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Legacy Progress Director's Production of Documents (Part 3 ... - NCUC

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Duke's Coal Gasification Plant Slanimed for High Costs'EnergyBiz, 7-4-12Barry GassellConsumer and environmental groups recently filed testimony at the Indiana Utility RegulatoryCommission (IURC) opposing the proposed'settlement between Duke Energy (NYSE: DUK), the:Indiana Office <strong>of</strong> Utility Consumer.Counselor, Nucor Steel and the Duke.Energy Indiana IndustrialGroup regarding the Edwardsport' integrated gasification combiried-cycle. (IGGC) power plant.The proposed settlement claims to pfotecf the captive ratepayers <strong>of</strong> Duke by placing a $2.595bn"hard cap" on the construction costs that could be passed onto ratepayers, said the groups in a July 2public statement. However/the expert testimony <strong>of</strong> both David Schlissel, President <strong>of</strong> SchlisselTechnicalConsulting, and Ralph Smith, Senior Regulatory Cprisu Ita nt at Larkin & Associates PLLC,provides evidence thatthe $2.595bn:"cap: , -is nothing more ; than:;a 'firm flooP' that <strong>of</strong>fers consumers 1iittle protection, they added 1 .Also, the proposed settlement ensures that captive ratepayers will in fact pay a minimum total <strong>of</strong>$3.25bn for the coal-fueled, in : cphsfructioh.|GCG project whethef or not if in fact ever comes online."The settlement also rewards Duke Energy for its gross mismanagement and ordinary •mismanagement <strong>of</strong> the project.by giving the Company significantly more than the original $1.985:billion estimate," the groups said."The proposed Settiement Agreement <strong>of</strong>fers no protection for ratepayers" against the likelihood thatthe Edwardsport project will not operate; at or near the annual 84% avaiiability, and approximateannual 82-83% capacity, factors, which; Duke has claimed since 2007 that if would achieve; Schlisselstated in prerfiled testimony.^Smith's testimohy discusses the t fact that the $2:595bn is not aH that customers will pay to completethe construction <strong>of</strong>the project.shouid.the^terms/initheproposed' settlement be accepted by the IURC',given that Construction Work in <strong>Progress</strong> (CWIP) finance related.costs that Duke already collectedfrom ratepayers is not inciuded inithe settiement.inor are.'future&WiP finance related charges.Additional testimony was also filed at the : IURC by Nachy Kahfer, Deputy Director for the CentralRegion <strong>of</strong> the Sierra Club: Beyond Coal to Clean Energy Campaign. Kanfer points out the claimedfailure <strong>of</strong> Duke Energy to propose any plan to mitigate carbbh emissions.Hearings on the proposed settlement are scheduled to. begin on July 16.In a May SO filing at the: commission, Duke sakithat within a subdocket; the settling parties are askingthe.commission to:;- approve a new cost estimate for the IGCC project, .equivalent to the hard cost cap <strong>of</strong> $2.595bn (plusadditional allowance for funds used during construction);- find that there'has been no imprudence and/or fraud, concealment or gross mismahagement whichexceeds the value.<strong>of</strong> the.impairment:buke:Energy lndiana,has^^agreed to in-the settlement-(almost$700-million) (plus the "value <strong>of</strong>. other settlement provisions); and- appfoye'otherprovisi<strong>of</strong>is <strong>of</strong> the settlemeht agreement, like.the agreed-upon proposed changes indepreciation rates and a partially corresponding change rn'retail e jectric rates,. a nd the agreedruponproposed change in calculation <strong>of</strong> CWIP return based on;the treatment <strong>of</strong> deferred taxes."16LEGPGNDIR001156

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