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AMMJ Lessons Learnt In 45 Years of Condition Monitoring 26<br />

Case study 4<br />

The new graduate engineer hooked up the accelerometer via the long cable reel to the signal conditioning/<br />

readout instrument. He reported that turbine vibration was 55mm/s rms – over 10 times greater than what might<br />

be expected! Before panic set in, we found that he had used the cable to connect the accelerometer to the<br />

instrument. It was an ordinary shielded co-axial type, intended to be used from the instrument to an analyser. Low<br />

noise cables are required from charge output accelerometers to avoid tribo-electric boosting of the output to give<br />

a spurious high vibration reading.<br />

Case study 5<br />

Lesson #13 Check, and recheck, critical data values if any look to be unusual.<br />

Using an innovative approach, site trim balancing<br />

was conducted on a 120MW generator rotor.<br />

The coupling between turbine and generator<br />

was unbolted, and faces held apart. The exciter<br />

was connected to run as a motor, with the rolling<br />

torque provided using the overhead crane and<br />

a rope wrapped around the rotor. (Appropriate<br />

design checks had been made).<br />

After reassembly, run-up proceeded as normal,<br />

until when nearing normal service speed<br />

generator bearing vibration suddenly jumped<br />

so much that the floor shook and dust fell from<br />

the rafters! The operator tripped the machine.<br />

Subsequent attempts at run-up were no different.<br />

A challenge for the vibration team! The gear<br />

was set up with the analyser set to PEAK HOLD<br />

mode. The extreme vibration was revealed as at<br />

19 Hz – the first critical speed of the rotor. It<br />

was noticed that the vibration started soon after<br />

the auxiliary oil pump was stopped, so it was<br />

left running and the unit was eventually put into<br />

service. The 19Hz vibration was still evident, and<br />

could be varied in amplitude by changing the oil<br />

temperature.<br />

Bearing dimensions and clearances were found, and the bearing wedge pressures (giving shaft loading) and oil<br />

temperatures noted to calculate the Load Parameter. The resulting plot on a bearing stability assessment chart<br />

showed that the operating range was well outside the “recommended” area (ESDU 1966), as shown in Figure 5.<br />

The only variable that could be changed permanently was the length of the bearings (to increase the specific<br />

loading). Surprisingly, the spares in the store were found to be shorter, as were those on the adjacent “identical”<br />

machine! Bearing changeover was the cure. This was a strange case, as this machine had operated 17 years<br />

without this problem. The vibration team gained superhero status for this success. (Beebe, 2002).<br />

CM by performance analysis – the big bucks<br />

Case study 6<br />

Fig 5 Bearing stability chart showing effect of oil viscosity<br />

and bearing length<br />

Load parameter W’<br />

Original<br />

operation<br />

Operation<br />

when<br />

bearings<br />

modified<br />

I had developed performance tests for both types of 200MW machine at Hazelwood with useful outcomes and<br />

continued this at Yallourn W. The methods followed had since been published (ASME, 1970). On one unit, our<br />

tests were run before the official acceptance tests.<br />

Routine tests on a 350MW unit showed a small but significant decline in performance. Prior to a planned outage, a<br />

steam forced cool was conducted. This procedure is used to bring the machine to standstill more quickly by cooling<br />

the turbine metal, rather than allowing slow natural cooling. The inlet steam temperatures were slowly decreased<br />

over some hours during offloading. Testing after return to service showed that the performance has returned to its<br />

initial level. Close examination of the data concluded that there was some restriction in the intermediate pressure<br />

section, deduced to be from blade deposits (Beebe, 1978).<br />

Soon afterwards, the OEM site manager met with the plant manager to tell him that as the first unit had<br />

reached 2 years of service, it was time to arrange a major outage and stripdown. When asked the reason for the<br />

recommendation he was told that an inspection after two years was standard practice in the OEM’s country. The<br />

manager had been my boss and mentor in my initial job, so was well versed in CM! He did not support an overhaul<br />

given our vibration and performance condition assessment, and the machine continued to operate for 17 years<br />

before its high pressure section was opened.<br />

Lesson #14 Take OEM recommendations into careful consideration,<br />

but do not follow them blindly.<br />

10<br />

1.0<br />

0.1<br />

Oil 71°C<br />

Oil 40°C<br />

Lines of<br />

increasing<br />

constant b/d<br />

Increased risk of halffrequency<br />

whirl<br />

0.1 0.5 0.9<br />

Eccentricity ratio<br />

Recommended<br />

area<br />

Bearing<br />

too short<br />

Vol 24 No 2

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