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German Federal Armed Forces<br />

Technical Center for Weapons<br />

and Ammunition<br />

<strong>Final</strong> <strong>Report</strong><br />

!"#$%&'()*)+'$,-"#.)&()/"0$)!"#$1!<br />

Author: BR z.A. Mathias<br />

Wagner<br />

VS- NUR FÜR DEN DIENSTGEBRAUCH<br />

%2345-46)78)9:;38)>;8=?;@;)<br />

This document is German MoD property. It contains intellectual property of the BWB as<br />

well as confidential information of companies/institutes. This document, including its<br />

contents, shall not be disclosed to unauthorized third parties.<br />

1


Defense Technical Order (WTA)<br />

Tel.: 05931/ 43 0<br />

Fax: 05931/ 43 2091<br />

BwFw: 90 2422 –88 (od. App.<br />

Abstract<br />

The mine-clearing system <strong>MineWolf</strong> was tested at WTD 91 Meppen in March 2004 during clearing runs over<br />

live antitank mine types DM 21, TM 57 und TM 62. The purpose of the tests was to assess the effects that<br />

mine detonations in the clearing device area have on the operator and to ascertain the damage caused to<br />

the vehicle.<br />

The effects on the operator by mine detonations of the above types are within the admissible and<br />

acceptable range, provided that the detonations occur on the mine-clearing device.<br />

After each mine detonation the damage on the vehicle was checked and documented and the vehicle was<br />

repaired as required. Necessary repairs, mainly welding work, could be performed on site the same day.<br />

WTD91-310-26/04<br />

BR z.A. Matthias Wagner<br />

Keywords:<br />

Distribution: Seiten: 32<br />

BWB K 61<br />

3EA+7CD`s<br />

WTD 91 - 310<br />

1EA<br />

DirWTD 91 1 EA<br />

BWB Fist 1 EA<br />

WTD 91-AGB-001-01-03<br />

German Federal Armed Forces<br />

Technical Center for Weapons and Ammunition<br />

Schießplatz, 49716 Meppen<br />

Task designation: <strong>MineWolf</strong> – Clearing of Live Mines<br />

Task number:<br />

Task manager:<br />

Business area / section: 300 / 310<br />

<strong>Final</strong> <strong>Report</strong><br />

WTD No.: 91 - 300 - 143/04<br />

Ref.: 90 - 13 - 45<br />

Project designation: Landmine Counter Measures<br />

Project number: 1F050<br />

Requesting authority: BWB<br />

Requesting section : BWB K61 Kronjäger 6352<br />

OrgKz Name Tel.<br />

E/ KP0A/ 31880/ 1F050<br />

BTK OrgKz lfd. WTA-Nummer lfd. Vorh.-Nummer<br />

WTD 91<br />

WTD 91 - 310 Kasper <strong>Report</strong> prepared by: Wagner 2104<br />

OrgKz. Bearbeiter Telefon<br />

2


Content<br />

VS- Nur für den Dienstgebrauch<br />

1.0 Task Description 4<br />

2.0 Summary of Results 4<br />

3.0 Short Description of the Test Item 5<br />

4.0 Schedule and Required Effort 6<br />

5.0 Detailed Description of 7<br />

5.1 Background 7<br />

5.2 Remote Control Tests 7<br />

5.3 Tests with Manned Mine-Clearing Vehicle 8<br />

6.0 Determination of Results and Assessment 9<br />

6.1 Biomechanical Assessment of ATD Measured Values 9<br />

6.2 Blast Pressure Measurements 10<br />

6.3 Mine-Clearing Runs against Live Antitank Mines 10<br />

6.3.1 Test with Flail against Antitank Mine DM 21 (Test 01) 10<br />

6.3.2 Test with Flail against Antitank Mine DM 21 (Test 1) 11<br />

6.3.3 Test with Flail against Antitank Mine TM 57 (Test 2) 11<br />

6.3.4 Test with Tiller against Antitank Mine DM 21 (Test 3) 13<br />

6.3.5 Test with Tiller against Antitank Mine TM 57 (Test 4) 2<br />

6.3.6 Test with Tiller against Antitank Mine TM 62 P3 (Test 02) 4<br />

6.3.7 Test with Flail against Antitank Mine TM 57 (Test 5) 2<br />

6.3.8 Test with Flail against Antitank Mine TM 62 P3 (Test 6) 21<br />

6.3.9 Test with Tiller against Antitank Mine TM 57 (Test 7) 22<br />

6.3.10 Test with Tiller against Antitank Mine TM 62 P3 (Test 8) 24<br />

6.3.11 Test with Tiller against Antitank Mine TM 57 (Test 9) 25<br />

3


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6.3.12 Contact Detonation with Antipersonnel Mine DM 31 1<br />

6.3.13 Damage Determination by the Manufacturer<br />

7.0 List of References 3<br />

List of Figures and Pictures 4<br />

4


1 Task Description<br />

The effects of mine detonations on the vehicle during the clearing of live antitank mines<br />

were to be ascertained. This, however, was limited to mine detonations which occur on<br />

the clearing device in front of the vehicle due to the clearing process. The results shall<br />

yield information on<br />

• the mental and physical effects on the operator<br />

• the scope of the resulting damage and the maintenance effort<br />

• the negative effects on an ongoing clearing process<br />

• the planning of an ongoing clearing process<br />

To this end, the vehicle had to be subjected to clearing tests and contact explosions<br />

with live antitank mine types DM 21, TM 62 and TM 57 . Furthermore, a lateral contact<br />

explosion was to be conducted on the vehicle with bounding fragmentation mine DM<br />

31.<br />

2 Summary of Results<br />

VS- Nur für den Dienstgebrauch<br />

The mine-clearing system <strong>MineWolf</strong> with both accessory devices is suitable for<br />

clearing live antitank mines.<br />

The use of the flail device for clearing live antitank mines caused only minor damage<br />

which could be repaired with a limited effort or did not necessitate any repairs at all.<br />

The use of the tiller against live antitank mines resulted in considerably greater damage.<br />

These can only be repaired with a substantially greater effort than those caused with<br />

the flail. The repairs, mainly welding work, could be performed on site the same day.<br />

As a result of the biomechanical evaluation of dummy (ATD) measurements and the<br />

questioning of three operators it can be said that the load on the operator by mine<br />

detonations is within the admissible and acceptable range. This statement applies to the<br />

examined mine types DM 21, TM 62 and TM 57 and only refers to mine detonations<br />

which occur in the area of the clearing device.<br />

5


VS- Nur für den Dienstgebrauch<br />

3 Short Description of the Test Item<br />

The Minewolf is a mine-clearing device which has been developed especially for<br />

humanitarian mine-clearing. It is used for area clearing. The <strong>MineWolf</strong> system consists<br />

of a fragment-proof caterpillar, a protected driver's cab and a mechanically driven<br />

mine-clearing device. Both a flail device and a mine tiller are available. The clearing<br />

process comprises two phases. First the area to be cleared is worked with the flail. This<br />

shall especially initiate or destroy surface-laid antitank mines (ATM) and antipersonnel<br />

mines (APM). In a subsequent second phase with the tiller the remains of the ATM, the<br />

mine fuzes and all APM shall be crushed or initiated. Clearing depths of up to 30 cm in<br />

the soil are achieved with the tiller. According to the UN and the <strong>MineWolf</strong> SOP, a<br />

follow-up search is required to remove incompletely destroyed fuzes and mines.<br />

Fig. 1 <strong>MineWolf</strong> with Flail in Operation<br />

6


Fig. 2: <strong>MineWolf</strong> with Tiller<br />

4. Schedule and Required Effort<br />

Test site: WTD 91 Meppen<br />

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Area at Bunker 30000<br />

Schedule: 24 – 25 Feb 04 familiarization and test runs at the "Hufeisenwall"<br />

(horseshoe wall)<br />

01 – 03 Mar 04 unmanned (remote) clearing tests with live<br />

antitank mines<br />

08 – 09 Mar 04 manned clearing tests with live antitank mines<br />

09 Mar 04 contact detonation with bounding mine DM 31<br />

7


5. Detailed Description of Tests<br />

5.1 Background<br />

The clearing tests with live mines were conducted between 01 and 09 March 2004 on the<br />

Meppen premises at bunker 30000. The soil was grown sand covered with grass. The first<br />

four trials were performed via remote control. Then 5 tests with human operators could be<br />

performed.<br />

5.2 Remote Control Tests<br />

On the one hand, the remote control tests serve to ascertain damage that a mine<br />

which is initiated by the clearing process causes to the vehicle. Furthermore, the physical<br />

effects and potential risks for the operator had to be measured by means of an<br />

instrumented test dummy, in order to be able to perform a human-related biomechanical<br />

assessment. This was an indispensable prerequisite for the safety board and the firing<br />

controller to approve manned tests.<br />

To record the measured values an ATD (Anthropometric Test Device = instrumented test<br />

dummy) was placed on the driver's seat, which was fitted with various sensors to measure<br />

the human relevant loads. The pertinent details are contained in the feeder report<br />

"Biomechanical Assessment of Mine-Clearing Tests with Live Mines".<br />

The following measurements and documentations were performed:<br />

• Video recording from outside<br />

• Video recording inside the driver's cab<br />

• Blast pressure measurement inside the driver's cab<br />

• Acceleration measurement inside the driver's cab<br />

• Measurements with the ATD<br />

VS- Nur für den Dienstgebrauch<br />

• Photos of the damage to the mine-clearing devices<br />

A total of 6 remote clearing tests were conducted against live antitank mines. Four of these<br />

tests led to the detonation of the cleared mines and thus to exploitable measuring results.<br />

Two tests each with the two mine-clearing devices<br />

8


(flail and tiller) were conducted against one DM 21 and TM 57 ATM each. In order to<br />

be able to rule out uncontrolled movements of the <strong>MineWolf</strong>, it was secured to a<br />

recovery tank during the tests. The mines to be cleared were laid one by one centrally<br />

in front of the clearing device. After a detonation the vehicle was stopped immediately<br />

and the effects were documented. If required, the clearing device was repaired prior to<br />

the next test run.<br />

5.3 Tests with Manned Mine-Clearing Vehicle<br />

The remote control tests were a necessary prerequisite to perform the manned tests.<br />

The results of the biomechanical assessment and the blast pressure measurement had<br />

to rule out any hazard to the operator when clearing live antitank mines. Since the<br />

results thus obtained only reflected the effect of detonations on the mine-clearing<br />

device, an additional safety measure was required which would prevent the vehicle from<br />

possibly driving over non-initiated mines. This was achieved by securing the <strong>MineWolf</strong><br />

to a recovery tank in such a way that the forward movement of the vehicle was stopped<br />

when the mine had reached the end of the clearing device. The following<br />

measurements and documentations were performed:<br />

• Video recording from outside<br />

• Photos of the damage to the mine-clearing devices<br />

• Questioning of the operators<br />

• Blast pressure measurement<br />

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A total of 5 clearing runs with 3 different drivers were performed.<br />

Both mine-clearing devices and 3 different antitank mines (DM 21, TM 57 und TM 62)<br />

were used. The following table provides an overview of the tests conducted:<br />

Run Date Detonation Mine Clearing device Operator<br />

01 01 Mar 04 no DM 21 flail RC<br />

02 03 Mar 04 no TM 62 P3 tiller RC<br />

1 01 Mar 04 yes DM 21 flail RC<br />

2 02 Mar 04 yes TM 57 flail RC<br />

9


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02 Mar 04 yes DM 21 tiller RC<br />

4 03 Mar 04 yes TM 57 tiller RC<br />

5 08 Mar 04 yes TM 57 flail human<br />

6 08Mar 04 yes TM62P3 flail human<br />

7 09Mar 04 yes TM57 flail human<br />

8 10 Mar 04 yes TM 62 P3 tiller human<br />

9 10Mar 04 yes TM57 tiller human<br />

6 Determination of Results and Assessment<br />

6.1 Biomechanical Assessment of ATD Measured Values<br />

The measured values of the ATD were evaluated by WTD91 GF 450. As a result of this<br />

evaluation it can be stated there is no intolerable risk of injury for the <strong>MineWolf</strong> operator<br />

itting inside the driver's cab. All human-related criteria which could be evaluated were<br />

fulfilled. The risks of injury are minimal and are far below the valid limits for mine-protected<br />

vehicles. Even in case of repeated consecutive loads no serious consequences have to be<br />

expected. Slight temporary disturbances like headache or muscular pain cannot be<br />

excluded, however.<br />

These statements, however, only apply to mine detonations that occur in the area of the<br />

mine-clearing device. Should there be a mine detonation underneath the vehicle or a track,<br />

completely different effects have to be considered. According to the present state of<br />

knowledge, it cannot be ruled out in that case that the valid limits for mine protection tests<br />

will be exceeded and thus the mine protection criteria will not be fulfilled.<br />

In all areas investigated the loads measured during tiller operation were higher than those<br />

during the flail tests.<br />

10


VS- Nur für den Dienstgebrauch<br />

The biomechanical assessment of the mine-clearing tests are compiled in a separate subtask<br />

report. The details of this summary can be taken from this report.<br />

6.2 Blast Pressure Measurements<br />

The blast pressure measurements were performed by WTD 91 – 630 at the position<br />

"driver's head" in accordance with the "Regulations and Guidelines for the Recording and<br />

Evaluation of Weapons and Detonation Blasts".<br />

The averages peak pressure level was 151.4 dB, the mean time of exposure 68.19 ms<br />

and the averaged peak pressure 0.74 kPa.<br />

The daily permissible number of mine detonations was determined from the measured<br />

values according to the "Threshold level diagram for preventing auditory defects due to<br />

blast loads" for ear protection devices.<br />

Accordingly, the blast pressure load without ear protection is inadmissible.<br />

With headset H – 280 the permissible number of blast pressure loads is 23, with headset<br />

MAX Lite the permissible number of blast pressure loads is 561.<br />

6.3 Mine-Clearing Runs against Live Antitank Mines<br />

6.3.1 Test with Flail against Antitank Mine DM 21 (Test 01)<br />

This test was performed on 01 March 04 at 14:45 hrs with remote control and<br />

instrumented dummy.<br />

The ATM was passed over without any reaction. The vehicle was driven back. The mine<br />

was not visible. It was located with a spade in the loose soil and its surface was carefully<br />

exposed. It was located about 2 m behind its original position. The top was upside. The<br />

garnishing material bonded to the arming cover was missing. Thus it had received<br />

sufficiently strong shocks that should have be led to an initiation.<br />

After 15 minutes it was passed over again without changing its position, again without any<br />

reaction. The mine body was visible in the soil material and was covered with about 2 cm<br />

of soil. This was carefully removed by hand. The flail hits were even stronger than before.<br />

The mine had to be destroyed without any further contact.<br />

The test could not be exploited.<br />

11


VS- Nur für den Dienstgebrauch<br />

6.3.2 Test with Flail against Antitank Mine DM 21 (Test 1)<br />

This test was performed on 01 March 04 at 15:45 hrs with remote control and<br />

instrumented dummy.<br />

The ATM DM 21 detonated on site upon contact with the mine-clearing device. The<br />

vehicle was stopped immediately.<br />

The hit occurred approx. 1 m off the right-hand outer edge.<br />

Damage:<br />

The right-hand rubber mats had been torn off. One link of the mainly affected flail chain<br />

was slightly bent. Clearing could be continued with this damage.<br />

Thus, the clearing result was very good.<br />

Fig. 3: Effects of the Mine Detonation from Test 1<br />

6.3.3 Test with Flail against Antitank Mine TM 57 (Test 2)<br />

This test was performed on 02 March 04 at 10:05 hrs with remote control and<br />

instrumented dummy.<br />

12


VS- Nur für den Dienstgebrauch<br />

The ATM TM 57 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 1 m off the left-hand outer edge.<br />

Damage:<br />

The left-hand rubber mats were lightly torn. Their mounting rails on the left support arm<br />

were less damaged than during the previous test on the right-hand side.<br />

The mount of the mainly affected flail chain was expanded but easy to repair.<br />

Thus, the clearing result was still very good.<br />

Fig. 4: Eroded Flail after Test 2<br />

13


Fig. 5: Expanded Mount after Test 2<br />

6.3.4 Test with Tiller against Antitank Mine DM 21 (Test 3)<br />

This test was performed on 02 March 04 at 11:35 hrs with remote control and<br />

instrumented dummy.<br />

The ATM DM 21 detonated on site upon contact with the mine-clearing device. The vehicle<br />

was stopped immediately.<br />

The hit occurred centrally. Damage:<br />

Two directly affected chisel teeth were worn, 2 others were pushed out to the rear. Three<br />

of the 30 x 130 cross spars of the tiller were bent.<br />

Clearing could have continued but it was decided to perform repairs instead.<br />

Repair effort:<br />

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14


Some of the elements were disassembled by 2-4 persons in the afternoon, some parts of<br />

the affected cross spars were detached, new parts welded in and all parts reassembled.<br />

Thus the damage was slightly greater, but acceptable for a cleared ATM.<br />

Thus, the clearing result was still good.<br />

Fig 6: Mine Detonation during Test 3<br />

Fig 7: Damage to the Tiller after Test 3<br />

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15


Fig. 8: Repaired Tiller after Test 3<br />

6.3.5 Test with Tiller against Antitank Mine TM 57 (Test 4)<br />

This test was performed on 03 March 04 at 09:55 hrs with remote control and<br />

instrumented dummy.<br />

The ATM TM 57 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 1.1 m off the right-hand side.<br />

Damage:<br />

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One chisel had been pushed out to the rear. 3 rubber mats were torn off.<br />

One of the 30 x 130 cross spars was torn apart and strongly deformed. The adjacent spars<br />

were obviously less deformed than during the preceding test.<br />

Clearing could thus be continued.<br />

Thus, the clearing result was still rather good.<br />

16


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Fig. 9: Damage to the Tiller after Test 4<br />

Fig. 10: Missing Chisel after Test 4<br />

17


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Fig. 11: Damaged Rubber Mats after Test 4<br />

6.3.6 Test with Tiller against Antitank Mine TM 62 P3 (Test 02)<br />

This test was performed on 03 March 04 at 10:55 hrs with remote control and<br />

instrumented dummy.<br />

The ATM TM 62 P3 was passed over without any reaction. <strong>Final</strong>ly, the bottom part of the<br />

green plastic case was ejected approx. 10 m in forward direction. The vehicle was pulled<br />

back.<br />

The mine with the plastic case had been completely milled in its laying position but not<br />

properly cleared.<br />

The light brown plastic case (100 x 100) with the mine fuze and the primer charge form the<br />

mine body lay on top of the soft soil. The fuze cover had been hit twice and was torn in<br />

nearly over its entire circumference. Thus the firing pin was visible. Its two safety pins were<br />

still attached. This suggests that the fuze with the primer charge was still functional. The<br />

possible effect of the mine was clearly reduced by separating the main charge from the<br />

fuze with primer charge. Nevertheless, a functional fuze with primer charge still represents<br />

a similar threat potential as an antipersonnel mine.<br />

The mine fragments and the fuze had to be destroyed. The clearing result was inadequate.<br />

18


Fig 12: Laid ATM prior to Test 02<br />

Fig 13:PiecesoftheATMafterTest02<br />

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19


Fig. 14 Mine Fuze after Test 02<br />

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6.3.7 Test with Flail against Antitank Mine TM 57 (Test 5)<br />

This test was performed on 08 March 04 at 13:45 hrs with Michael Kelly (company STS)<br />

as an operator.<br />

The ATM TM 57 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 1.1 m off the right-hand side.<br />

Damage:<br />

No particular damage could be recognized.<br />

Repair effort:<br />

Clearing could have been continued but it was decided to perform repairs instead. Five flail<br />

chains were replaced within 30 minutes.<br />

Operator's impressions:<br />

Mr. Kelly perceived the blast pressure and the acceleration in the armored cabin to be by<br />

all means acceptable.<br />

20


The clearing result was very good.<br />

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Fig. 15: Effects of the Mine Detonation from Test 5<br />

Fig. 16: Flail Chain Mounts after Test 5<br />

21


Fig. 17: Repaired Flail after Test 5<br />

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6.3.8 Test with Flail against Antitank Mine TM 62 P3 (Test 6)<br />

This test was performed on 08 March 04 at 15:05 hrs with Michael Kelly (company STS)<br />

as an operator.<br />

The ATM TM 62 P3 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 0.7 m off the right-hand side.<br />

Damage:<br />

Only minor damage was recognizable, one flail element was missing.<br />

The mine crater in the ground was of normal size, the same as during the other mine<br />

detonations.<br />

Clearing could have been continued with this damage.<br />

Repair effort:<br />

Since the clearing test with the flail were finished, no repair was performed. Instead, the<br />

flail was replaced by the tiller. This was done with the crane of the armored recovery<br />

vehicle in about 40 minutes.<br />

22


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Operator's impressions:<br />

Mr. Kelly perceived the blast pressure and the acceleration in the armored cabin to be by<br />

all means acceptable.<br />

The clearing result was very good.<br />

Fig. 18: Effects of the Mine Detonation from Test 6<br />

6.3.9 Test with Tiller against Antitank Mine TM 57 (Test 7)<br />

This test was performed on 09 March 04 at 10:10 hrs with Michael Kelly (company STS)<br />

as an operator.<br />

The ATM TM 57 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 1.1 m off the right-hand side.<br />

Damage and repair effort:<br />

No chisel was missing. One cross spar (30 x 130) of the tiller was torn off and heavily<br />

deformed. One weld seam of a cross spar was torn. A total of 4 parts would have needed<br />

replacement.<br />

However, clearing could still continue.<br />

23


Operator's impressions:<br />

Mr. Kelly perceived the blast pressure and the acceleration in the armored cabin to be<br />

by all means acceptable.<br />

The clearing result was still rather good.<br />

Fig. 20: Damage to Tiller after Test 7<br />

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Fig.19: Effects of Mine Detonation from Test 7<br />

24


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6.3.10 Test with Tiller against Antitank Mine TM 62 P3 (Test 8)<br />

This test was performed on 09 March 04 at 10:45 hrs with Rolf Albrecht (WTD 91) as an<br />

operator.<br />

The ATM TM 62 P3 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 0.5 m off the left-hand side. Damage:<br />

One chisel was worn, two cross spars 30 x 130 were bent. The damage seemed to be<br />

minor as compared to the previous tests with the TM 57. The mine crater in the ground<br />

was of normal size. Clearing could thus be continued.<br />

Operator's impressions:<br />

Mr. Albrecht perceived the blast pressure and the acceleration in the armored cabin to be<br />

by all means acceptable.<br />

Thus, the clearing result was still rather good.<br />

Fig. 21: Effects of the Mine Detonation from Test 8<br />

25


Fig. 22: Damage to Tiller after Test 8<br />

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6.3.11 Test with Tiller against Antitank Mine TM 57 (Test 9)<br />

This test was performed on 09 March 04 at 11:05 hrs with Jürgen Kronjäger (BWB) as an<br />

operator.<br />

The ATM TM 57 detonated on site upon contact with the mine-clearing device.<br />

The vehicle was stopped immediately.<br />

The hit occurred approx. 0.2 m off the right-hand outer edge of the tiller.<br />

Damage:<br />

The grinding sound when running down the tiller became stronger because one outer tooth<br />

was bent outwards. 4 cross spars 30 x 130 were deformed, two cross spars were torn off<br />

at the end of the weld seam. The depth control device was bent outwards but still<br />

functioning.<br />

After some provisional works of about 15 minutes a test run with the tiller was performed.<br />

The tiller performance was still sufficient.<br />

Thus, the clearing result was still rather good even after the third hit on the same tiller.<br />

26


Fig. 23 : Laid Antitank Mine prior to Test 9<br />

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27


Fig. 25: Damage to Tiller after Test 9<br />

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Fig. 24: Effects of the Mine Detonation from Test 9<br />

28


Fig. 26: Missing Chisel Tooth after Test 9<br />

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6.3.12 Contact Detonation with Antipersonnel Mine DM 31<br />

These tests were performed on the afternoon of 09 March 04 at the request of the<br />

company STS/AHWI/RUAG. Two contact detonations with AP fragmentation mine DM31<br />

were performed.<br />

The mines were placed on solid ground 10 m and 5 m from the tiller on the left-hand (fully<br />

armored) side of the mine-clearing vehicle and the mine fuze DM56A1B1 was initiated by<br />

a detonator placed on top of it. After approx. 2 s the explosive device of the mine jumped<br />

from the launch box and detonated about 1 m above the ground.<br />

At 10 m distance there were only a few fragment hits on the equipment: there were only<br />

small marks on the 6mm armor plates, there were 2 dents in the 3mm instrument box, one<br />

hit was found on the cabin glass.<br />

At 5 m distance the fragment hits were more severe: slight dents in the 6mm armor plates,<br />

two full penetrations in the 3mm instrument box , also two full penetrations in the GPS<br />

arm, and two on the glass.<br />

No fragment penetrations through the protected operator cab were detected.<br />

The operability of the <strong>MineWolf</strong> was not affected by the fragment hits.<br />

29


6.3.13 Damage Determination by the Manufacturer<br />

After completion of the tests the <strong>MineWolf</strong> was disassembled by the company AHWI and<br />

the damage it had suffered was determined.<br />

Damage had occurred especially by deformations of the V-belt pulleys and the<br />

lockwashers, which – according to the company – are due to the (elastic) pushing apart of<br />

the tiller box side panels.<br />

The company estimated the damage at 19,723 Euro.<br />

Fig. 27: V-belt Pulleys and Lockwashers<br />

VS- Nur für den Dienstgebrauch<br />

No fragment penetrations through the protected operator cab were detected.<br />

The operability of the <strong>MineWolf</strong> was not affected by the fragment hits.<br />

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Fig. 28: Deformed Lockwashers<br />

VS- Nur für den Dienstgebrauch<br />

7 ListofReferences<br />

Theimer, Gerhard: Kurzbericht Räumen von scharfen Panzerminen mit dem<br />

MINEBREAKER 2000 (2002) (Brief <strong>Report</strong>: Clearing of Live Antitank Mines with the<br />

MINEBREAKER 2000)<br />

Königstein, Gunnar: Versuchsprotokoll Minenräumgerät <strong>MineWolf</strong> (Abschrift, erstellt von<br />

BWB K 61 vom 24.03.2004) (Test <strong>Report</strong>: Mine-Clearing Equipment <strong>MineWolf</strong>)<br />

Nies, Oliver: Bericht / Teilauftrag Minenräumer <strong>MineWolf</strong> (<strong>Report</strong> / Subtask Mine-Clearing<br />

Equipment <strong>MineWolf</strong>)<br />

Biomechanische Bewertung der Räumversuche mit scharfen Minen vom März 2004<br />

(Biomechanical Assessment of Mine-Clearing Tests with Live Mines of March 2004)<br />

31


VS- Nur für den Dienstgebrauch<br />

List of Figures<br />

Fig. 1: <strong>MineWolf</strong> with Flail in Operation 6<br />

Fig. 2: <strong>MineWolf</strong> with Tiller 7<br />

Fig. 3: Effects of the Mine Detonation from Test 1 12<br />

Fig. 4: Eroded Flail after Test 2 13<br />

Fig. 5: Expanded Mount after Test 2 14<br />

Fig. 6: Mine Detonation during Test 3 15<br />

Fig. 7: Damage to the Tiller after Test 3 15<br />

Fig. 8: Repaired Tiller after Test 3 16<br />

Fig. 9: Damage to the Tiller after Test 4 17<br />

Fig. 10: Missing Chisel after Test 4 17<br />

Fig. 11: Damaged Rubber Mats after Test 4 18<br />

Fig. 12: Laid ATM prior to Test 02 19<br />

Fig. 13: Pieces of the ATM after Test 02 19<br />

Fig. 14: Mine Fuse after Test 02 20<br />

Fig. 15: Effects of the Mine Detonation from Test 5 21<br />

Fig. 16: Flail Chain Mounts after Test 5 21<br />

Fig. 17: Repaired Flail after Test 5 22<br />

Fig. 18: Effects of the Mine Detonation from Test 6 23<br />

Fig. 19: Effects of the Mine Detonation from Test 7 24<br />

Fig. 20: Damage to Tiller after Test 7 24<br />

Fig. 21: Effects of the Mine Detonation from Test 8 25<br />

Fig. 22: Damage to Tiller after Test 8 26<br />

Fig. 23: Laid Antitank Mine prior to Test 9 27<br />

Fig. 24: Effects of the Mine Detonation from Test 9 28<br />

Fig. 25: Damage to Tiller after Test 9 28<br />

Fig. 26: Missing Chisel Tooth after Test 9 29<br />

Fig. 27: V-Belt Pulley and Lock Washers 30<br />

Fig. 28: Deformed Lock Washers 31<br />

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