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International Dyestuff Industry - ColorantsHistory.Org

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Figure 4. Chlorine Ovens. Edelstein Collection, Hebrew University.<br />

The end manholes were slabs of wood covered with lead. The ovens were charged through<br />

openings at dd (b in the cross section), and the lids to these were made airtight with a<br />

liquid seal of "chlorine oils," the residual oil from the reaction, which was placed in the door<br />

channels. Lead piping was used to deliver the chlorine and carry away hydrochloric acid and<br />

unreacted chlorine from the last stages of the chlorination. Since this caused loss of the<br />

valuable reagent, the ovens were then operated in pairs so that outgoing gas from the first<br />

oven was then passed into the second.<br />

The next day a new charge of anthracene was placed in the first oven, the incoming gas<br />

was then directed into the second oven, to complete chlorination, and then passed through<br />

the fresh charge. By this continuous alternation in the supply of chlorine, losses were<br />

minimized.<br />

A steam chamber was built into the surrounding brickwork to maintain the desired<br />

temperature. Hydrogen chloride gas was recovered for re-use by condensation in coke<br />

towers. Wooden tools were used to loosen the crystalline dichloroanthracene remaining in<br />

the oven, which was then transferred to tubs and broken up in the presence of caustic soda<br />

which neutralized the hydrochloric acid. The product was afterwards separated from the<br />

solution and hydraulically pressed between linen cloths to remove unwanted materials as<br />

the “chlorine oils.”<br />

The resulting crystalline cake then underwent further purification by repeated breaking up,<br />

soaking in coal tar naphtha, and pressing. Any residual naphtha was recovered by steam<br />

treatment. Finally, the product dichloroanthracene was dried on trays in a drying room and<br />

was found to be about 84 per cent pure.<br />

In the important sulfonation step, the dichloroanthracene was treated with sulfuric acid in<br />

iron pots, each capable of holding about 30 gallons of liquid, and fixed in place in rows<br />

above ovens. The whole arrangement was surrounded by brickwork to retain heat (Perkin’s<br />

Figure 5).

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