Removal of Bromate and Perchlorate in Ozone/GAC Systems
Removal of Bromate and Perchlorate in Ozone/GAC Systems
Removal of Bromate and Perchlorate in Ozone/GAC Systems
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Influent:<br />
CUW<br />
10-50 ug/L <strong>Bromate</strong><br />
pH 6.8-8.2<br />
2-14mg/LDO<br />
0.3 - 42 mg/L Nitrate<br />
t<br />
NOTE: Not to Scale<br />
2.5-cm Inner-Diameter<br />
8.0-cm BAC Bed Height<br />
Support<br />
Material<br />
Figure 2.1 Schematic <strong>of</strong> BAG filters us<strong>in</strong>g CUW<br />
For the filter be<strong>in</strong>g operated with an <strong>in</strong>fluent nitrate concentration <strong>of</strong> 5.0 mg/L <strong>and</strong> a 25-m<strong>in</strong>ute<br />
EBCT, the last two weeks <strong>of</strong> this experiment showed 81 ± 6 percent bromate removal. The<br />
consistent bromate removals observed <strong>in</strong> these filters demonstrated the atta<strong>in</strong>ment <strong>of</strong> steady state.<br />
New filters were not assembled for each experimental condition (i.e. DO concentration, nitrate<br />
concentration, EBCT). Therefore, zero bed volumes is a term relative to the start <strong>of</strong> the particular<br />
experiment, not necessarily to the overall life <strong>of</strong> the filter. Each experimental condition was run for<br />
approximately 2 weeks, to ensure adequate acclimation to the experimental conditions.<br />
Figure 2.2 shows a schematic diagram <strong>of</strong> another set <strong>of</strong> filters that was constructed to<br />
evaluate bromate reduction us<strong>in</strong>g LMW. Norit 830 <strong>GAC</strong> (Norit Americas Inc., Atlanta, GA) was<br />
the medium <strong>in</strong> these filters, <strong>and</strong> it was taken from the full-scale plant at the Paul M. Neal Water<br />
Treatment Facility (Lake Bluff, IL). This carbon had <strong>and</strong> average particle diameter <strong>of</strong> 0.9 mm <strong>and</strong><br />
had been used for approximately seven years to treat ozonated LMW. Prior to pack<strong>in</strong>g the carbon<br />
<strong>in</strong>to the column, the BAC was r<strong>in</strong>sed with DDW to remove excessive turbidity. S<strong>in</strong>ce this carbon<br />
was already biologically active, no extensive preload<strong>in</strong>g period was required. For some <strong>of</strong> the LMW<br />
experiments, a syr<strong>in</strong>ge pump (74900 series, Cole Farmer Instrument Co., Vernon Hills, IL) was used<br />
to add an electron donor solution conta<strong>in</strong><strong>in</strong>g 1.2 mM<br />
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