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Latis II Underwater Remotely Operated Vehicle Technical Report

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CHALLENGES<br />

One of the most difficult challenges faced by<br />

the UMaine Team was preparing the ROV to<br />

operate in a submerged environment. Due to<br />

the extensive electronic systems both inside<br />

and outside the electronics enclosure, excellent<br />

waterproofing processes were essential. To<br />

address this challenge, initial testing was<br />

conducted on prototype, <strong>Latis</strong> I. The<br />

information gained from these tests influenced<br />

the final ROV design. For example, difficulties<br />

with small leaks through the waterproof<br />

connectors led to a final design with a<br />

permanent wire configuration and only<br />

installing a single removable part to access the<br />

sealed enclosure. Furthermore, sealing<br />

compounds such as potting epoxy were used<br />

more on <strong>Latis</strong> <strong>II</strong> because of the hardening<br />

capabilities not observed when using silicone or<br />

polyurethane.<br />

Another challenge faced by the team was<br />

dealing with conflicting opinions within the<br />

group regarding the steps to address a technical<br />

issue or the particular technical issue itself. It<br />

became obvious to the team that a process for<br />

resolving such conflicts would increase the<br />

productivity while avoiding interpersonal<br />

aggravations. To solve this problem it was<br />

agreed upon that testing would be conducted,<br />

when possible, on each idea to determine its<br />

viability. The criterion for selection was based<br />

on design parameters for our project such as<br />

cost, reliability, ease of implementation, and<br />

integration into existing systems. This process<br />

allowed a comparison between the ideas of the<br />

individual, and the goals of the team, usually<br />

resulting in one idea that best fit the situation<br />

at hand.<br />

15<br />

LATIS <strong>II</strong><br />

TECHNICAL REPORT<br />

Finally, one of the biggest challenges was<br />

manufacturing the parts for <strong>Latis</strong> <strong>II</strong>. After<br />

spending more time and effort than anticipated<br />

on <strong>Latis</strong> I it was decided early on in designing<br />

<strong>Latis</strong> <strong>II</strong> that the team should outsource<br />

manufacturing responsibilities to a company<br />

that specializes in the task. This however did<br />

not work well due to the slow turn-around time<br />

of the parts and frequent mistakes made by the<br />

manufacturing company. To solve this problem,<br />

the team decided to learn how to operate the<br />

Computer Numerically Controlled (CNC)<br />

machine available in the lab and manufacture<br />

some of the simpler parts. The team fabricated<br />

the remainder of the parts needed to finish the<br />

ROV, control arms and power supply box.<br />

TROUBLESHOOTING TECHNIQUES<br />

To gain some knowledge and experience that<br />

the UMaine ROV Team could later call upon<br />

when troubleshooting issues on <strong>Latis</strong> <strong>II</strong>, the<br />

team designed and constructed their prototype<br />

<strong>Latis</strong> I in the fall of 2009. From this first attempt<br />

the team gained valuable insight into the things<br />

that may go wrong in the future.<br />

WATERPROOFING<br />

In designing <strong>Latis</strong> I the team decided to use<br />

factory-made water proof electrical connectors.<br />

However, finding such connectors at the 40A<br />

current rating was problematic. Furthermore,<br />

the waterproof connectors finally purchased<br />

ended up being the weakest link in the entire<br />

electronics enclosure for <strong>Latis</strong> I. After weeks of<br />

trying different techniques such as greasing the<br />

O-rings of the connectors, tightening the<br />

connectors more than the specified torque, and<br />

even creating a positive pressure inside the<br />

electronics compartment, the team was still

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