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Akron Water Pollution Control Station No Feasible Alternative

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Table 4-2<br />

Secondary Treatment System Loadings<br />

(Based on 1994 Baseline Year Data)<br />

90 MGD 110 MGD 150 MGD 200 MGD<br />

Raw BOD5 (mg/l) 108 100 80 70<br />

Primary Effluent BOD5 (mg/l) 60 60 56 56<br />

Aeration Basin Loading (lbs/day) 45,036 55,044 70,056 93,408<br />

A.B. Unit Loading 1 (lbs./day/1,000 cf) 13.0 15.9 20.0 27.0<br />

Final Settling Tank Surface Overflow Rate (SOR) 2<br />

636 778 1,060 1,414<br />

FST Solids Loading 3 (lbs./day/sf) 12.2 14.9 20.3 27.1<br />

1 Aeration basin total volume = 3,444,000 cf<br />

2 Final settling tank total surface area = 141,400 sf<br />

3 Based on 15% RAS rate<br />

Based on the above data, and projecting from 2006 Stress Test simulated results, it may be<br />

possible to meet effluent parameters, with the likely exception of NH3-N, at flows exceeding 150<br />

MGD. Aeration Basin and Final Settling Tank hydraulic limitations would need to be addressed.<br />

Influent flow records for the established 1994 baseline year were reviewed to determine the<br />

number of days flow exceeded the 110 MGD secondary treatment capacity, and the higher<br />

capacities being reviewed in this report. The year 1994 data was also compared with Years<br />

1995 to 2005 to further support use of 1994 data as the baseline year. A summary of these<br />

reviews is presented in Tables 4-3 and 4-4.<br />

Table 4-3<br />

1994 <strong>Akron</strong> WPCS Influent Flow<br />

Yearly Average MGD Maximum MGD Minimum MGD Secondary Bypass<br />

Influent Days >110 22 Days >110 98 Days 120 17 Days >120 86 Days 130 12 Days >130 72 Days 170 4 Days >170 42 Days 210 2 Days >210 19 Days 275 0 Days

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