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COVER STORY<br />

JAL 123: AUGUST 12, 1985<br />

520 LOST<br />

IT’S 20 YEARS SINCE THE WORLD’S<br />

WORST SINGLE AIRLINER ACCIDENT.<br />

MACARTHUR JOB AND STEVE SWIFT REPORT.<br />

Japan Air Lines’ 747SR, registered<br />

JA8119, completed four uneventful<br />

inter-city trips on Monday, <strong>August</strong> 12,<br />

1985, arriving back at Tokyo’s Haneda Airport<br />

at 5.17 pm. Its next service was <strong>Flight</strong> JAL123<br />

to Osaka, 215nm (400 km) south-west of<br />

Tokyo. A senior training Captain was in command,<br />

supervising the upgrading of a former<br />

747 first offi cer.<br />

With 509 passengers and 15 crew aboard,<br />

JAL 123 took off at 6.12 pm. Th e planned route<br />

was via the island of Oshima, 50 nm southwest<br />

of Tokyo, cruising at FL240 (24,000 ft).<br />

At 6.25, the controller saw the emergency<br />

code 7700 suddenly appear beside the 747’s<br />

radar target. Seconds later the aircraft called,<br />

requesting an immediate return to Haneda.<br />

Controller: “Roger – approved as requested.”<br />

JAL123: “Radar vector to Oshima, please.”<br />

Controller: “Turn right, heading 090.”<br />

But instead of making the expected turn<br />

back towards Oshima, the aircraft gradually<br />

turned to a north-west heading.<br />

Controller: “Negative, negative...confirm you<br />

are declare [sic] emergency?”<br />

JAL123: “Th at’s affi rmative!”<br />

Controller: “Request your nature of emergency?”<br />

Th ere was no immediate reply.<br />

Controller: “JAL123 – fly heading 090 radar<br />

vector to Oshima.”<br />

JAL123 (tensely): “But now uncontrol! [sic]”<br />

FLIGHT SAFETY AUSTRALIA JULY-AUGUST <strong>2005</strong> 28<br />

News that the flight was in trouble leaked<br />

to the media. Japanese television conducted a<br />

live-to-air telephone interview with an eyewitness<br />

watching the 747. He described it as “wavering<br />

and having trouble keeping to its flight<br />

path”. Meanwhile the aircraft had turned north<br />

towards the mountain ranges forming a spine<br />

along the main Japanese island of Honshu.<br />

Then, just on sunset at 6.56<br />

pm, as its altitude fell to<br />

8400 ft, the controller was<br />

horrified to see the target<br />

vanish from his screen.<br />

At 6.34 pm the company called the 747.<br />

Company operator: “JAL123 – this is Japan<br />

Air. Tokyo control received an emergency call<br />

30 miles west of Oshima Island.”<br />

Th e flight engineer responded, obviously<br />

under pressure: “Ah ... the R5 door is broken.<br />

Ah ... we are descending now...”<br />

Company operator: “Roger – does the Captain<br />

intend to return to Tokyo?”<br />

JAL123: “Ah ... just a moment ... we are making<br />

an emergency descent ... we’ll contact you<br />

again. Ah ... keep monitoring.”<br />

Out of control: Th e 747 continued north about<br />

25 nm, then began a gradual turn north-east<br />

in the direction of the US Air Force base at<br />

Yokota, 77 nm distant. It was maintaining<br />

around 22,000 ft above scattered thunderstorms<br />

and rain showers.<br />

When 45 nm west of Haneda Airport, the<br />

aircraft entered a descending turn to the right,<br />

completing a full circle before straightening out<br />

on an easterly heading towards the airport. Its<br />

descent then continued, but at 13,500 ft one of<br />

the crew called in an agitated voice: “JAL123,<br />

JAL123 – uncontrollable!”<br />

Tokyo control: “Roger – understood. Do you<br />

wish to contact Haneda (approach)?”<br />

JAL123 (frantically): “Ah ... stay with us!”<br />

JAL123 (now down to 9000 ft): “JAL123 –<br />

request radar vector to Haneda!”<br />

Controller: “Roger – I understand. It is runway<br />

22, maintain heading 090.”<br />

Still descending, the 747 now gradually<br />

turned to the left on to a heading of about 340<br />

degrees. It was below the level of mountains<br />

that now lay in its path.<br />

Controller: “Can you control now?”<br />

JAL123 (desperately): “JAL123 – uncontrollable.<br />

JAL123 – ah uncontrol. JAL123, uncontrol<br />

[sic].”<br />

Approach: “Your position ... ah ... 45 miles<br />

north-west of Haneda.”<br />

JAL123 (anxiously, with altitude read-out now<br />

13,000 ft): “North-west of Haneda – ah – how<br />

many miles?”<br />

Approach: “According to our radar, 55 miles<br />

north-west. I will talk in Japanese – we are ready


COVER STORY<br />

Photo:AAP<br />

photo: newsweek<br />

for your approach anytime. Also Yokota landing<br />

Sprawling (above): The wreakage of Japan<br />

is available – let us know your intentions.”<br />

Airlines <strong>Flight</strong> 123 on the slopes of Mount<br />

Th ere was no reply. Th e 747’s height was<br />

Osutaka. Clearly visible is part of a wing.<br />

Aftermath (inset right): Rescue workers<br />

now decreasing again and, by 6.54 pm, its<br />

with debris from the accident.<br />

altitude read-out was 11,000 ft. Approach<br />

called the aircraft again, advising its position<br />

was “50 miles – correction 60 miles”<br />

to recover its balance to the right. It was<br />

north-west of Haneda Airport. But again<br />

flying just like a staggering drunk.”<br />

there was no response.<br />

Because of the inaccessibility of the area, it<br />

A minute later, its target suddenly devi-<br />

was not until 9 am, more than 14 hours after<br />

ated 90° to the right and, as its altitude read-<br />

the crash, that civil defence workers reached<br />

out rapidly decreased, it entered a tight turn<br />

the site. Fog had forced a temporary suspen-<br />

of less than 2 nm radius. Th en, just on sunset<br />

sion of mountain flying, but when conditions<br />

at 6.56 pm, the controller was horrified to<br />

improved, army paratroopers arrived aboard<br />

see the target vanish from his screen.<br />

Chinook helicopters, rappelling down to<br />

Further calls to the 747 went unanswered.<br />

where the wreckage lay.<br />

Moments later, a military jet reported “a huge<br />

Th e disaster was now revealed. Flying a<br />

burst of flame in the Nagano Mountains”.<br />

westerly heading, the Boeing 747 had de-<br />

Impact in the mountains: It was dark by<br />

scended into a pine forest near the top of the<br />

the time two search helicopters reached the<br />

northern face of the 5400 ft Mt Osutaka, a<br />

area through showery weather. Attracted by<br />

narrow, steep-sided east-west ridge, explod-<br />

a fire blazing near the top of the 5400 ft Mt<br />

ing into flames and breaking up as it bounced<br />

Osutaka in inaccessible ranges more than<br />

along the ridge line.<br />

60 nm north-west of Tokyo, one helicopter<br />

Th ere was no sign of survivors. In Tokyo,<br />

pinpointed the site of the crash, reporting<br />

the fearful news was confirmed to waiting<br />

flames “over an area about 300 m square”.<br />

media – the highest death toll ever in a single-<br />

One witness, surprised at seeing an airaircraft<br />

accident.<br />

liner above his remote mountain village,<br />

Well down the mountain face, a fireman<br />

described its erratic flight. “All of a sudden,<br />

stood on the steep slope surveying the wreck-<br />

a big aeroplane appeared from between<br />

age. Suddenly he saw something that looked<br />

mountains,” he told police. “Four times<br />

like an arm waving! Sure enough, a young<br />

it leaned to the left, and each time it tried<br />

woman, conscious though suffering a broken<br />

Photo:AAP<br />

AAP<br />

pelvis and a fractured arm, was pinned between<br />

two sets of seats.<br />

Not long afterwards there was more good<br />

news – a 12-year-old schoolgirl was found<br />

wedged in a tree, suffering nothing more serious<br />

than cuts and bruises. Even more was to<br />

come – rescuers discovered another young<br />

woman and her daughter beneath wreckage.<br />

Both suffered fractures. All four survivors<br />

had been seated among the last seven rows of<br />

seats.<br />

Medical staff found some victims had<br />

clearly survived the impact but, wearing only<br />

light summer clothes, had died of exposure<br />

during the night.<br />

Investigation: Th e aircraft had been worked<br />

hard, flying 25,000 hours in the course of<br />

18,800 cycles. Did this demanding utilisation<br />

show up some unknown flaw?<br />

Th e only clue to the loss of control was the<br />

tense radio transmission that the 5R cabin<br />

door – the rear most door on the starboard<br />

side – was “broken”. Could the door have<br />

broken away and struck the tail, disrupting<br />

the multiple hydraulic systems that actuate the<br />

aircraft’s control surfaces?<br />

FLIGHT SAFETY AUSTRALIA JULY-AUGUST <strong>2005</strong> 29


COVER STORY<br />

There was no sign of<br />

survivors. In Tokyo, the<br />

fearful news was confirmed<br />

to waiting media – the<br />

highest death toll ever in<br />

a single-aircraft accident.<br />

Th e finding of the door amongst the wreckage<br />

with its latches in the closed position only<br />

deepened the mystery. Why had the flight crew<br />

referred to it as “broken”? Could structural distortion<br />

of the fuselage have caused the door<br />

warning lamp to light up?.<br />

A photograph of the stricken aircraft,<br />

snapped from a mountain village shortly<br />

before the 747 crashed, provided new and dramatic<br />

evidence (see cover photo). A portion of<br />

its vertical fin, together with the section of the<br />

tailcone containing the auxiliary power unit<br />

(APU), was missing.<br />

Th e photographic evidence was confirmed<br />

when a 5 m piece of the aircraft’s fin was found<br />

floating in the bay where the aircraft had been<br />

passing when the emergency developed. Could<br />

the APU’s gas turbine have disintegrated, rupturing<br />

the hydraulic lines to the rudder and<br />

elevators?<br />

While Boeing and US investigators were<br />

on their way to join the Japanese team, other<br />

important evidence was emerging. One of<br />

the surviving passengers described what took<br />

place in the rear passenger cabin.<br />

She was an off-duty JAL flight attendant, sitting<br />

only four rows from the rear of the cabin.<br />

“Th ere was a sudden loud noise, somewhere<br />

to the rear and overhead,” she said. “It hurt my<br />

ears and the cabin filled with white mist. Th e<br />

vent hole at the cabin crew seat also opened.”<br />

Th e white mist was characteristic of sudden<br />

cabin decompressions. Th e “vent hole” was one<br />

of the modifications made to wide-bodied aircraft<br />

as a result of the Turkish Airlines DC-10<br />

disaster near Paris 11 years before in 1974. (See<br />

<strong>Flight</strong> <strong>Safety</strong> <strong>Australia</strong>, March-April <strong>2005</strong>).<br />

“Th ere was no sound of any explosion,” the<br />

witness continued, “But ceiling panels fell off,<br />

and oxygen masks dropped down.” Th en she<br />

felt the aircraft going into a “hira-hira” (Japanese<br />

for a falling leaf).<br />

Investigators soon discovered the flight data<br />

recorder (FDR) and cockpit voice recorder<br />

(CVR).<br />

A read-out of the FDR, and a transcription<br />

of the CVR tape, confirmed the flight attendant’s<br />

report.<br />

Th e explosive decompression occurred a<br />

few seconds past 6.24 pm, soon after the 747<br />

reached its cruising level. After the aircraft was<br />

cleared to return to Haneda, the Captain exclaimed:<br />

“Hydraulic pressure has dropped!”<br />

Th e failure of the 747’s multiple hydraulic<br />

control systems completely deprived the<br />

crew of primary control. Stabiliser and aileron<br />

trim were also rendered useless, and the yaw<br />

5


COVER STORY<br />

damper was no longer effective. With the aircraft’s<br />

stability also seriously impaired by the<br />

loss of a substantial part of its fin, it began<br />

combined “phugoid” and “Dutch roll” oscillations,<br />

settling into a pitching, yawing, and<br />

rolling motion.<br />

Th e pitching, in cycles of about 90 seconds,<br />

was taking the aircraft from about 15° noseup<br />

to 5° nose-down, with vertical accelerations<br />

varying between +1.4 g and -0.4 g. Variations<br />

in airspeed and altitude during the cycles<br />

were averaging around 70 kt and 3000 ft, with<br />

peaks of as much as 100 kt and 5000 ft. Th e<br />

yawing and rolling motion was much faster,<br />

the aircraft alternately rolling 50° either way in<br />

cycles of about 12 seconds.<br />

Delicate handling: Holding the aircraft’s attitude<br />

by increasing and decreasing power, the<br />

crew also achieved limited directional control<br />

by applying power asymmetrically. At 6.29<br />

pm they achieved a bank to the right, turning<br />

the aircraft on to a northerly heading while<br />

maintaining an altitude between 23,000 and<br />

25,000 ft.<br />

Desperate efforts: Th e altitude excursions<br />

reached a peak, with the nose pitching down<br />

and the aircraft diving from 25,000 to 20,000<br />

ft in a little over half a minute as the airspeed<br />

rose from 200 kt to 300 kt. Just as quickly the<br />

motion then reversed, the speed falling off<br />

again to 200 kt as the nose rose and the aircraft<br />

began climbing again.<br />

Preoccupied with trying to maintain control,<br />

the flight crew had overlooked donning<br />

their oxygen masks. Nearly 10 minutes had<br />

passed since the decompression and they were<br />

undoubtedly suffering a degree of hypoxia<br />

and some deterioration in judgement. But at<br />

the flight engineer’s prompting, this was remedied.<br />

Th e oxygen took effect quickly, for the pilots<br />

now limited the pitching excursions to about<br />

2000 ft in altitude and 60 kt in airspeed. But<br />

they could do nothing to dampen the continuous<br />

rolling from side to side.<br />

Th e CVR revealed the pilots’ increasingly<br />

desperate efforts to control the aircraft. Over<br />

and over again, the Captain instructed the<br />

co-pilot to “lower the nose”. Just before 6.39<br />

pm, the flight engineer suggested lowering<br />

the undercarriage to help stabilise the motion,<br />

but both Captain and co-pilot countered: “We<br />

cannot decrease the speed!”<br />

A minute later, with the pitch oscillations<br />

reduced to about half, the pilots succeeded in<br />

turning the aircraft towards Haneda Airport,<br />

42 nm distant. As they did so, the flight engineer,<br />

seizing the opportunity as the airspeed<br />

fell below 200 kt at the top of a pitch-up, selected<br />

the undercarriage down.<br />

Although the change of longitudinal trim<br />

required an immediate increase in engine<br />

power, the increased drag dampened the<br />

pitching, reducing the amplitude of the airspeed<br />

and altitude excursions as the aircraft<br />

entered a descent of about 3000 fpm. But the<br />

drag also dampened its response to directional<br />

control and, instead of continuing towards the<br />

airport, it entered a turn to the right, still descending.<br />

But after turning through 360 degrees, the<br />

pilots regained some measure of directional<br />

control at 15,000 ft. Th eir reprieve was shortlived<br />

– the aircraft began turning again, this<br />

time to the left.<br />

Now below 9000 ft and still descending, the<br />

747 was heading north again towards mountainous<br />

country. “Hey – there’s a mountain<br />

– up more!” the Captain called anxiously. Th e<br />

co-pilot carefully applied more power, trying<br />

to juggle the aircraft’s attitude. But with the<br />

undercarriage down, this failed to check the<br />

descent.<br />

Captain: “Turn right! Up! We’ll crash into a<br />

mountain!”<br />

With the application of more power, the aircraft<br />

pitched nose-up, gaining 2000 ft, while<br />

the airspeed fell from 210 to 120 kt.<br />

Captain (urgently): “Maximum power!”<br />

But the coarse application of power triggered<br />

the phugoid oscillation again.<br />

Captain: “Nose down ... nose down!”<br />

Th e co-pilot reduced power again and the<br />

nose pitched down. Th e aircraft was plung -<br />

ing to below 5000 ft with the airspeed rising<br />

quickly to around 280 kt, before recovering<br />

from the dive at a loading of 1.85 g. Th e air -<br />

craft then climbed even more steeply to about<br />

8000 ft and, as its airspeed fell sharply, the stall<br />

warning began sounding.<br />

Captain (dismayed): “Oh no!” (urgently):<br />

“Stall! Maximum power!”<br />

Calls from Tokyo, Approach and Yokota<br />

were ignored as the crew fought to prevent the<br />

747 plunging out of control.<br />

Th e final 108 seconds of the CVR revealed<br />

a string of increasingly desperate instructions<br />

calling for “Nose up”, “Nose down, and “Flap”<br />

as the pilots tried to prevent the aircraft falling<br />

out of control.<br />

Finally, as it entered a tightening descending<br />

turn to the right, the ground proximity warning<br />

system began sounding. Fourteen seconds<br />

later there was the sound of the aircraft striking<br />

tree-tops, followed three seconds later by<br />

the sound of the crash.<br />

Wreckage examination: It was clear that<br />

the explosive decompression, the pre-impact<br />

damage to the fin and rudder, and the loss<br />

of all four hydraulic systems, were somehow<br />

linked. But what was the link – and what had<br />

precipitated it?<br />

As a precautionary measure, the Japanese<br />

Fatal flight: The explosive decompression occurred soon after the 747 reached it’s<br />

cruising level (point of rupture). The crew lost primary control as a result of loss of<br />

hydraulic control systems.<br />

FLIGHT SAFETY AUSTRALIA JULY-AUGUST <strong>2005</strong> 31


COVER STORY<br />

DESTRUCTION OF THE REAR PRESSURE BULKHEAD<br />

Tail cone blown off: A Japan Air Lines 747 SR. The red line shows the rear tail cone part<br />

of which was destroyed when the rear pressure bulkhead failed.<br />

Tear stop straps<br />

Line of<br />

cracks<br />

Tremendous force: The rear pressure bulkhead (shown left in blue) must contain tremendous<br />

force from the pressure difference at altitude between the cabin and outside air.<br />

The 4.55 m bulkhead is constructed of reinforced aluminium alloy sheets in a domed shape to<br />

resist pressure. The line of cracks (right) formed mid way between the upper and lower parts of<br />

the dome.<br />

UPPER<br />

BULKHEAD<br />

LOWER<br />

BULKHEAD<br />

Fracture<br />

Upper doubler<br />

plate splice<br />

Lower doubler<br />

plate splice<br />

Tear stop<br />

straps<br />

Line of cracks: A side view of the cracks formed prior to rupture of the bulkhead.<br />

The bulkhead was destroyed after the cracks ran past the tear stop straps.<br />

INCORRECT REPAIR<br />

Fillet seal<br />

NORMAL<br />

BULKHEAD<br />

Stiffener<br />

Rivets<br />

LOWER<br />

UPPER<br />

Filler sealant<br />

Doubler plate<br />

CORRECT<br />

REPAIR<br />

Upper doubler plate<br />

Gap filled with<br />

filler sealant<br />

Lower doubler plate<br />

Forward<br />

JA8119<br />

REPAIR<br />

Over-loaded rivets: A “section” through the bulkhead showing normal construction (left)<br />

a correct repair (centre) and an incorrect repair (right) that led to the JAL 123 tragedy.<br />

In the wrong repair, technicians tried to connect two doubler plates, which forced the<br />

middle row of rivets to carry too much load.<br />

Up<br />

UPPER<br />

LOWER<br />

Bulkhead 4.55 m diameter<br />

Photo: Kjell Nilsson<br />

<strong>Civil</strong> <strong>Aviation</strong> Board ordered inspections of all 69<br />

of Japan’s 747s. Boeing, in a telex to 747 operators<br />

world-wide, suggested they inspect the aft portion<br />

of the pressure hull. Airworthiness authorities<br />

world-wide issued airworthiness directives.<br />

Although Boeing 747s had no history of bulkhead<br />

failure, a major bulkhead fracture seemed to<br />

fit the evidence. Pressurised air, escaping from such<br />

a fracture, could have burst the fin.<br />

Th e rear pressure bulkhead was certainly badly<br />

damaged. But had the damage all been sustained in<br />

the impact?<br />

Although Boeing investigators argued that the<br />

design had been tested to a simulated service life<br />

of 20 years, and that the wreckage exhibited no evidence<br />

of corrosion, a profound shock lay in store.<br />

Examining the wreckage, Boeing’s structures engineer<br />

picked up a broken off section of pressure<br />

bulkhead plating. It had been repaired, and the<br />

repair didn’t look right.<br />

Electron microscope photographs of the fracture<br />

surfaces of the doubler plate revealed striations indicative<br />

of metal fatigue.<br />

Th e discovery posed two vital questions: Why<br />

was the bulkhead repaired in the first place? And<br />

why had it been wrongly repaired?<br />

An examination of JAL maintenance records<br />

revealed the rear fuselage of the crashed 747SR<br />

had scraped the ground during a nose-high landing<br />

seven years before. Th e impact had been severe<br />

enough to remove skin panels and crack the rear<br />

pressure bulkhead.<br />

Th e aircraft had been grounded for a month<br />

while Boeing engineers supervised repairs at JAL’s<br />

maintenance facility. Th e repair included replacement<br />

of the lower part of the rear fuselage and a<br />

portion of the lower half of the damaged bulkhead.<br />

Close examination of the bulkhead repair showed<br />

that two separate doubler plates, instead of one continuous<br />

one, were used as reinforcement. Th e result<br />

was excessive load on one row of rivets.<br />

JAL’s maintenance planning manager said the repairs<br />

were examined by the Japanese <strong>Civil</strong> <strong>Aviation</strong><br />

Bureau, and the aircraft test flown after the work<br />

was done. No shortcomings were detected.<br />

Moreover, in the seven years the aircraft had<br />

flown since, six 3000 hourly “C-checks” had been<br />

carried out. Yet these had found nothing.<br />

Lessons: Boeing changed its 747 design to make it<br />

more forgiving to failures like this in the future – in<br />

other words to improve its “fail safety”. Th e manufacturer<br />

strengthened tear-stop straps in the bulkhead<br />

to stop cracks running. It improved venting<br />

of the tail compartment behind the bulkhead to<br />

reduce pressure if a bulkhead failed. And it provided<br />

a cover for an internal access hole to prevent<br />

pressurised air from entering the vertical fin.<br />

FLIGHT SAFETY AUSTRALIA JULY-AUGUST <strong>2005</strong> 32


COVER STORY<br />

Modifications were also developed to prevent<br />

a total loss of hydraulic fluid from the<br />

four independent hydraulic control systems<br />

if the lines were severed for any reason, and<br />

to provide additional protection for control<br />

cables.<br />

Boeing had thought about most of these<br />

things when designing the 747, but events<br />

proved they had not tested them suffi ciently.<br />

Aircraft manufacturers have since learned<br />

the value of testing to prove design assumptions.<br />

Th e JAL 123 tragedy reminds us how unforgiving<br />

structural fatigue continues to be<br />

in aviation, long after the infamous Comet<br />

crashes of the 1950s. Accidents resulting from<br />

structural fatigue have killed thousands, including<br />

many in <strong>Australia</strong>: In 1945, a Stinson<br />

A2W lost a wing, killing 10; and in 1968, a<br />

Vickers Viscount lost a wing, killing 26.<br />

In 1990, an <strong>Australia</strong>n-built Nomad lost a<br />

tailplane, killing the pilot.<br />

Anyone repairing an aircraft needs to carefully<br />

follow approved data. To those repairing<br />

the bulkhead of the Japan Airlines’ 747, the improvised<br />

doubler plate repair probably looked<br />

strong enough – and it was, for a while. But,<br />

the fatigue aspects of a design are not always<br />

obvious. If you can’t install the repair exactly<br />

to the approved data, check with the designer.<br />

In JAL 123’s case, the Boeing repair team<br />

did not communicate well enough with their<br />

own company’s designers. Internal communication<br />

can be a problem for large companies.<br />

Operators should ask for assurance that the<br />

advice they are getting (including the NTO, or<br />

no technical objection) has engineering support,<br />

especially the support of company regulatory<br />

delegates.<br />

It is a good idea to check your old repairs.<br />

Be suspicious of all structural repairs. Be especially<br />

concerned about patches that are<br />

unusually old, large or thick. And be alert for<br />

small cracks emerging from under the edge of<br />

a patch repair.<br />

Look for signs of loose or working rivets,<br />

and be wary of stains streaking from under a<br />

patch. Th ey might be the signature of pressure<br />

or fluid leaks. And take any available opportunity<br />

to check internally for cracks hidden<br />

under external repairs.<br />

An improperly treated scratch on the aircraft<br />

pressure vessel skin, especially if covered<br />

under a repair doubler, could be hidden<br />

damage that might develop into fatigue cracking,<br />

eventually causing structural failure (see<br />

“Hidden hazard”, <strong>Flight</strong> <strong>Safety</strong> <strong>Australia</strong>, September-October<br />

2003).<br />

Anyone operating a large airliner should<br />

check their compliance with Airworthiness<br />

Directive AD/GENERAL/82 Amdt 1. Th e<br />

scope of this airworthiness directive is likely<br />

to expand in the future.<br />

Finally, JAL123 warns owners and maintainers<br />

that fatigue cracks can stay hidden,<br />

even from the most thorough general maintenance.<br />

You need to adopt a systematic approach<br />

(see “Diamond standard maintenance”<br />

below).<br />

Th at’s why airworthiness authorities around<br />

the world are progressively requiring aircraft<br />

manufacturers to upgrade the maintenance<br />

programs they publish for the types they support.<br />

And that’s why <strong>Australia</strong>’s safety regulator<br />

insists that aircraft owners follow them,<br />

unless they have done a similarly systematic<br />

engineering analysis to justify the safety<br />

equivalence of their alternative.<br />

Fatigue is indiscriminate and inevitable. If<br />

not carefully managed, it can result in catastrophe<br />

for any aircraft, large or small, repaired<br />

or not.<br />

Macarthur Job is an aviation writer and<br />

aviation safety specialist. Steve Swift is a<br />

CASA structural engineer.<br />

DIAMOND STANDARD<br />

MAINTENANCE<br />

By Steve Swift<br />

At an international conference on aeronautical<br />

fatigue held in Hamburg, Germany,<br />

in June this year the concept of diamond<br />

standard maintenance received a lot of<br />

attention.<br />

Site<br />

Detectable<br />

Duration<br />

Scenario<br />

Dangerous<br />

The “diamond”: a new way of<br />

describing the “damage tolerance”<br />

rules for managing structural fatigue.<br />

Diamond standard maintenance is based<br />

on a systematic analysis of how fatigue is likely<br />

to affect all the safety-critical parts of the airframe.<br />

Th e analysis has five elements:<br />

Site: Where could cracks start? Th is is a predictive<br />

element that requires analysis, testing<br />

and service experience, if available.<br />

Scenario: How will cracks grow? For example,<br />

will there be one or many? Will they interact?<br />

Will cracks in one part start cracks in another?<br />

Detectable: What is the smallest detectable<br />

size, considering the nature of the inspection<br />

method and other factors? Once you know<br />

this you can more effectively design your crack<br />

detection regime. Beware of optimism: For<br />

every lucky find of a small crack, there may be<br />

many more misses of large ones.<br />

Dangerous: As a crack continues to grow,<br />

sooner or later it starts to become “dangerous”,<br />

because the structure is about to lose the<br />

strength we want to assure.<br />

Duration: Th is is the time it will take a crack<br />

to grow from “detectable” to “dangerous”. It is<br />

the “safety window”. Th e inspection interval<br />

must be narrower, and must account for uncertainty<br />

and variability.<br />

Airworthiness authorities worldwide are<br />

Crack size<br />

Duration<br />

Detectable<br />

Dangerous<br />

Time<br />

The time between inspections must<br />

be shorter than the “Duration”. So, for<br />

safety, we must know “Detectable”,<br />

“Dangerous” and how fast a crack will<br />

grow.<br />

working with aircraft manufacturers and<br />

operators to put in place diamond-standard<br />

maintenance programs for all aircraft, including<br />

their repairs and modifications.<br />

Diamond standard maintenance programs<br />

are usually called airworthiness limitations or<br />

supplementary inspection documents (SIDs).<br />

With two out of three <strong>Australia</strong>n aircraft<br />

having seen a quarter century of hard service,<br />

the dangers of fatigue are ever present. Th ere is<br />

no room for complacency.<br />

For a copy of the full paper on diamond<br />

standard maintenance (called “Rough<br />

Diamond”), and other safety-related papers<br />

and reports on structural fatigue, visit CASA’s<br />

web site.<br />

FLIGHT SAFETY AUSTRALIA JULY-AUGUST <strong>2005</strong> <strong>33</strong>

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