April - Library
April - Library
April - Library
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1<br />
What is Predictive Maintenance<br />
Vol 20 No 2<br />
FIGURE 3 Motor Limestone Ball Mill FIGURE 4 Inner Race Damage<br />
Oil analysis identified a sleeve bearing problem on one of our forced draft fan motors. These are 3000 HP, oiled,<br />
sleeve bearing, 6.9kv motors. Oil samples are taken quarterly based on previous track record for this<br />
equipment. We had a spike to 35ppm tin in the sample of January 27, 2005 (Figure 5). A unit shut<br />
down would be required to remove this equipment from service, so a bleed and feed was performed<br />
until the oil tested clean (patch test). We increased sampling and patch tested for presence of tin. A<br />
5 micron patch didn’t reveal much, but tin was very evident with a 1.2 micron patch. We performed a<br />
couple more bleed and feeds before a scheduled shut down on February 19, 2005. Inspection of the<br />
removed bearing showed one area in the leading edge of the lower half with loose and missing<br />
babbitt (Figure 6). A repaired bearing was installed and the motor returned to normal service.<br />
A patch test was run after<br />
of couple weeks run time<br />
with no tin seen. Quarterly<br />
sampling was resumed with<br />
tin slightly trended up to<br />
9ppm by the September 05<br />
sample, by January 03, 2006<br />
the tin had jumped to 67ppm<br />
(Figure 5). These results<br />
came in a couple days before<br />
an un-scheduled shut down<br />
for a tube leak repair, so the<br />
bearing was replaced during<br />
that time.<br />
FIGURE 5 Tin Levels From Oil Sample<br />
This motor was removed for a 5 year rebuild in March 2006. During the inspection process the recently<br />
replaced inboard bearing was found to already have similar damage to it after less than three months run<br />
time. No external causes such as, water for hydrogen embrittlement, improper clearances, damaged shaft<br />
journals, or any other problems, could be found during the motor rebuild to have caused these bearing failures.<br />
FIGURE 6 Loose and Missing Babbitt<br />
During the run in of the rebuilt motor we experienced<br />
another bearing failure, this time on the outboard end. All<br />
4 of the failed bearings were almost identical in nature and<br />
all had been repaired at the same facility, this prompted<br />
some in depth conversations with the repair facility and<br />
their quality control measures.<br />
On the subject of sleeve bearing oiled motors, we have<br />
almost all of our oiled, 6.9kv motors equipped with sight<br />
glass oilers which are a bulls eye sight glass with a 4 oz<br />
make up oiler. This not only adds to the comfort zone over<br />
the bulls eye sight glass, it maintains the correct oil level<br />
as long as there is oil in the reservoir and reduces the