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Laterite Leach Tests

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ANSTO Minerals Report C1206 to Lagoon Creek Resources – Westmoreland Deposits<br />

For most elements, the actual solution values are close to the weighted averages after 24<br />

hours. The exceptions are as follows:<br />

• Higher Fe: as mentioned earlier this was due to the mild steel grinding media and mill<br />

components partly dissolving in the leach.<br />

• Higher Mn: due to pyrolusite being used as the oxidant.<br />

• Lower Na: in the individual tests LC5 C and LC6 B sodium permanganate was used as<br />

the oxidant, thereby artificially raising the sodium levels in the product solutions.<br />

• Higher S: due to the extra acid added due to the metallic iron dissolving. Also<br />

pyrolusite dissolution consumes acid, thereby increasing the sulphate tenor of the<br />

solution.<br />

5.3.2 Vendor Settling and Filtration Results<br />

A summary of the FLSmidth settling test results are given in Table 5.5 (and compared with<br />

the ANSTO settling test results) and a summary of the filtration test results are given in Table<br />

5.6. The detailed report from FLSmidth has been included as Appendix J.<br />

TABLE 5.5<br />

Settling Test Results<br />

Parameter FLSmidth Junnagunna Redtree<br />

Thickener feed tonnage (t/h) 30 30 30<br />

Feed solids (wt%) 45<br />

Feedwell solids (wt%) 7.5 7.5 6.6<br />

Flocculant addition rate* (g/t) 50-100 62.5 71.6<br />

Flocculant type 800HP E 10 E 10<br />

Rise rate (m/h) 4.1<br />

Free settling rate (m/h) 30 5.9 5.9<br />

Expected underflow solids (wt%) 60-61<br />

Underflow stress yield (Pa) 14-19<br />

Flux rate (t/m 2 /h) 0.38 0.103 0.142<br />

Thickener diameter (m) 10 19.3 16.4<br />

Number of thickeners 1<br />

* Magnafloc 800HP for FLSmidth tests, Magnafloc for ANSTO tests<br />

48

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