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POLYMER INSULATORS - Hubbell Power Systems

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♦ <strong>INSULATORS</strong> ♦<br />

BY JOHN M. BURCH<br />

Director of Engineering<br />

Florida Keys Electric Cooperative, Inc.<br />

Tavernier, FL<br />

<strong>POLYMER</strong> <strong>INSULATORS</strong><br />

For Florida Electric Company<br />

“. . . Ohio Brass polymer insulators con-<br />

tributed significantly to our ability to<br />

complete the project about one year<br />

ahead of schedule.”<br />

®<br />

POWER<br />

SYSTEMS, INC.<br />

Fax 573-682-8714 http://www.hubbellpowersystems.com<br />

The history of electric service to the Florida<br />

Keys is a bit unique. Initially it consisted of<br />

a 50HP generator operated by H.S.<br />

McKenzie in conjunction with Florida<br />

<strong>Power</strong> and Light (FPL). His subscribers<br />

were provided with service from 5 to 10 AM and<br />

from 5 to 10PM - except on Saturday when the<br />

service was extended to midnight. In 1935, President<br />

Franklin Delano Roosevelt created the Rural<br />

Electric Administration (REA) and in 1936 congress<br />

passed the Rural Electrification Act. About<br />

that same time, a hurricane wiped out the Flagler<br />

Railway system to the Keys. The already developed<br />

right of way and bridges provided the<br />

surface over which the overseas highway (U.S. 1)<br />

was later built.<br />

In January 1940, the Florida Keys Electric<br />

Cooperative (FKEC) was certified by the Florida<br />

Secretary of State. Its service area was from the<br />

Dade-Monroe county line on the north to the 7mile<br />

bridge south of Marathon on the south.<br />

Using REA funds made available to rural com-


munities, an electric distribution system was built. Progress<br />

was slowed by the demand for war material although the<br />

Keys benefited from the war when the Navy built a water line<br />

all the way to Key West. The stage was set for rapid growth<br />

with a roadway to access the Keys, an electric system and an<br />

adequate water supply.<br />

The FPL/McKenzie holdings were purchased in 1941 and<br />

in 1942 a power plant was built in Tavernier. Marathon<br />

relied on a portable generator. From this evolved the system<br />

as it exists today. It is important to note that the FKEC is not<br />

only a distribution cooperative but has 16.5MW of generation<br />

and extensive transmission facilities.<br />

The transmission system got started in 1956 when a 69kV<br />

line was built from Tavernier to Florida City on the mainland.<br />

The FKEC then purchased power from the city of<br />

Homestead and later from FPL. The line paralleled U.S. 1<br />

and FKEC built the line from Florida City to Jewfish, then<br />

from Jewfish to Tavernier. In addition, a 69kV cable was<br />

installed between Tavernier and Islamorada. The first effort<br />

to establish overhead transmission between Marathon and<br />

Tavernier met with disaster when a line to Coco Plum was<br />

immediately destroyed by hurricane Donna in 1960.<br />

To keep up with growing demand, construction for a new<br />

138kV line began in 1975. The new line went from Key<br />

Largo to the Card Sound Bridge on state route 905 where it<br />

tied into FPL. About five years later, the old 69kV line from<br />

Key Largo to Tavernier was upgraded to 138kV and a new<br />

section was built from Tavernier to Marathon. This line was<br />

designed for 217MW but voltage considerations limit us to<br />

about 180MW. Capacitors have already been added.<br />

Text continues ➥


The joint FKEC<br />

— City Electric System<br />

of Key West<br />

(CES) transmission<br />

system had its inception<br />

in 1985 when the<br />

CES built a 138kV line<br />

and tied into the FKEC<br />

at Marathon. An agreement<br />

was reached<br />

whereby CES could get<br />

as much as 50MW if it<br />

was available. However the<br />

demand continued to grow<br />

and it became clear that it<br />

would be necessary to beef<br />

up the transmission facilities<br />

for the entire Florida<br />

Keys. In 1991 a plan calling<br />

for joint ownership of the<br />

transmission system was<br />

evolved. The percentage of<br />

ownership and the allocation<br />

of transferred energy were defined<br />

in the contract.<br />

The plan called for replacing<br />

the 69kV line from Key Largo<br />

to the county line with a new<br />

138kV line. This line would<br />

then proceed south to Tavernier<br />

where a new four breaker ring<br />

bus substation would be built.<br />

The line would be designed for<br />

230kV but operated at 138kV<br />

and FPL agreed to upgrade their<br />

tie line to 230kV. This would<br />

provide FKEC with a loop feed<br />

to Tavernier. All this was to be<br />

completed by 1996.<br />

In August 1992 hurricane Andrew<br />

severely damaged the existing 138kV line and essentially<br />

destroyed the old 69kV line. It was imperative that the whole<br />

plan be put on a fast track with completion now scheduled for<br />

early 1995. Expediting the permits presented special problems<br />

because the line is in an area of environmentally sensitive<br />

mangroves and adjacent to the Everglades National Park. The<br />

switchyard in Tavernier was proposed for construction in the<br />

area of a sensitive hardwood hammock. After much debate and<br />

some compromise, the permits were finally issued. After<br />

hurricane Andrew it was decided to design the line for a<br />

maximum effective wind speed of 172 mph at the pole top!<br />

The CES and FKEC retained the Maguire Group in<br />

Foxborough, MA to do the line<br />

design. The new line was to<br />

have a capacity of 360MW<br />

but once again voltage limitations<br />

have limited us to about<br />

220MW until corrective measures<br />

were taken. It was to be<br />

built in two phases. Phase 1<br />

was 7.5 miles long and went<br />

north from the Jewfish substation<br />

in Key Largo to the<br />

Dade-Monroe county line<br />

where it tied to FPL. Phase 2<br />

was about 15 miles long and<br />

extended south from Jewfish<br />

sub to the new<br />

switchyard at Tavernier.<br />

A single pole line of steel<br />

and spun concrete was chosen.<br />

Since it was designed<br />

for later upgrading to<br />

230kV, the insulator selected<br />

had to be such as<br />

to provide adequate<br />

leakage distance for operation<br />

at the higher<br />

voltage. This is important<br />

because during<br />

the long winter dry<br />

spells, the insulators<br />

accumulate a layer<br />

of surface contamination<br />

consisting<br />

largely of salt from<br />

the ocean spray.<br />

The Ohio Brass<br />

Hi*Lite XLHP<br />

horizontal post<br />

selected is equipped with 235<br />

inches of leakage distance or 1.685 inches per kV to<br />

ground at the maximum line to ground voltage for 230kV.<br />

This compares to 1.19 inches for a porcelain post.<br />

An additional advantage of the polymer post was its weight<br />

of only 130 pounds compared to a weight of 374 pounds for<br />

an equivalent porcelain insulator. The weight advantage becomes<br />

even more pronounced when you employ a braced post<br />

assembly on angle structures. In addition to the weight saving<br />

in the post, polymer suspensions weigh only 5 to 10 percent as<br />

much as porcelain suspensions.<br />

Insulator failures have occurred on the original 138kV line<br />

started in 1975. Investigation revealed that corrosion had taken<br />

place in the cement joints of these insulators. This deterioration


esulted in wind resonance fractures. Wind<br />

speeds in the Keys are consistently in the<br />

7.4 mph range — about the resonant<br />

wind speed for the porcelain posts on the<br />

line. The resulting oscillations caused the<br />

weakened insulators to fail in cantilever.<br />

A consultant was retained to recommend<br />

the line design tension and the type<br />

of insulator to be used on the new line.<br />

His study revealed that the line design<br />

tension should not exceed 18 percent of<br />

the conductor breaking strength. Since<br />

we preferred not to use vibration dampers,<br />

he recommended the use of polymer<br />

posts which he indicated would perform<br />

somewhat like dampers.<br />

The ability of the Ohio Brass ESP<br />

compound to withstand exposure to ultra<br />

violet light was demonstrated by the<br />

QUV test. This test which alternates<br />

exposure to UV and condensation during<br />

each cycle simulates the effect of<br />

sunlight by means of fluorescent UV<br />

lamps positioned within inches of the test<br />

specimen. The relative humidity is maintained<br />

at 100 percent. After the equivalent<br />

of approximately 25 years of exposure<br />

in the Arizona desert, the sample was<br />

still hydrophobic and there was no cracking,<br />

checking, crazing or erosion.<br />

Samples of the ESP compound were<br />

exposed to continuous corona. In addition,<br />

an oxidative stability test was conducted<br />

to determine its ability to withstand<br />

exposure to ozone. All test results<br />

revealed satisfactory characteristics.<br />

Another consideration was the inherent<br />

strength of the compound. The basic<br />

EPDM used in this alloy is physically<br />

much stronger than silicone rubber, as<br />

such, it is less likely to be damaged during<br />

handling and construction.<br />

Certainly our objective was to bring<br />

this project to fruition at minimum cost.<br />

This had to be tempered with the need to<br />

complete it without delay. The light<br />

weight and one piece construction of the<br />

polymer post simplified construction and<br />

resulted in lower construction costs.<br />

The removable base was attached to<br />

the pole before the pole was set. The<br />

insulator was then raised to the pole top<br />

by a bucket truck and remounted on its<br />

base. An equivalent porcelain post would<br />

require that the insulator be assembled<br />

on the ground. Due to the weight of the<br />

porcelain insulator, a crane would be<br />

required to raise it to the pole top. The<br />

© Copyright 2001 <strong>Hubbell</strong> • 210 North Allen Street • Centralia, MO 65240<br />

project contractor, Mr. Whitey Kohler of<br />

Kohler Construction, estimated that the<br />

installation time for the polymer post was<br />

only one-half the time for porcelain posts.<br />

In addition, the need for a crane on the job<br />

site resulted in the polymer post having a<br />

3 or 4 to 1 cost advantage over porcelain.<br />

As alluded to earlier, time was of the<br />

essence. We are convinced that the use of<br />

Ohio Brass polymer insulators contributed<br />

significantly to our ability to complete<br />

the transmission project about one<br />

year ahead of schedule. ■<br />

&<br />

TiPS NEWS<br />

view from<br />

Vol. 1, No. 5 November 1995<br />

NOTE: Because <strong>Hubbell</strong> has a policy of continuous product improvement, we reserve the right to change design and specifications without notice.<br />

EU1508-WB

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