November 2012 - Indian Airforce
November 2012 - Indian Airforce
November 2012 - Indian Airforce
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The time was 2100h and I had just finished my<br />
dinner when my mobile rang. It was Gp Capt<br />
xx C Eng B from the Command Headquarters.<br />
He said that the VIP Avro ac of Command<br />
Communication Flight had made an emergency<br />
landing at Mumbai International Airport at 2030<br />
h due to nose undercarriage red light remaining<br />
‘ON’. Luckily there was no VIP on board and the ac<br />
was returning to base. The ac had landed safely but<br />
had been switched off on the taxi link due to nose<br />
wheel steering failure and was being towed back to<br />
the parking. The STO of the unit was on leave and<br />
since I was the STO of the neighbouring AVRO unit,<br />
I was asked to speak to the aircrew to ascertain the<br />
complete snag and keep a rectification party ready<br />
to go to Mumbai at first light.<br />
I called the senior most aircrew who was a Sqn Ldr<br />
with sufficient experience on type. He said that for<br />
this sortie he was the co pilot and the captain was a Fg<br />
Offr with about one year’s experience. He explained<br />
that they had taxied out normally and after takeoff<br />
when the undercarriage had been selected up, the<br />
nose undercarriage light had changed from green<br />
to red and remained ‘ON’, indicating that the nose<br />
wheel had not locked up. They tried one cycling of<br />
undercarriage and when the red light persisted, they<br />
declared the emergency and carried out a priority<br />
landing back at Mumbai. During the landing roll,<br />
while turning onto the link, he (the Sqn Ldr) realised<br />
that the nose wheel steering was ineffective and<br />
therefore had switched off the ac after clearing the<br />
runway. I spoke to one of my clueful Airframe Fitter<br />
JWO and we suspected that the snag might have<br />
been due to a bird hit during takeoff, which might<br />
have damaged the nose undercarriage door linkage<br />
and also severed the nose wheel steering cable.<br />
However, it was reported by the crew that they could<br />
not find any avian remains or damage, other than<br />
two large dents on the right undercarriage door of<br />
the nose wheel.<br />
A rectification team with I as the team leader<br />
(also the technical member of the Court of Inquiry)<br />
was airlifted to Mumbai to ascertain the cause of<br />
malfunction of the undercarriage and to undertake<br />
rectification on site. Since Mumbai did not have the<br />
requisite equipment, it was decided to carry even<br />
the 10 ton jack along with other requisite tools.<br />
Draining out of hydraulic fluid due to pipeline<br />
rupture was initially suspected, however, it was seen<br />
that the reservoir was still full and no abnormality<br />
in the nose undercarriage system was found<br />
during visual inspection. However two major dents<br />
wherein one of them had torn the aluminium skin<br />
were seen on the right front undercarriage door.<br />
We decided to jack up the front wheel and do a<br />
retraction test with pins on the two main wheels in<br />
place. The system was energised and pressure built<br />
up using the hand pump and the front wheel was<br />
retracted. No fouling was observed and the nose<br />
wheel undercarriage light changed from green to<br />
red and upon getting locked up, the red light went<br />
off. This confirmed that the system was working<br />
perfectly well. The nose wheel steering was also<br />
checked and tested thoroughly and was found to<br />
be serviceable.<br />
The team thereon proceeded to find the<br />
cause of the dent on the undercarriage door.<br />
The nose wheel toggle pin was removed and on<br />
closer examination it was seen that the dent was<br />
commensurate to the shape of the toggle pin<br />
head and there were even traces of red paint near<br />
the dent. The undercarriage was again retracted<br />
this time with the toggle disconnected and the<br />
pin fixed in the upper toggle. It was seen that the<br />
undercarriage door got obstructed by the upper<br />
toggle link at exactly the same place where it was<br />
dented. It was therefore deduced that the ac had<br />
taken off with the nose wheel toggle disconnected<br />
and this had caused the nose undercarriage not<br />
getting locked up and the red light remaining ‘ON’,<br />
creating an emergency in air.<br />
Exact Cause of Failure<br />
Parking for AF aircraft in Mumbai is such, that it<br />
requires being towed out of the slot during refuelling<br />
or just before starting. In this case the ac was towed<br />
out twice for refuelling and also just before departure<br />
at around 1915h. During towing the nose wheel<br />
toggle link is disconnected from the nose wheel<br />
steering jack. However, in this case the ground crew<br />
INDIAN AIR FORCE 2 0 1 2 N o v e m b e r Aerospace Safety 15