06.02.2014 Views

Float technology progress - Riser - Argo

Float technology progress - Riser - Argo

Float technology progress - Riser - Argo

SHOW MORE
SHOW LESS

Create successful ePaper yourself

Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.

Recent Technical Developments with <strong>Argo</strong> <strong>Float</strong>s<br />

Stephen <strong>Riser</strong><br />

University of Washington<br />

riser@ocean.washington.edu<br />

• Apex air pump solenoid problems<br />

• First tests of ARGOS-3<br />

• Pressure sensor updates<br />

• SBE conductivity drift


Air pump (back)<br />

Air pump (front)<br />

The Apex air pump is used to<br />

inflate the air bladder at low<br />

pressures (< 100 dbar) so that the<br />

float rides on the sea surface with<br />

the antenna well out of the water.


UW- added PCB<br />

solenoid<br />

The air pump is controlled by a solenoid (switch), shown above. For<br />

reasons unknown, a number of these solenoids (cost: < $100) have failed<br />

in laboratory tests at UW in recent months. A failure in the field would<br />

mean the air bladder would not inflate, resulting in possible loss of the<br />

ability to communicate with a satellite. This is especially problematic for<br />

Iridium floats.


ACTIONS<br />

(1) The cause was found (by D. Swift) to be an inability of the solenoid to latch<br />

closed over the duration of an applied transient current. If the duration of the<br />

transient current was increased, the solenoid would always latch properly. There<br />

are no known changes in the controller electronics or the solenoid itself that<br />

would lead to this problem.<br />

(2) The problem can be corrected by adding a small, inexpensive (< $50) printed<br />

circuit board near the solenoid that regulates the current to the solenoid and<br />

insures that it always opens and closes on command. The board was designed<br />

by D. Swift, and 100 units were built commercially in Seattle. This fix has been<br />

added to all UW and PMEL floats since February 2011.<br />

(3) Individual floats can be tested for this problem by connecting a laptop prior<br />

to deployment and inflating the bladder.<br />

(4) Teledyne/Webb has been notified of this problem and the suggested remedy.<br />

As of March 1 2011 they have NOT instituted this remedy, and they continue to<br />

build and ship floats with this potential problem. It is not clear whether or not<br />

they intend to add the auxiliary PCB in their production process.


FIRST TESTS OF ARGOS-3 PMT:<br />

• UW has developed a prototype float that uses a Kenwood PMT to<br />

communicate with ARGOS-3 satellites. Reasons to do this: (1) ARGOS-3 will<br />

someday provide bidirectional communications, a possible alternative to<br />

Iridium; (2) the Seimac PTT used in Apex floats is no longer being<br />

manufactured, so alternative communication methods for Apex ARGOS floats<br />

need to be explored.<br />

• First tests of the Kenwood PMT have shown that energy use is larger than<br />

with present ARGOS-2 PTTs. The PMT float has been running on a simulator<br />

at UW for several months. The PMT consumes more than twice the energy per<br />

transmission of the present ARGOS-2 Seimac PTT or Telonics PTT units.


SeaBird CTD ISSUES:<br />

• SBE claims the microleak problem is now understood and fixed at the<br />

Druck factory. The glass/metal seals that caused the problem have been reengineered.<br />

These new sensors will be installed in SBE float CTDs<br />

beginning in July 2011. Until then, SBE is screening all Druck pressure<br />

sensors that are installed in float CTD units (possibly resulting in continued<br />

reduced production of CTD units).<br />

• SBE continues its warranty return program for CTDs with documented<br />

microleak or snowflake problems. A number of <strong>Argo</strong> groups have already<br />

received compensation. See the SBE website for details.<br />

• Kistler pressure sensors: some groups have tried these in tests (SIO, UW,<br />

PMEL, ??) with good results so far in a limited number of floats for a limited<br />

time. SBE claims laboratory tests show the Kistler sensor to be as good as<br />

or better than the new Druck sensors.<br />

• Conductivity drift: both Jamstec and PMEL have noted floats with<br />

unacceptable conductivity drift after deployment (>0.01 PSU equivalent).<br />

This problem was traced to erosion of the platinum in the CTD electrodes.<br />

The cause of the problem has been found and new QC procedures have<br />

been installed at SBE. It is believed that this problem occurred in an<br />

isolated group of floats (CTDs built late in 2010) but all groups should<br />

check for this.

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!