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April - Library

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1<br />

What is Predictive Maintenance<br />

Vol 20 No 2<br />

FIGURE 3 Motor Limestone Ball Mill FIGURE 4 Inner Race Damage<br />

Oil analysis identified a sleeve bearing problem on one of our forced draft fan motors. These are 3000 HP, oiled,<br />

sleeve bearing, 6.9kv motors. Oil samples are taken quarterly based on previous track record for this<br />

equipment. We had a spike to 35ppm tin in the sample of January 27, 2005 (Figure 5). A unit shut<br />

down would be required to remove this equipment from service, so a bleed and feed was performed<br />

until the oil tested clean (patch test). We increased sampling and patch tested for presence of tin. A<br />

5 micron patch didn’t reveal much, but tin was very evident with a 1.2 micron patch. We performed a<br />

couple more bleed and feeds before a scheduled shut down on February 19, 2005. Inspection of the<br />

removed bearing showed one area in the leading edge of the lower half with loose and missing<br />

babbitt (Figure 6). A repaired bearing was installed and the motor returned to normal service.<br />

A patch test was run after<br />

of couple weeks run time<br />

with no tin seen. Quarterly<br />

sampling was resumed with<br />

tin slightly trended up to<br />

9ppm by the September 05<br />

sample, by January 03, 2006<br />

the tin had jumped to 67ppm<br />

(Figure 5). These results<br />

came in a couple days before<br />

an un-scheduled shut down<br />

for a tube leak repair, so the<br />

bearing was replaced during<br />

that time.<br />

FIGURE 5 Tin Levels From Oil Sample<br />

This motor was removed for a 5 year rebuild in March 2006. During the inspection process the recently<br />

replaced inboard bearing was found to already have similar damage to it after less than three months run<br />

time. No external causes such as, water for hydrogen embrittlement, improper clearances, damaged shaft<br />

journals, or any other problems, could be found during the motor rebuild to have caused these bearing failures.<br />

FIGURE 6 Loose and Missing Babbitt<br />

During the run in of the rebuilt motor we experienced<br />

another bearing failure, this time on the outboard end. All<br />

4 of the failed bearings were almost identical in nature and<br />

all had been repaired at the same facility, this prompted<br />

some in depth conversations with the repair facility and<br />

their quality control measures.<br />

On the subject of sleeve bearing oiled motors, we have<br />

almost all of our oiled, 6.9kv motors equipped with sight<br />

glass oilers which are a bulls eye sight glass with a 4 oz<br />

make up oiler. This not only adds to the comfort zone over<br />

the bulls eye sight glass, it maintains the correct oil level<br />

as long as there is oil in the reservoir and reduces the

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