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test installation of a water mist catcher.<br />

We have made a full scale test on various<br />

water mist catcher designs, including<br />

some sub-supplied designs, which<br />

<strong>MAN</strong> <strong>Diesel</strong> & <strong>Turbo</strong> design Sub-supplier I Sub-supplier II<br />

Fig. 33: Tested designs<br />

Efficiency [%]<br />

100 100<br />

90 90<br />

80 80<br />

70 70<br />

60 60<br />

50 50<br />

40 40<br />

30 30<br />

20 20<br />

10 10<br />

94,8 94.8 94,7 94.7<br />

88,7 88.7<br />

69.7 69,7<br />

16 <strong>Service</strong> <strong>Experience</strong> of <strong>MAN</strong> B&W Low Speed <strong>Diesel</strong> Engines<br />

have been applied in big numbers in our<br />

large bore engines. Fig. 33 shows three<br />

of the tested designs and Fig. 34 shows<br />

an example of the results obtained. In<br />

WMC efficiency as function a function of of air air velocity velocity<br />

Constant boundary boundary conditions: conditions<br />

Mass flow of water = 0.0016 kg/s<br />

Massflow Air temperature of water = 25 ≈ 0.016 kg/s<br />

Air temperature ≈ 25 C<br />

Air absolute pressure ≈ 3.5 bara<br />

oC Air absolute pressure = 3.5 bara<br />

88.2<br />

88,2<br />

66.8<br />

66,8<br />

92.6 92,6<br />

84.1 84,1<br />

63.3<br />

63,3<br />

<strong>MAN</strong> <strong>Diesel</strong> & design <strong>Turbo</strong><br />

Sub-supplier Design II<br />

Sub-supplier II I<br />

0 0<br />

5.5 6 6.5 7 7.5 8<br />

5,5 6 6,5 7 7,5 Velocity [m/s] 8<br />

Velocity[m/s]<br />

Fig. 34: Full scale test results<br />

this case, the water mist catching efficiency<br />

is shown as a function of air<br />

velocity and very big deviations in efficiency<br />

can be seen.<br />

On the basis of these results and an up-<br />

date of the mechanical design, we have<br />

now fully re-specified the water mist<br />

catcher design, and we expect that this<br />

will limit water ingress related scuffing.<br />

Cracks in the bedplate lifting bracket of K98<br />

engines<br />

In 2008, cracks in the lifting bracket<br />

on K98 bedplates were discovered on<br />

engines produced 5-7 years earlier,<br />

see Fig. 35. Soon after the first cracks<br />

were discovered, a so-called ‘Circular<br />

Letter’ was issued to all owners/operators<br />

of K98 engines, see Fig. 36. In<br />

this letter we asked for help to inspect<br />

for lifting bracket cracks. Furthermore,<br />

we informed about preventive countermeasures,<br />

which were burr grinding<br />

of the weld seams on the aftmost and<br />

foremost brackets. Also, a repair procedure<br />

was developed when the cracks<br />

first occurred. A modified bracket profile<br />

has been designed for new engines,<br />

see Fig. 37.<br />

Due to the high number of K98 engines<br />

in service, these rectifications are still<br />

ongoing and, fortunately, we are able to<br />

perform this work without disturbing the<br />

operation of the vessels involved.

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