27.02.2013 Views

NTSB/AAR-84-09 - AirDisaster.Com

NTSB/AAR-84-09 - AirDisaster.Com

NTSB/AAR-84-09 - AirDisaster.Com

SHOW MORE
SHOW LESS

Create successful ePaper yourself

Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.

can pass into tine open space beneath the amenities section from the area beneath the<br />

sink. Thus, if the fit between the trash chute and waste disposal door or between the<br />

chute and trash receptacle had not been secure, it is possible that a lighted cigarette<br />

placed in the chute partition could have fallen from the chute and thereafter rolled or<br />

maSe its way through the hole into the open area below the amenities section. The fact<br />

Lhat debris can enter this area was illustrated by the discovery of the vial and<br />

m8.intenance tag below Flight 797's vanity, w,d the waste materials found in this area on<br />

another air carrier's DC-9. The Safety Board concludes that the possihility thet this<br />

occurred cannot be p:iled out.<br />

To investigate the possibility that the fire was ignited as a result Of a?<br />

overheated flush motor, the Safety Board conducted two tests. The highest temperature<br />

achieved during the tests was 803OF, which was not high enough to ignite isvatory<br />

components in the vicinity of the flush motor. k addition, the izotors used in the tests<br />

were damaged internally by heat. The flush motor involved in the accident did not show<br />

any evidence of internal heat damage or internal failure.<br />

In order for the flush motor to overheat in service, three ma!functions must<br />

take place: the motor must seize; the flush button must be held in or fail in the<br />

depressed, or power on, position; ard finally, the timer must either be defective or fail.<br />

(A properly functioning timer will limit the flash motor to a LO-second cycle even if the<br />

flush button is held in the depressed position. Once the timer cycles the motor off, the<br />

flush button must be released and then depressed again to restart tne motor.) The<br />

recovered components of the timer circuitry were tested functionally after the accident<br />

and were found to be operationel.<br />

The last known person to use the lavatory did so about 35 to 40 minutes before<br />

the fire was detected. She stated that the flush motor worked properly at that time. She<br />

also stated that another passenger was waiting to enter the lavatory when she left;<br />

therefore, the Safety Board conciudes that the flush motor was operating normally within<br />

35 to 40 minutes before the fire was Ciscovered. Given the facts that (1) the test<br />

demonstrated that an overheated flush motor would not produce temperstures high enocgh<br />

to ignite edjacen: lavatory materials; (2) evidence showed that the flush motor had not<br />

failed internally and was not damaged internally by heat: (3) there was no evidence to<br />

indicate that tke flush motor timer had failed; and (4) the flush motor was most probably<br />

operating normally before the fire was discovered, the Safety Board cor,c!udes it uniiely<br />

that the flush motor was the source of ignition of the fire.<br />

Another possible source of ignition Fear the area where the fire was<br />

discovered was the flush motor wiring harness. The tripping of the three circuit breakers<br />

accompanied by the arcing sounds recorded by the CVR occurred at 1851:14. The three<br />

circuit breakers tripped almost simultaneously indicating that the circuitry of all three<br />

phases shorted at the same time. The only evidence of wiring damage was found where<br />

the flush motor wiring harness passed through the lightening hole in the partition between<br />

the amenities section and the toilet section of the lavatory. The damage noted in the<br />

wiring harnes et this location could only have been the result of fire and heat, and the<br />

Safety Board concludes :hat the damage ?o the wiring which caused the three &ash motor<br />

circllit breakers to Pip was caused by heat md fire.<br />

numerous arcing sounl;s were recorded on the CVR. The.:e sounds were accompanied by<br />

Beginning 3 minutes 2 seconds before the 'hree circuit breakers tripped,<br />

voltage fluctuetions and the electrical components whic!. showed these fluctuations, as<br />

well as the flush motor, were ell powered by the right LC. bus. Because of the extensive

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!