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November 2012 - Indian Airforce

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The time was 2100h and I had just finished my<br />

dinner when my mobile rang. It was Gp Capt<br />

xx C Eng B from the Command Headquarters.<br />

He said that the VIP Avro ac of Command<br />

Communication Flight had made an emergency<br />

landing at Mumbai International Airport at 2030<br />

h due to nose undercarriage red light remaining<br />

‘ON’. Luckily there was no VIP on board and the ac<br />

was returning to base. The ac had landed safely but<br />

had been switched off on the taxi link due to nose<br />

wheel steering failure and was being towed back to<br />

the parking. The STO of the unit was on leave and<br />

since I was the STO of the neighbouring AVRO unit,<br />

I was asked to speak to the aircrew to ascertain the<br />

complete snag and keep a rectification party ready<br />

to go to Mumbai at first light.<br />

I called the senior most aircrew who was a Sqn Ldr<br />

with sufficient experience on type. He said that for<br />

this sortie he was the co pilot and the captain was a Fg<br />

Offr with about one year’s experience. He explained<br />

that they had taxied out normally and after takeoff<br />

when the undercarriage had been selected up, the<br />

nose undercarriage light had changed from green<br />

to red and remained ‘ON’, indicating that the nose<br />

wheel had not locked up. They tried one cycling of<br />

undercarriage and when the red light persisted, they<br />

declared the emergency and carried out a priority<br />

landing back at Mumbai. During the landing roll,<br />

while turning onto the link, he (the Sqn Ldr) realised<br />

that the nose wheel steering was ineffective and<br />

therefore had switched off the ac after clearing the<br />

runway. I spoke to one of my clueful Airframe Fitter<br />

JWO and we suspected that the snag might have<br />

been due to a bird hit during takeoff, which might<br />

have damaged the nose undercarriage door linkage<br />

and also severed the nose wheel steering cable.<br />

However, it was reported by the crew that they could<br />

not find any avian remains or damage, other than<br />

two large dents on the right undercarriage door of<br />

the nose wheel.<br />

A rectification team with I as the team leader<br />

(also the technical member of the Court of Inquiry)<br />

was airlifted to Mumbai to ascertain the cause of<br />

malfunction of the undercarriage and to undertake<br />

rectification on site. Since Mumbai did not have the<br />

requisite equipment, it was decided to carry even<br />

the 10 ton jack along with other requisite tools.<br />

Draining out of hydraulic fluid due to pipeline<br />

rupture was initially suspected, however, it was seen<br />

that the reservoir was still full and no abnormality<br />

in the nose undercarriage system was found<br />

during visual inspection. However two major dents<br />

wherein one of them had torn the aluminium skin<br />

were seen on the right front undercarriage door.<br />

We decided to jack up the front wheel and do a<br />

retraction test with pins on the two main wheels in<br />

place. The system was energised and pressure built<br />

up using the hand pump and the front wheel was<br />

retracted. No fouling was observed and the nose<br />

wheel undercarriage light changed from green to<br />

red and upon getting locked up, the red light went<br />

off. This confirmed that the system was working<br />

perfectly well. The nose wheel steering was also<br />

checked and tested thoroughly and was found to<br />

be serviceable.<br />

The team thereon proceeded to find the<br />

cause of the dent on the undercarriage door.<br />

The nose wheel toggle pin was removed and on<br />

closer examination it was seen that the dent was<br />

commensurate to the shape of the toggle pin<br />

head and there were even traces of red paint near<br />

the dent. The undercarriage was again retracted<br />

this time with the toggle disconnected and the<br />

pin fixed in the upper toggle. It was seen that the<br />

undercarriage door got obstructed by the upper<br />

toggle link at exactly the same place where it was<br />

dented. It was therefore deduced that the ac had<br />

taken off with the nose wheel toggle disconnected<br />

and this had caused the nose undercarriage not<br />

getting locked up and the red light remaining ‘ON’,<br />

creating an emergency in air.<br />

Exact Cause of Failure<br />

Parking for AF aircraft in Mumbai is such, that it<br />

requires being towed out of the slot during refuelling<br />

or just before starting. In this case the ac was towed<br />

out twice for refuelling and also just before departure<br />

at around 1915h. During towing the nose wheel<br />

toggle link is disconnected from the nose wheel<br />

steering jack. However, in this case the ground crew<br />

INDIAN AIR FORCE 2 0 1 2 N o v e m b e r Aerospace Safety 15

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