Learn more - Johnson Controls Inc.
Learn more - Johnson Controls Inc.
Learn more - Johnson Controls Inc.
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Case study<br />
Beverage bottling plant lowers energy<br />
costs with compressor technology upgrade<br />
A national food and beverage corporation had to increase production of one of its<br />
beverage bottling plants in order to keep pace with sales growth. This called for an<br />
increase in refrigeration capacity, which traditionally would have translated into higher<br />
energy costs to run the new equipment.<br />
Instead, the company desired a solution that would reduce the cost of providing<br />
refrigeration, and asked a <strong>Johnson</strong> <strong>Controls</strong> Frick Factor representative to develop<br />
a strategy to accomplish this. Frick Factor is an authorized seller of Frick industrial<br />
refrigeration products. <strong>Johnson</strong> <strong>Controls</strong> absorbed the Frick product line through its<br />
acquisition of York International.<br />
Challenges<br />
• <strong>Inc</strong>rease the overall refrigeration capacity, while making the equipment less<br />
expensive to operate.<br />
• Perform the retrofit without disrupting the bottling production process and without<br />
the need to enlarge the size of the engine room’s existing footprint.<br />
• Reduce the cost of annual maintenance and the associated compressor downtime.
Frick RWF II Screw Compressor<br />
<strong>Johnson</strong> <strong>Controls</strong> solutions<br />
• Replace two aging reciprocating compressors with one new Frick Vyper <br />
Variable Speed screw compressor package with a larger capacity and that fits<br />
into the same footprint as the old equipment.<br />
• Install a new refrigerant-based oil cooling system that avoids increasing the<br />
existing compressor water cooling system.<br />
• Provide a state-of-the-art compressor that is designed to minimize annual<br />
maintenance.<br />
Results<br />
• Reduced the annual electrical energy consumption of the refrigeration<br />
equipment by <strong>more</strong> than 30 percent within the first year of operation.<br />
• Created consistent product quality by removing the sudden load swings<br />
experienced during the bottle filling process.<br />
• Lowered the plant’s compressor maintenance budget by $22,000 per year.<br />
©2008 <strong>Johnson</strong> <strong>Controls</strong>, <strong>Inc</strong>. Printed in USA 3/08<br />
www.johnsoncontrols.com