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REDUCTION OF BOILER STACK PARTICULATE EMISSIONS <br />

AND SCRUBBER WATER FLOW USING LOW-SODIUM COAL <br />

BY: <br />

DONALD D. HILL <br />

ENGINEERlNG & MAINTENANCE MANAGER <br />

FORT MORGAN FACTORY <br />

WESTERN SUGAR COMPANY <br />

18317 HWY. 144, FORT MORGAN, CO., 80701 <br />

AND <br />

PATRICIA R. FULLER-PRATT <br />

MANAGER OF ENVIRONMENTAL AFFAIRS <br />

WESTERN SUGAR COMPANY <br />

1700 BROADWAY, SUITE 1600, DENVER, CO., 80290 <br />

ABSTRACT<br />

Two 1947 coal-fired stoker <strong>boiler</strong>s, using a low-pressure mid-1970's design venturi <strong>scrubber</strong>, were<br />

able to demonstrate compliance at one-half the regulated limit <strong>and</strong> less than 0.1 Ib/MMBTU by<br />

converting to a low-sodium coal. The sodium content in coal impacts the <strong>particulate</strong> <strong>emissions</strong> <strong>and</strong><br />

is the cause <strong>of</strong> higher <strong>particulate</strong> <strong>emissions</strong> <strong>and</strong> higher opacity. Analysis indicates that the sodium<br />

content must be less than 2.5 percent, or the ash to sodium ratio must be greater than 40, to be<br />

effective in reducing <strong>particulate</strong> <strong>emissions</strong> <strong>and</strong> opacity. The higher ash content provides sites to<br />

absorb or attach the sodium in the <strong>boiler</strong> without overloading the pollution control devices. The<br />

increased ash bed also insulates the grates <strong>and</strong> allows for better combustion efficiency.<br />

305


INTRODUCTION<br />

Voluntary compliance tests for <strong>particulate</strong> <strong>emissions</strong> were performed in October <strong>of</strong> 1995 at the<br />

Western Sugar Company's Fort Morgan sugar beet processing plant.<br />

The <strong>boiler</strong>house contains two Babcock & Wilcox stoker-fired <strong>boiler</strong>s. The units were placed in<br />

service in 1947 <strong>and</strong>, except for a short time using natural gas, have used Detroit Stoker stokers as<br />

the coal-firing system. Each <strong>boiler</strong> has an American St<strong>and</strong>ard Series 361 fly-ash collector <strong>and</strong> an<br />

in-house (Great Western Sugar Company) designed low-pressure venturi <strong>scrubber</strong>. Exhaust gas<br />

streams from each <strong>boiler</strong> are combined in a common <strong>stack</strong> which has a chevron-type mist<br />

eliminator.<br />

BOILER STACK TESTS - 22 OCTOBER 1995<br />

Normal intercampaign maintenance was performed on the <strong>boiler</strong> equipment <strong>and</strong> the Detroit Stoker<br />

field service representative "tuned" the <strong>boiler</strong> combustion system the week prior to the October<br />

1995 tests. The <strong>particulate</strong> emission limit is 0.14 Ib.lMMBTU. The first day's test results were<br />

under the limit (see Table 1). The second day the limit was exceeded twice <strong>and</strong> the average for the<br />

three compliance runs was 0.16 Ib.lMMBTU. The information was presented to the State <strong>of</strong><br />

Colorado under the State's program <strong>of</strong> voluntary disclosure <strong>and</strong> a second test was scheduled as<br />

quickly as possible. Also, several <strong>boiler</strong> consultants were contacted to observe the compliance<br />

retest.<br />

TABLE 1 <br />

OCTOBER STACK TESTS <br />

PARTICULATE EMISSIONS <br />

OCTOBER 2 AND 3; 1995 <br />

ITEM RUNNO.1 RUNNO.2 RUN NO.3 AVERAGE<br />

Boiler No.1<br />

PLUG<br />

CONE<br />

250 gpm<br />

285 gpm<br />

250 gpm<br />

280 gpm<br />

250 gpm<br />

280 gpm<br />

250 gpm<br />

282 gpm<br />

Boiler No.2<br />

PLUG<br />

CONE<br />

280 gpm<br />

260 gpm<br />

275 gpm<br />

250 gpm<br />

275 gpm<br />

250 gpm<br />

277 gpm<br />

253 gpm<br />

PARTICULATE<br />

EMISSIONS<br />

(lb.lMMBTU)<br />

0.128<br />

0.189<br />

0.163<br />

0.160<br />

306 <br />

- - .... - -­


RETESTS - 15 NOVEMBER 1995<br />

The coal supplier provided a consultant to review the coal as-delivered <strong>and</strong> as-fired, <strong>and</strong> also to<br />

observe the <strong>boiler</strong> operation. Detroit Stoker provided the same technician who was on site in<br />

October to "tune" the <strong>boiler</strong>s. He also observed the <strong>boiler</strong> operation during the tests in order to<br />

advise us if any mechanical problems may have developed. A <strong>scrubber</strong> manufacturer was contacted<br />

to observe the venturi <strong>scrubber</strong> operation during the tests <strong>and</strong> to inspect it prior to the tests. This<br />

individual had been previously employed as a "<strong>stack</strong> tester" <strong>and</strong> also observed the <strong>stack</strong> testing<br />

company during the compliance runs.<br />

The November tests were run with more <strong>scrubber</strong> <strong>water</strong> flow, higher pressure drops across the<br />

<strong>scrubber</strong>, but no "h<strong>and</strong>s-on" operation by any <strong>of</strong> the consultants. The average <strong>of</strong> the three<br />

compliance runs for <strong>particulate</strong>s was 0.271 Ib.lMMBTU (see Table 2), which is nearly twice the<br />

permitted limit.<br />

TABLE 2<br />

NOVEMBER STACK TESTS<br />

P ARTICULATE EMISSIONS<br />

NOVEMBER 15 AND 16, 1995<br />

ITEM RUN NO.] RUN NO. 2 RUN NO.3 AVERAGE<br />

Boiler No.1<br />

PLUG 335 gpm 334 gpm 333 gpm 334 gpm<br />

CONE 340 gpm 338 gpm 337 gpm 338 gpm<br />

Boiler No.2<br />

PLUG 323 gpm 321 gpm 328 gpm 324 gpm<br />

CONE 335 gpm 332 gpm 332 gpm 333 gpm<br />

PARTICULATE<br />

EMISSIONS<br />

(lb. / MMBTU) 0.269 0.280 0.265 0.271<br />

SODIUM<br />

EMISSIONS<br />

(lb. / MMBTU) 0.110 0.123 0.122 0.118<br />

SODIUM OXIDE<br />

(% in ASH) 8.015 6.685 8.05 7.58<br />

During the tests, the opacity <strong>of</strong> the <strong>stack</strong> was observed (not using Method 9) by all the consultants<br />

<strong>and</strong> a "blue haze" was evident after the vapor break <strong>of</strong> the "plume". The coal consultant suggested<br />

that the "blue haze" might be due to sodium <strong>and</strong> was a condition he had observed before with<br />

Northern Powder River Basin coal. The <strong>scrubber</strong> consultant agreed that this was possible, <strong>and</strong><br />

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suggested that a sub-micron sodium fume would pass through a low-pressure venturi <strong>scrubber</strong>. He<br />

suggested that we analyze the <strong>particulate</strong> catch for "sodium". This analysis by the <strong>stack</strong> testing<br />

company averaged 0.118 lb. Sodium/MMBTU, which is nearly 90% <strong>of</strong> the permitted limit. An<br />

analysis <strong>of</strong> the coal as-fired for sodium oxide, averaged 7.58% sodium oxide in the ash. When the<br />

coal shipments were reviewed for the 1995-1996 campaign (see Table 3), the percent sodium in the<br />

ash during the October test was around 4.0% <strong>and</strong> the highest values -- 7.0% to 8.0% -- occurred<br />

during the November test. The consultants agreed that the <strong>boiler</strong>s were performing correctly <strong>and</strong><br />

that the coal was the biggest contributor to the problem.<br />

TABLE 3<br />

COAL SIDPMENT DATA FOR 1995-1996 CAMPAIGN<br />

Date <strong>of</strong> lb/MMBTU % Ash % Sodium Calculated % Sulfur<br />

Shipment<br />

Ratio<br />

9/17/95 9,309 4.37 4.5 22.22 0.33<br />

9/24/95 9421 4.55 4.95 20.2 0.41<br />

9/29/95 9379 4.58 4.5 22.22 0.34<br />

10/3/95 9427 3.97 4.21 23.75 0.37<br />

10/4/95 9356 4.29 4.45 22.47 0.35<br />

10/11 /95 9438 3.79 5.32 18.8 0.35<br />

10113/95 9467 3.85 4.41 22.68 0.34<br />

10118/95 9244 4.5 3.91 25.58 0.33<br />

10/22/95 9553 3.98 5.19 19.27 0.3<br />

10/28/95 9407 3.82 4.42 22.62 0.34<br />

10/30/95 9368 4.13 6.74 14.84 0.3<br />

10/30/95 9377 4.71 6.44 15.53 0.36<br />

1114/95 9420 4.15 7.07 14.14 0.35<br />

11111195 9475 3.74 7.89 12.67 0.32<br />

11116/95 9453 3.96 8.35 1l.98 0.34<br />

11119/95 9612 4.42 5.19 19.27 0.33<br />

11122/95 9485 4.08 5.83 17.15 0.34<br />

11127/95 9328 4.47 4.62 2l.64 0.34<br />

12/2/95 9383 4.07 5.02 19.92 0.3<br />

12/7/95 9463 4.46 5.63 17.76 0.45<br />

12111/95 9222 4.37 6.57 15.22 0.33<br />

12114/95 9424 3.81 7.38 13.55 0.33<br />

12117/95 8795 4.6 1.47 68.03 0.15<br />

12/22/95 9442 3.6 5.26 19.01 0.32<br />

12/26/95 9434 3.94 5.09 19.65 0.35<br />

AVERAGES 9387 4.17 5.38 20.81 0.33<br />

308<br />

_ .-._---_..- .-... - - ­


ENGINEERING TESTS - 21 DECEMBER 1995<br />

A source for ]ow-sodium coal was found in the Southern Powder River Basin <strong>and</strong> a test burn <strong>and</strong><br />

compliance test were arranged for December 21, 1995. These tests were not full compliance tests<br />

but were engineering-level tests only meant to test the "sodium in the coal" theory. Also, these tests<br />

were observed by a representative <strong>of</strong> the Colorado Department <strong>of</strong> PubEc Health <strong>and</strong> Environment,<br />

as were the November tests. However, no consultants were present. The <strong>scrubber</strong> <strong>water</strong> flows were<br />

returned to the levels <strong>of</strong> the October test (see Table 4) <strong>and</strong> the <strong>particulate</strong> <strong>emissions</strong> were an average<br />

<strong>of</strong> 0.09 IbIMMBTU, which is ]ess than 65% <strong>of</strong> the permit limit <strong>of</strong> 0.14 Ib.lMMBTU. Unfortunately,<br />

we were ten days away from the end <strong>of</strong> campaign <strong>and</strong> a full compliance test could not be scheduled<br />

until the start <strong>of</strong> the 1996 -1997 campaign.<br />

TABLE 4<br />

DECEMBER STACK TESTS ("ENGINEERING TESTS") <br />

PARTICULATE EMISSIONS <br />

DECEMBER 21, 1995 <br />

ITEM RUN NO.1 RUN NO.2 AVERAGE<br />

Boiler No.1<br />

PLUG 200 gpm 200 gpm 200 gpm<br />

CONE 200 gpm 200 gpm 200 gpm<br />

Boiler No.2<br />

PLUG 195 gpm 200 gpm 198 gpm<br />

CONE 200 gpm 200 gpm 200 gpm<br />

PARTICULATE<br />

EMISSION S<br />

(lb.lMMBTU) 0.087 0.085 0.09<br />

CALCULATION MISCONCEPTION<br />

Research at another Western Sugar factory regarding opacity suggested that an Ash to Sodium-inthe-Ash<br />

ratio <strong>of</strong> 48 or better at that factory would produce an opacity <strong>of</strong> about 10%. The consultant<br />

suggested a b ~ end <strong>of</strong> "high" <strong>and</strong> "low" sodium coals to reduce opacity at that factory. However,<br />

that consultant felt that sodium wou1d not contribute much to <strong>particulate</strong> <strong>emissions</strong> (which proved<br />

incorrect in our testing at Ft. Morgan).<br />

The consultant's report attempted to establish the Ash/Sodium ratio by using lb. AshlMMBTU <strong>and</strong><br />

lb. Sodium/MMBTU. Basically, this is mathematically incorrect. In order to calculate each <strong>of</strong> these<br />

numbers <strong>and</strong> then take the ratio you have essentially canceled out the units <strong>and</strong> the ratio is really<br />

one (1) divided by the Sodium in the Ash percentage expressed as a number, i.e. 2.5% Sodium in<br />

the Ash is equal to 0.025. Therefore, 1/0.025 = 40. For the Ft. Morgan factory, we developed a<br />

309


conservative estimate that a coal with an Ash to Sodium in the Ash ratio <strong>of</strong> greater than 40, or a<br />

Sodium in the Ash content <strong>of</strong> less than 2.5 %, would achieve compliance.<br />

COMPLIANCE AND ENGINEERING TESTS - 22 OCTOBER 1996<br />

A low-sodium Southern Powder Ri ver Basin coal was contracted for the 1996-1997 beet campaign.<br />

A compliance test was conducted on October 22, 1996 (see Tabl 5). The results averaged 0.072<br />

Ib.lMMBTU, which is well below the 0.14 Ib.lMMBTU <strong>particulate</strong> emission limit.<br />

TABLES<br />

OCTOBER 1996 COMPLIANCE DEMONSTRATION STACK TEST<br />

PARTICULATE EMISSIONS<br />

OCTOBER 22,1996<br />

ITEM RUN NO.1 RUN NO.2 RUN NO.3 AVERAGE<br />

Boiler No.1<br />

PLUG 210 gpm 211 gpm 210 gpm 210 gpm<br />

CONE 208 gpm 209 gpm 207 gpm 208 gpm<br />

Scrubber Diff. Press. 5.8 in. H 2 O 5.6 in H 2 O 5.9 in H 2 O 5.8 in H 2 O<br />

Boiler No.2<br />

PLUG 199 gpm 214 gpm 211 gpm 208 gpm<br />

CONE 199 gpm 204 gpm 214 gpm 206 gpm<br />

Scrubber Diff. Press 5.6 in. H 2 O 5.6 in H 2 O 5.6 in H 2 O 5.6 in H 2 O<br />

PARTICULATE <br />

EMISSIONS <br />

(lb.lMMBTU) 0.079 0.066 0.070 0.072 <br />

After the compliance tests were completed, the <strong>water</strong> flows to the <strong>scrubber</strong> plug <strong>and</strong> cone <strong>and</strong> the<br />

venturi plug placement were varied in order to establish parameters which could be tested in order<br />

to prove compliance using parmetric monitoring for the Title V Operating Permit. A total <strong>of</strong> eight<br />

engineering tests were performed at four different <strong>water</strong> flows <strong>and</strong> lor pressure differentials (two<br />

tests at each level).<br />

~<br />

The <strong>water</strong> flowrates for the plug <strong>and</strong> cone <strong>of</strong> the venturi were varied from 200 gpm to 150 gpm to<br />

100 gpm <strong>and</strong> the pressure drop was changed from 5.0, 4.0, to 3.0 in. H 2 0. The idea was to vary the<br />

<strong>water</strong> flow <strong>and</strong> hold the pressure drop constant to simulate a condition <strong>of</strong> loss/<strong>reduction</strong> <strong>of</strong> <strong>water</strong><br />

flow (pump belt slippage, pat1ial blockage or some other reason). The pressure drop was varied<br />

while holding the <strong>water</strong> flow constant in order to simulate a loss in air flow (a mechanical problem<br />

with the fans or their steam-turbine drivers, a damper problem or some other reason). The<br />

variations all worked, except the 3.0 in. H 2 0 pressure drop setting, which required decreasing the<br />

<strong>water</strong> flow by 50 gpm in order to get the pressure to drop even though the venturi plug had been<br />

lowered to its lowest point. As the results show (see Table 6), the <strong>water</strong> flow variation tests had<br />

310


<strong>particulate</strong> <strong>emissions</strong> <strong>of</strong> 0.072, 0.076 <strong>and</strong> 0.078 lb.lMMBTU <strong>and</strong> the pressure drop <strong>particulate</strong><br />

emission rates were 0.072, 0.09 <strong>and</strong> 0.088 lb.lMMBTU.<br />

TABLE 6<br />

OCTOBER 1996 "ENGINEERING" STACK TEST<br />

PARTICULATE EMISSIONS VARYING WATER IiLOW & PRESSURE DIFFERENTIAL<br />

OCTOBER 23 & 24, 1996<br />

VARYING WATER FLOW<br />

VARYING PRESSURE<br />

ITEM RUN NO.1 RUN NO.2 RUN NO.3 RUN NO.4<br />

Scrubber Water Flow<br />

PLUG & CONE #1 307 gpm 214 gpm 414 gpm 300 gpm *<br />

PLUG & CONE #2 309 gpm 211 gpm 412 gpm 296 gpm *<br />

Scrubber Differential Pressure<br />

BOILER N O. 1 5.5 in. H 2 0 4.9 in H 2 0 4.4 in H 2 0 3.4 in H 2 0<br />

BOILER N O. 2 5.3 in. H 2 0 5.0 in H 2 0 4.1 in H 2 0 3.3 in H 2 0<br />

Particulate Emissions<br />

(lb.lMMBTU) 0.079 0.066 0.070 0.072<br />

These engineering tests showed that there is a wide operating window for the <strong>scrubber</strong>s when using<br />

a low-sodium coal. It appears that low <strong>water</strong> flowrate <strong>and</strong> a small pressure drop will still allow the<br />

<strong>boiler</strong>s to operate below their <strong>particulate</strong> permit limit <strong>of</strong> 0.14 Ib.lMMBTU.<br />

CONCLUSIONS AND BENEFITS<br />

The Fort Morgan factory is in compliance with <strong>boiler</strong> <strong>particulate</strong> limits when it uses low-sodium<br />

coal. The Fort Morgan factory can successfully demonstrate on-going compliance by monitoring<br />

the following parameters:<br />

• COAL SUPPLY<br />

Maintain a record <strong>of</strong> the coal analysis <strong>of</strong> each shipment <strong>of</strong> coal to the factory <strong>and</strong> verify<br />

that it is less than 2.5% Sodium in the Ash. (Ash/Sodium ratio <strong>of</strong> greater than 40).<br />

• SCRUBBER WATER FLOW<br />

Keep the <strong>water</strong> flow to each venturi plug above 100 gpm <strong>and</strong> 100 gpm to each venturi<br />

cone. These are recorded continuously on a strip chart recorder.<br />

311


• SCRUBBER PRESSURE DIFFERENTIAL <br />

Set the venturi plug at a point to maintain at least 2.5 in. H 2<br />

0 or more <strong>of</strong> pressure drop for<br />

each venturi <strong>scrubber</strong>. The pressure drops are also continuously recorded on strip chart<br />

recorders in the <strong>boiler</strong> control room.<br />

BENEFITS<br />

1. The original <strong>scrubber</strong> <strong>water</strong> flowrates had a "design" need for 800 gpm for each <strong>scrubber</strong><br />

system or 1600 gpm for both, which all ended up in the ash pond. This flow has now<br />

been reduced to 200 gpm to 250 gpm for each system or 400 gpm to 500 gpm, a total<br />

savings <strong>of</strong> 1100 + gpm.<br />

2. By having a thicker ash bed, the combustion air entry points can be redirected to have<br />

the undergrate air decreased as the grates are better insulated <strong>and</strong> the overfire air<br />

increased to "lower" the flame <strong>and</strong> improve 02 addition in the suspended- burning zone.<br />

3. With better air flow distribution, even though the BTU content <strong>of</strong> the low-sodium coal is<br />

less than that <strong>of</strong> the previous higher-sodium coal, the combustion efficiency has<br />

improved <strong>and</strong> coal consumption is less (about 30 + tons per day).<br />

4. Post campaign <strong>boiler</strong> cleanup is easier <strong>and</strong> quicker, as the lower sodium coal does not<br />

"slag" as much <strong>and</strong> the slag that does form appears s<strong>of</strong>ter <strong>and</strong> easier to remove.<br />

312

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