 .6%<br />

reduction in secondary BOD loading, which averaged 38,182 kg/d. The reduction is probably a result of<br />

the biologically active solids from the activated sludge system and the favorable aerobic environment of<br />

the DAFTS. Interestingly, DAFT effluent soluble BOD remained fairly constant though influent soluble<br />

<strong>CO</strong>D varied considerably, which accounted for the change in percent soluble BOD removal.<br />

While BOD removal in the DAFTS represents a significant impact, operating conditions at EDRP tend<br />

to minimize soluble BOD production. First, wastewater temperatures in the Pacific Northwest are lower<br />

than those in much of the country throughout the year, which helps to limit the development of anaerobic<br />

conditions in the collection system and within the plant. Thus, soluble BOD concentrations of the plant<br />

influent and feed to the thickening system can be expected to be lower than in other parts of the country.<br />

Second, primary sludge is removed from the EDRP clarifiers without attempting to achieve thickening.<br />

This tends to minimize the production of soluble BOD associated with anaerobic conditions. In fact,<br />

work done at Metro’s EDRP and West Point facilities found that attempts to thicken sludge in the<br />

primary clarifiers led to a significant increase in primary effluent soluble BOD. Third, gravity thickeners,<br />

if utilized at EDRP, would be expected to promote even more solubilization, resulting in significantly<br />

higher recycle soluble BOD than is encountered at the EDRP. Thus, the soluble BOD removals and<br />

reductions in secondary organic loadings observed at EDRP represent a lower baseline. Potentially much<br />

higher removals and reductions would occur if gravity thickening of primary sludge was practiced.<br />

The reduction in BOD loading to the secondary presents several advantages. First, there would be a<br />

direct reduction in the amount of air required in the secondary process. Using current operating data at<br />

the EDRP, this would translate to an annual savings in electrical cost for aeration of $20,250 based on a<br />

electrical rate of $0.037 / kwh. Savings in other areas of the country where electric rates are significantly<br />

higher would be correspondingly greater. As discussed previously, elimination or avoidance of processes<br />

or procedures which promote BOD solubilization would lead to an even greater savings. Since the<br />

treatment of soluble BOD in the secondary process would result in the production of biological solids, a<br />

reduced solids loading to the secondary clarifiers and reduced pumping of waste sludge, both of which<br />

have either direct or indirect cost savings to the facility, would result from the removal of soluble BOD<br />

during the DAFT thickening process.<br />

In addition to the removal of soluble BOD, DAFT co-thickening results in an improved capture of grit<br />

and thus a reduced rate of grit accumulation in the digesters. The mass of grit being removed under<br />

normal conditions is fairly low at the EDRP, due in part to the separated nature of the collection system.<br />

Operation at the West Point treatment plant, which is on a combined system and which utilizes primary<br />

tanks to thicken the primary sludge, has shown a significant accumulation of grit in the digesters which<br />

necessitates frequent digester cleaning. Personnel from both plants have commented on the significant<br />

difference in the grit accumulation in the digesters of the two facilities. While the average mass of grit<br />

removed was low, the data on storm conditions suggests that there is a significant potential for reducing


grit loading to the digesters as a result of coincidental grit removal during the DAFT co-thickening. The<br />

cost savings associated with reduced digester cleaning frequency and reduced abrasion on downstream<br />

equipment will depend on the magnitude of the problem at each utility. As a consequence, no attempt<br />

has been made to assign a dollar value to this benefit.<br />

Conclusions<br />

Co-thickening of primary and waste activated sludge using dissolved air flotation offers several<br />

opportunities for savings over the separate thickening of the two sludges. Based on pilot testing and full<br />

scale operation, DAFT loading rates can be increased over those conventionally used for thickening of<br />

wasted activated sludge alone so that the total size of the thickeners does not have to be increased<br />

significantly. In addition, the thickened sludge from the co-thickening DAFT operation has a higher<br />

solids concentration than can be achieved using separate gravity thickening for primary solids and DAFT<br />

thickening for secondary solids.<br />

Elimination of the separate primary thickening process has direct cost savings associated with reduced<br />

siteing needs, reduced capital costs and reduced operation and maintenance costs. The elimination of<br />

gravity thickening also has a positive effect in that it avoids the potential for BOD solubilization during<br />

the thickening process with a subsequent increase in secondary BOD loading. Coupled with this is the<br />

enhanced removal of soluble BOD which occurs as a direct result of the mixing of primary and secondary<br />

solids in the DAFT under aerobic conditions. This effect can be enhanced by routing all solid streams<br />

processes having high soluble BOD levels, such as dewatering filtrate or centrate, through the DAFTS.<br />

In addition to helping to eliminate BOD loading on the secondary, the solids removal which occurs<br />

reduces the secondary solids loading associated with the solid area recycle streams. All of these factors<br />

translate into reduced operating costs and improved process reliability.<br />

Coincidental degritting of the primary solids provides another benefit to DAFT co-thickening. The<br />

reduced grit load on the digesters can reduce the accumulation of grit and thus the frequency with which<br />

the digesters must be cleaned. This has advantages from a operational standpoint as well as providing<br />

greater process stability by preventing the need to operate with reduced numbers of digesters and/or with<br />

digesters having reduced active capacity due to grit accumulation. The removal of grit during the<br />

thickening process also serves to limit abrasion on downstream equipment.<br />

While DAFT co-thickening may not be the answer for all treatment plants, there are compelling<br />

reasons related to ease of operation and reduced operating costs why this option should be considered<br />

when new plant deign or upgrade of existing plants is being undertaken. In addition, plants presently<br />

having both DAFTS and gravity thickeners could benefit from the conversion to a DAFT co-thickening<br />

operation. As discussed above, there are a number of operational advantages including the potential for<br />

significant cost savings.<br />

Acknowledgments<br />

The work reported in this paper was performed as a part of the routine operation of the King County<br />

Department of Metropolitan Services East Division Reclamation Plant and could not have been<br />

accomplished without the fill support of the plant’s Operations, Maintenance and Process Control Staff


The authors would especially like to thank the Process Laboratory Specialists, who’s analytical work was<br />

instrumental in documenting the results of this work. A special acknowledgment is extended to Warren<br />

Uhte, the principal designer of the original Renton Plant and the three subsequent enlargements, who<br />

deserves credit for many of the innovations which have helped make the East Division Reclamation Plant<br />

the outstanding facility it is.<br />

References<br />

Anwar, P., Finger, R., Merrill, S. and Uhte, W. (1983) A New Look at Liquid, Solids Separation<br />

Predesign and Design for the Renton Treatment Plant. presented 50th Annual Pacific Northwest Pollution<br />

Control Association Conference.<br />

Finger, R. (1 992) Development and Testing of an On-Line Automatic Sampler for High Solids Samples.<br />

presented Water Environment Federation 65th Annual Conference<br />

Finger, R., Grenet, D., Pitts, J., and Uhte, W. (1992) Metro Seattle Renton Treatment Plant Sludge<br />

Thickening Update.<br />

Standard Methods for the Examination of Water and Wastewater (1989) 17th Ed., Am. Public Health<br />

Assoc., Washington, D.C.<br />

Uhte, W. R. (1964) “Metropolitan Seattle’s Renton Treatment Plant.” Journal Water Pollution Control<br />

Federation, 36, 475 (1964).

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