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Journey of Improvements in Beehive <strong>Coke</strong> Conversion for Better Quality<br />

of <strong>Coke</strong> for Blast Furnaces<br />

Dhirendra Prasad, P. C. Choudhary & Sandip Bhattacharya<br />

1. Introduction<br />

Tata Steel, Jamshedpur, India<br />

Steel industry is cyclic in nature and demand for steel fluctuates according to the<br />

economic scenario of country. In the course of high demand of steel, the iron<br />

making capacity of Tata Steel, India was increased in several expansions<br />

projects completed during year 2003, 2005 and 2008.<br />

Enhanced capacity of blast furnaces at Tata Steel, India created the requirements<br />

of additional metallurgical coke of 1 million tons per annum which was beyond<br />

the coke making capacity of around 2.3 million tons per annum existed during<br />

year 2003-04. The requirement of extra coke was further augmented due to<br />

shutting down of some of the coke ovens at Tata Steel, India for rebuilding and<br />

repairing. The requirement of additional coke was temporarily fulfilled by either<br />

import or by coke conversion through beehive ovens (outsourcing). During<br />

2003-06, Tata Steel had sourced 15000 to 20000 tons per month of metallurgical<br />

coke through coke conversion route which further got increased to 35000 to<br />

40000 tons per month (during 2007-08). Beehive coke ovens are situated in<br />

Dhanbad and Ramgarh district in the state of Jharkhand, India. Tata Steel<br />

supplied coals and received coke after conversion from various beehive coke<br />

ovens through conversion agents at predetermined rate.<br />

<strong>Coke</strong> supplied during initial period of coke conversion was not meeting the<br />

quality requirements of blast furnaces. It created confusion and poor confidence<br />

of procurement of coke through coke conversion route. A series of affirmative<br />

actions were initiated to achieve the required levels of quality in converted<br />

beehive coke. The present paper describes the journey of coke conversion from<br />

bad to good period and various improvement initiatives undertaken to achieve<br />

target levels of coke quality during the last one decade.<br />

1


2. Description of Beehive <strong>Coke</strong> <strong>Oven</strong>s<br />

2.1 Basic design: Beehive coke ovens are very small in capacity. A battery<br />

usually consists of 12 - 16 ovens and is arranged symmetrically back to back<br />

with 6 - 8 ovens on one side. Normally the capacity of each oven varies from 5<br />

to 6.5 tons of coal charge. The capacity of beehive ovens varies from about<br />

1200 to 1600 tons coke per month per battery. A beehive oven generally<br />

consists of 2 batteries and in some cases more than 2 batteries. The structure is<br />

not exactly like a beehive but a rectangular box having an arched rooftop (figure<br />

1). The front has a door, which is fixed between channels. The oven bricks are<br />

made out of silica and there are no supporting members as in normal coke plant.<br />

There are charging holes form the top.<br />

Fig 1: Beehive <strong>Coke</strong> <strong>Oven</strong><br />

2.2 Heating system: There is no provision for external heating and it gets<br />

heated due to burning of volatile matter in the coal. The heat content of the<br />

burnt gases is utilized for heating the sole & arched rooftop. The sole is heated<br />

from bottom because of burnt hot gases pass below it. The hot burnt gases flow<br />

2


from top of the charge to two flues, located at the bottom of the sole and then<br />

through the chimney. Some oven pairs have individual chimneys while most of<br />

them have common chimney. There are coarse & fine control devices for<br />

controlling the draft in these chimneys.<br />

2.3 Coal Crushing & Charging: The top of the battery has rail tracks running<br />

along the length of the battery. Manually pushed trolleys are used for transfer &<br />

charging of coal into the ovens. Each trolley has a capacity of about 1 ton. The<br />

coal is crushed in small crushers and loaded into these trolleys. Normally 5-6<br />

trolleys filled with coal is collected on the top near the charging hole before<br />

charging is done.<br />

2.4 <strong>Coke</strong> Pushing: The front door is lifted using a winch system to open the<br />

oven. The hot coke is pulled out from the oven using a plough type of iron<br />

structure. Manual scraping is done to remove remaining portion of coke from<br />

inside the oven. The front door is lowered to close the oven. Quenching is done<br />

manually using water hosepipe on the platform where the hot coke is pulled out.<br />

2.5 Advantages & Disadvantages in Making <strong>Coke</strong> through Beehive <strong>Oven</strong>s:<br />

Advantages:<br />

1) Good quality, strong & blocky coke.<br />

2) Low capital & operating cost.<br />

3) <strong>Coke</strong> production is not connected with the availability of a market for byproducts.<br />

4) Environmental friendly as it is emission free, no handling of effluents etc.<br />

Hence creates no pollution issues.<br />

Disadvantages:<br />

1) No recovery of byproducts.<br />

2) Lower coke yield due to partial combustion.<br />

3) Production of quality coke only from good coking coals (blend of inferior<br />

coal can't be used).<br />

4) Lack of flexibility in operation.<br />

3


2.6 Specifications of Coals Supply:<br />

Specification of coal supplied by Tata Steel for conversion is shown in table 1.<br />

Coal Source Ash V.M. Moisture Coal in Blend<br />

Imported 10 % max. 23.5 %<br />

max.<br />

8 % max (may<br />

go up to 10%<br />

during<br />

monsoon)<br />

50 % or (Semi<br />

Soft - 30 %,<br />

Jellinbah- 20<br />

%)<br />

Captive<br />

(Jamadoba )<br />

17 % max. 24 % max. 9.5 % max<br />

(may go up to<br />

10% during<br />

monsoon)<br />

50 %<br />

Table 1: Specification of coal supplied by Tata Steel for conversion<br />

3. Challenges<br />

Problems were faced with respect to coke quality during initial stage of<br />

conversion of coal to coke through beehive oven route. The CSR of coke which<br />

is one of the vital parameters for coke quality was found varying significantly<br />

from ovens to ovens and even within a beehive oven battery. Also, the CSR<br />

values were low and varying in the range of 35-45. Blast furnace operators<br />

refused to charge such low CSR coke in to the blast furnaces. Therefore,<br />

challenge was taken to improve the CSR of beehive coke to above 60 as well as<br />

its consistency.<br />

As per the agreement between Tata Steel and conversion agent, maximum<br />

allowed moisture in converted beehive coke received at Jamshedpur works was<br />

10%. But, actual beehive coke moisture received at Jamshedpur works was<br />

15.1% (average). The undersize (-10 mm) in coke was approximately 3.55%.<br />

High moisture in beehive coke resulted in loss in coke yield, increased<br />

transportation cost and finally caused increase in blast furnace fuel rate. High<br />

fines in beehive coke resulted in coke yield loss and increased cost of<br />

transportation. Hence, challenge was taken to reduce beehive coke moisture by<br />

4


5% and fines (undersize) by 2% by improvements in processes for coke<br />

quenching and handling at beehive coke ovens.<br />

4. Analysis Phase<br />

A detailed cause and effect diagram (figure - 2) was prepared for a root-cause<br />

analysis of possible reasons which could lead to poor quality as well as<br />

inconsistency in the quality of coke from the beehive coke ovens.<br />

Coal<br />

Quality<br />

Operating<br />

Conditions<br />

Dispatch &<br />

receiving<br />

High Moisture<br />

High gap between pushing & charging<br />

Lack of control of air supply<br />

Deterioration on quality while loading<br />

Variability in input coal quality & Mix-ups<br />

Mode of transport<br />

Poor coking property<br />

Inadequate water for quenching<br />

Delay/early coke pushing<br />

Deterioration on quality while travel<br />

Improper crushing fineness<br />

No. of loading & receiving points<br />

Supervision<br />

Monitoring<br />

Analysis & Improvement<br />

Lack of storage facility<br />

Poor oven design conditions<br />

Inadequate control on leakage<br />

Inadequate control on air supply<br />

Improper blending<br />

Lack of instrumentation<br />

Lack of coke making knowledge<br />

Lack of blending facility<br />

Improper insulation<br />

Lack of knowledge sharing<br />

Long quenching time<br />

Non-availability of timely<br />

technical information<br />

Pilferage<br />

Sample collection & Preparation<br />

Lack of knowledge on<br />

coke quality parameters<br />

Lack of awareness<br />

training to operators<br />

Large no. of stages<br />

Sampling & quality control<br />

Standard Procedures<br />

Large no. of samples<br />

Poor <strong>Coke</strong><br />

Quality<br />

&<br />

Inconsistency<br />

Lack of instrumentation & testing facilities<br />

Process<br />

Control<br />

<strong>Oven</strong>/Process<br />

Design<br />

Knowledge<br />

& Training<br />

Inspection<br />

& Testing<br />

Fig. 2: Cause and Effect Diagram for poor quality of <strong>Coke</strong> from<br />

Beehive <strong>Coke</strong> <strong>Oven</strong>s.<br />

Most of the beehive ovens were of basic design and had no instrumentation for<br />

process control. One of major problems noticed that persons deployed as oven<br />

operators were unskilled and not aware of fundamentals of metallurgical coke<br />

making. Moreover, there was no penalty clause existed in commercial terms and<br />

conditions with conversion agents to ensure supply of good quality and quantity<br />

of coke from beehive ovens to Jamshedpur works.<br />

After thorough analysis of previous coke conversion processes, it was found that<br />

documented system was not available for coal management, carbonization and<br />

5


coke handling processes with beehive ovens operators. Written procedures were<br />

also not found for quality assurance activities like sampling, sample preparation<br />

and analysis of coal and coke. With respect to coal handling system, it was<br />

observed that no distinct demarcation was being maintained between various<br />

received coals (Semi Soft / Jamadoba/ HCC (imported hard coking coal) / WB<br />

(west bokaro) and blended coal) in the premises of beehive ovens. Different<br />

types of coal had no nameplates or display board for proper identification.<br />

Various individual coals were dumped haphazardly near the blended coal. Coals<br />

were stored in open areas which resulted in moisture gain during rains. It was<br />

also observed that process was not followed for coal usage based on the<br />

principle of “first in, first out” (FIFO) to avoid usage of weathered coal. Latest<br />

received coals were being utilized first. Crushing fineness of blended coals was<br />

inadequate. Stock management of various coals was poor.<br />

Assessment of old practices of coke quenching and handling system at beehive<br />

coke ovens was carried out. It was observed that the time elapsed between coke<br />

pushing and coal charging was very high and varying. The heat condition of the<br />

battery was poor which resulted in green coke pushing (un-carbonized / partially<br />

carbonized coke). This might led to the weakening of coke and generation of<br />

fines. Leakages through the door were noticed. In some of the ovens, whole<br />

bricks from the door were collapsed before coke pushing. Poor sealing of doors<br />

and opening of oven top covers was found in a number of ovens. Cracks on<br />

walls were also observed. Carbonization time was not being adjusted according<br />

to the coal moisture to get good quality of coke. After pushing from ovens, coke<br />

was not quenched immediately due to unpreparedness of quenching system<br />

which resulted in coke burning. Lots of green pushing was observed because of<br />

poor process control.<br />

It was observed that a single big hosepipe was being utilized for coke quenching<br />

with water. This led to requirement of more volume of water for completing the<br />

coke quenching because single stream of water could not cover entire hot coke<br />

pile at a time. This resulted in high moisture (15-17%) in dispatched coke. High<br />

moisture in coke resulted in sticking of fines on lump coke. It was also noticed<br />

that for coke quenching, uncontrolled and continuous single stage quenching<br />

operation was practiced. Quenching was being done continuously for 15-25<br />

minutes duration. Also, the quenching of coke was practiced without dispersing<br />

the red hot coke pile after the pushing. This caused inadequate quenching of hot<br />

coke inside the pile and restricted removal of fines. Velocity of water in single<br />

hosepipe was not sufficient to flush out the fines. Other observations were made<br />

6


like improper cleaning of platform and high tonnages of left out platform ash at<br />

each of the beehive ovens. This caused sticking of fines on to lump coke.<br />

Segregation of coke was not being done to separate out bad coke from good<br />

coke after the completion of quenching although there were evidences of green<br />

coke pushing. High percentages of moisture and fines in dispatched beehive<br />

coke were due to inappropriate process of quenching and coke handling<br />

operations at beehive coke oven.<br />

Based on the root-cause analysis, requirement was felt for implementations of<br />

beehive coke oven management systems for following purposes:<br />

1. Improvements in coal receiving and handling system to<br />

a. Avoid use of weathered coal.<br />

b. Prevent mixing of various coals in a beehive oven.<br />

c. Improve coal crushing fineness.<br />

d. Ensure proper blending of coal as decided by Tata Steel.<br />

2. Improvements in carbonization operations and coke handling system<br />

to<br />

a. Adjust carbonization time depending upon coal moisture to<br />

get proper coke.<br />

b. Improve heat condition of the battery.<br />

c. Avoid green pushing (un-carbonized / partially carbonized<br />

coal).<br />

d. Proper sealing of doors and lifting of openings on oven top.<br />

e. Avert delay in quenching of coke which may cause coke<br />

burning.<br />

f. Sorting of good quality coke for dispatch.<br />

5. Improvement Phase<br />

One of the major observations made during the analysis phase was lack of<br />

proper information about the various operating conditions of the ovens.<br />

Therefore, a format was designed and implemented to systematically capture<br />

data for further analysis and improvements. Table 2 presents the format and<br />

some typical data of beehive oven operation during initial period.<br />

7


Sl.<br />

No.<br />

<strong>Oven</strong><br />

No.<br />

Wt. Of<br />

Coal<br />

Charge<br />

( MT )<br />

Charging<br />

( A )<br />

Pushing ( B )<br />

Date Time Date Time<br />

Carbon<br />

-ization<br />

(Hours)<br />

Time<br />

(B-A)<br />

Next Charging<br />

( C )<br />

Date<br />

Time<br />

Time<br />

between<br />

pushing<br />

to next<br />

charging<br />

(Hours),<br />

(C-B)<br />

Cycle<br />

time ,<br />

(Hours)<br />

(C-A)<br />

Empty<br />

oven<br />

temp.<br />

prior to<br />

charging<br />

, ( 0 C)<br />

Carbon<br />

-ization<br />

Temp.<br />

( 0 C)<br />

Quenching<br />

time,<br />

(Min.)<br />

1 25 5.500 16.9.03 18.30 18.9.03 6.00 35.30 18.9.03 8.45 2.45 38.15 640ºC 935ºC 50<br />

2 25 5.500 18.9.03 8.45 19.9.03 17.00 32.15 19.9.03 19.15 2.15 34.30 650ºC 943ºC 40<br />

3 25 5.500 19.9.03 19.15 21.9.03 2.30 31.15 21.9.03 5.00 2.30 33.45 640ºC 940ºC 45<br />

4 27 5.500 15.9.03 24.00 17.9.03 10.45 34.45 17.9.03 12.45 2.00 35.45 660ºC 960ºC 55<br />

5 27 5.500 17.9.03 12.45 18.9.03 23.30 34.45 19.9.03 1.40 2.10 36.55 630ºC 950ºC 48<br />

6 27 5.500 19.9.03 1.40 21.9.03 12.40 35.00 21.9.03 14.25 1.45 36.45 680ºC 975ºC 40<br />

Table 2: Some typical data of beehive coke oven operation during initial period<br />

Processes for coal receiving, storing, crushing, blending and charging were<br />

developed and implemented across all beehive ovens at Dhanbad and Ramgarh<br />

area. Quality assurance systems for coal handling, carbonization operation and<br />

coke handling were developed and implemented in all beehive ovens. Written<br />

procedures were made for quality assurance activities for incoming raw<br />

materials (coal), in process materials (coal/coke) and product coke. Series of<br />

training sessions were organized by Tata Steel experts for all staffs of beehive<br />

ovens, conversion agency and third party quality assurance (QA) agency.<br />

Frequent audits were conducted by Tata Steel personnel on various activities<br />

starting from coal dispatch to coke received. Flow chart of various activities<br />

under new quality assurance system starting from Tata Steel washeries to<br />

beehive ovens for coke conversion and coke dispatch from beehive ovens to<br />

Jamadoba siding and Jamshedpur works of Tata Steel India are represented in<br />

figures 3 - 5.<br />

Temporary/permanent sheds were erected for coal & coke storage to prevent<br />

moisture gain during rains in all beehive ovens. For proper identification, coals<br />

received from different sources were stock-piled source-wise with different<br />

geometrical shapes and proper identification marks. Demarcation between<br />

individual coals and blended coal were maintained. Individual coals were not<br />

allowed to be stored nearer to blended coal to avoid mix-ups. The quantities of<br />

crushed coal for blending were ensured according to the capacity of oven before<br />

8


charging. Crushing fineness of coal was improved by proper preventive<br />

maintenance of crusher and screener (used for sieving the coal). The blending<br />

ratio of different coals was maintained as per weight volume assessment on the<br />

advice of Tata Steel experts.<br />

The time gap between coke pushing & coal charging was brought down to 30-<br />

40 minutes from 150 minutes by ensuring preparedness of resources like<br />

availability of power for pulling out the coke, readiness of quenching system,<br />

ensuring crushed coal for next charging etc. Heat condition of the battery was<br />

improved by implementation of new process monitoring and control system.<br />

Sealing of doors and openings on the oven top were ensured. Cracks on walls<br />

were repaired. In the case of oven door collapse, use of castable was suggested<br />

in place of bricks. More focus was given on maintenance and proper sealing of<br />

oven doors. Adjustment of carbonization time was started depending upon coal<br />

moisture to get proper coke. Operators were asked to observe the performance<br />

of oven during carbonization while keeping secondary port holes (including side<br />

ovens) open.<br />

<strong>Oven</strong> temperature measurement was started on routine basis for better process<br />

monitoring and control. <strong>Oven</strong>s operators were advised to maintain proper<br />

records of various process parameters. Green pushing was eliminated by proper<br />

process control of carbonization operation. It was ensured that the oven platform<br />

(wharf) is kept free from foreign materials like oven clay, brick pieces, platform<br />

ash / dust etc. before starting of discharging of oven. Required amount of<br />

crushed coal was kept ready for next feed before the coke pushing operation. It<br />

was sometimes found that some coke materials were still remained inside the<br />

oven after the dragging of hot coke from the oven, this material was taken out<br />

carefully and stocked separately with proper identification marks.<br />

9


Jamadoba washery Bheltand washery West Bokaro washery<br />

Quantity check & physical<br />

observation<br />

Process of coal<br />

loading<br />

Quality check<br />

Physical verification of empty<br />

truck, tarpaulin, Wooden Plate<br />

& rope<br />

Truck entry for coal<br />

loading<br />

---<br />

Checking of issue slip given by<br />

conversion agent<br />

Issue of loading slip ---<br />

* Checking of weighment for<br />

tare weight of truck<br />

Truck weighment<br />

(Tare)<br />

Maintaining register and report<br />

format of weighment truck and<br />

reporting to concerned<br />

authorities/QA agency<br />

Checking by QA agency,<br />

issued slip, gross & tare weight<br />

of coal loaded truck & sample<br />

collection during loading<br />

* Coal loading into<br />

the truck/ weighing<br />

(Gross)<br />

Sample preparation for analysis<br />

of moisture, ash & V.M.<br />

Checking of truck cover with<br />

tarpaulin & proper sealing<br />

Truck desptch to<br />

Beehive coke ovens<br />

Maintaining register and report<br />

format in remarks column<br />

Coal receipts to beehive ovens (Dhanbad<br />

& Ramgarh area)<br />

Remarks :- ( * ) Representative of Transporter to be present during the time of truck weighment (Gross & Tare) of coal & coke.<br />

Fig. 3: Activities at Washeries of Tata Steel Ltd.<br />

10


Coal receipts at beehive ovens<br />

(Dhanbad & Ramgarh area)<br />

Quantity check & physical observation<br />

Process of coal<br />

receipt & dispatch to<br />

beehive ovens<br />

Quality check (Moisture, Ash & V.M.)<br />

Physical verification of coal loaded trucks<br />

and checking of issue/ dispatch slip,<br />

tarpaulin, rope, wooden plates & sealing<br />

Coal receipts at<br />

beehive ovens and<br />

coke dispatch from<br />

beehive ovens<br />

---<br />

* Checking of weighment for gross & tare<br />

weight of coal loaded trucks. Calibration<br />

of beehive oven weighbridge checked<br />

Truck weighment<br />

Maintaining register and report format of<br />

weighment truck and reporting to<br />

concerned authorities/QA agency<br />

Stock measurement of coal every month<br />

end, physical verification of coal on day to<br />

day basis<br />

Stocking of coal<br />

Source-wise sample collection during coal<br />

unloading & sample preparation for<br />

moisture, ash & V.M.<br />

Calibration of pay loader bucket and<br />

maintaining the number of buckets of<br />

blended coal<br />

Calibration of oven trolley, weighment of<br />

charging coal per trolley checked, sample<br />

collection in three shifts & sample<br />

preparation for quality<br />

Supervision for low quenching, maintaining<br />

coking periods, checking of oven leakage<br />

& sample collection in three shifts<br />

Supervision for coke sizing at platform /<br />

stock yard, segregating the under size<br />

coke<br />

Supervision for coke loading from<br />

stockyard by 40mm fork shovel, checking<br />

the issue memo & sample collection during<br />

coke loading<br />

Checking of truck cover with tarpaulin &<br />

proper sealing<br />

Supervision of coal<br />

blending<br />

Coal charging<br />

<strong>Coke</strong> production<br />

Sizing of coke<br />

<strong>Coke</strong> loading<br />

Truck dispatch<br />

Maintaining register & blend format with<br />

signature of beehive oven representatives,<br />

conversion agent and QA agency<br />

Maintaining register with oven wise coal<br />

charged, maintaining charging format,<br />

reporting day-wise to concerned<br />

authority/office and analysis of ash &<br />

V.M.<br />

Maintaining register with oven wise coke<br />

production, maintaining format of cooking<br />

periods, reporting day-wise to concerned<br />

authority/office and analysis of ash &<br />

V.M.<br />

Reporting of all day activities on daily<br />

basis to offices and noted in reporting<br />

format<br />

Maintaining register as well as format of<br />

loaded truck and reporting to concerned<br />

authorities/office with daily observation.<br />

Samples of quality part sent to Dhanbad<br />

office for total moisture, ash & V.M.<br />

Maintaining register and report format in<br />

remarks column<br />

Dispatch from beehive coke oven to Tata Steel Ltd.-Jamadoba<br />

and Tata Steel Ltd. Works- Jamshedpur<br />

Remarks :- ( * ) Representative of Transporter to be present during the time of truck weighment (Gross & Tare) of coal & coke.<br />

Fig.4: Activities at Beehive <strong>Coke</strong> <strong>Oven</strong>s<br />

11


<strong>Coke</strong> receipt at Tata Steel Ltd. - Jamadoba<br />

and Tata Steel Ltd. - Works Jamshedpur<br />

<strong>Coke</strong> receipts at Jamadoba railway station siding (By road)<br />

<strong>Coke</strong> receipts by road from Ramgarh & by rail from<br />

Jamadoba Coal Processing Plant (JPCC) siding<br />

Quantity check &<br />

physical verification<br />

Process<br />

of coke<br />

receipts<br />

Quality check<br />

Quantity check & physical verification<br />

Physical verification<br />

of loaded trucks,<br />

checking of dispatch<br />

memo, tarpaulin<br />

cover, wooden plate<br />

& rope sealing<br />

* Weighment<br />

checking for gross<br />

& tare weight of<br />

coke truck<br />

Sample collection<br />

during coke<br />

unloading and size<br />

analysis<br />

<strong>Coke</strong><br />

receipts at<br />

Jamadoba<br />

railway<br />

siding<br />

Truck<br />

weighment<br />

<strong>Coke</strong><br />

trucks<br />

unloading<br />

at<br />

Jamadoba<br />

Railway<br />

Siding<br />

Physical verification of coke loaded trucks/wagons,<br />

sample collection during coke unloading, size analysis<br />

& sample preparation for quality<br />

Maintaining registor as well as format of loaded<br />

Maintaining register trucks/wagons and reporting to concerned<br />

and report format of authorities/office with daily observation. Samples of<br />

weighment truck and quality part sent to Dhanbad office for total moisture,<br />

reporting daily basis<br />

ash & V.M.<br />

to concerned<br />

authorities/office<br />

Sample preparation<br />

for quality and<br />

analysis of total<br />

moisture, ash &<br />

V.M. at Dhanbad<br />

office<br />

System of Reporting<br />

1. Daily - coal received, operation<br />

monitoring, charing/production, coke<br />

desptach & observation report (by Road).<br />

Sample preparation<br />

Physical verification<br />

<strong>Coke</strong><br />

for quality and<br />

of wagons, sample<br />

3. Reporting of coke despatch/receipts<br />

loaded /<br />

analysis of total<br />

collection during<br />

quantity, quality & under size (-10mm),<br />

despatched<br />

moisture, ash &<br />

wagon loading, size<br />

ash% ( by Rail).<br />

to wagons<br />

V.M. at Dhanbad<br />

analysis<br />

office<br />

4. Monthly - quantity report (GRN Sheet).<br />

5. Monthly - quantity & quality report.<br />

6. Abnormilities report.<br />

7. Reporting of improved process controll.<br />

Remarks :- ( * ) Representative of transporter to be present during the time of truck weighment (Gross & Tare) of coal & coke.<br />

--<br />

Quality check<br />

2. Daily - quantity & quality report of<br />

coal/coke despatch/receipts, charging &<br />

production size analysis of coke<br />

despatch/receipts and under size (-10mm),<br />

ash % (by Road).<br />

Fig.5: Activities at Jamadoba & Jamshedpur Siding.<br />

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Quenching system was made ready before pushing (dragging) of coke.<br />

Checking of water level in tank and condition monitoring of motor & pump<br />

used for quenching was started. The reservoir containing quenching water was<br />

cleaned periodically by the oven operators to make it free from contamination.<br />

Pump with 10 HP motor was arranged in each beehive ovens for quenching of<br />

hot coke mass with water. This ensured high pressure of water jet which helped<br />

in flushing out of fines from coke lumps which generally contains high ash.<br />

Proper preparedness helped in avoidance of delay in quenching of coke which<br />

was causing coke burning earlier. Two hosepipes were provided in place of<br />

single big hosepipe in all ovens. Quenching of hot coke mass was executed by<br />

using two hosepipes. Quenching by two hosepipes helped in proper quenching<br />

of hot coke mass simultaneously from two sides with less water. Two stage<br />

quenching was implemented in all ovens. Total quenching time was kept at 6<br />

minutes as against 40-50 minutes previously. In first stage coke was sprayed<br />

with water for 3 minutes after pulling (dragging) it out from oven. Then the<br />

partly cooled coke mass was spread out with the help of spikes. Again in second<br />

stage, water spraying was carried out covering the entire coke mass for 2-3<br />

minutes. Spot quenching was followed in the case of localized hot coke.<br />

After quenching the hot coke with water, it was suggested to leave the coke<br />

undisturbed on the platform for a period of 2-3 hours for further evaporation of<br />

moisture. It helped in reduction of moisture in dispatched coke. Sizing of coke<br />

lumps was conducted manually on platform or at stockyard, keeping the coke<br />

size between +40 to -100 mm. After completion of process of sizing, the sized<br />

coke was shifted from the platform to the stock yard by lifting it with the help of<br />

a +40 mm forked shovel. This helped in reducing the fines in dispatched coke.<br />

Finally sized coke loaded directly from the stockyard into the carriage by using<br />

a + 40 mm forked shovel. The remaining materials (-40 mm coke fraction) left<br />

at the stockyard were stored separately by lifting it with the help of plain shovel.<br />

The size analysis of – 40 mm coke conducted on day to day basis at each<br />

beehive oven. Subsequently, +10 mm size coke dispatched to Tata Steel<br />

Jamshedpur works along with the sized coke (+ 40 to -100 mm).<br />

After completion of loading, trucks used for transportation were covered with<br />

tarpaulin and sealed with plastic seals with unique numbers and the same were<br />

mentioned in the delivery slip/ memo. The rope used for sealing was tied with<br />

double roll technique. This was implemented to eliminate any malpractices<br />

during transportation of converted coke to Jamshedpur works. Truck-wise size<br />

analysis of dispatched coke was conducted at each beehive oven before<br />

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dispatching and was made available with the truck. Old contract with<br />

conversion agents was modified and penalty clause was introduced for lower<br />

CSR, higher moisture and fines in supplied beehive coke.<br />

6. Results & Discussion<br />

In improvement phase, several new systems were implemented which had given<br />

positive results and helped in fulfilling the coke quality requirement of blast<br />

furnaces. Initial period of improvements was focused on coal management and<br />

proper process control of carbonization process which resulted in improvement<br />

in CSR values as shown in figure 6 & 7.<br />

Fig. 6: CSR values (individual data) of Beehive <strong>Coke</strong> from year 2003 to 2009<br />

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Fig. 7: CSR values (yearly average) of Beehive <strong>Coke</strong> from year 2003 to 2009<br />

It can be observed from figures 6 & 7 that during starting period (year 2003) of<br />

coke conversion, CSR values of beehive coke were at the levels of 35-45 with<br />

high standard deviation. Then during year 2004, CSR values were gradually<br />

improved and went above 60 with improvement in its standard deviation. After<br />

that, CSR values were remained in the range of 60. During year 2007, some new<br />

beehive ovens were introduced which resulted in some drop in CSR values.<br />

After horizontal deployments of improvement initiatives in newly introduced<br />

ovens, CSR values regained its original range of 60 and above. In the these<br />

figures, standard deviation of CSR values was improved during year 2004 and<br />

remained in the level of 3 till 2007. Afterward standard deviation has improved<br />

in year 2008.<br />

After achieving desired levels of CSR values, next improvement initiatives were<br />

focused on coke quenching and handling system which resulted in reduction of<br />

moisture and fines contents of beehive coke as depicted in figures 8 & 9.<br />

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Fig. 8: Percentage of Moisture of Beehive <strong>Coke</strong> received before and after<br />

implementation of Improvement Initiatives.<br />

Fig. 9: Percentage of undersize in Beehive <strong>Coke</strong> received before and after<br />

implementation of Improvement Initiatives.<br />

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It can be seen from figures 8 & 9 that moisture and fines levels in beehive coke<br />

received at Jamshedpur works were in the range of 14-16% and 3-4%<br />

respectively before the implementation of improvement initiatives till August<br />

2008. After implementation of various recommendations moisture and fines<br />

levels had reduced to below 10% and 1.5% respectively. Time duration in coke<br />

pushing to next coal charging had come down from over 150 minutes to 30-40<br />

minutes due to readiness of coal charging arrangement. Quenching time was<br />

reduced from over 40-50 to 6 minutes. This was primarily due to<br />

implementation of two stage quenching technique and use of two hosepipes<br />

simultaneously. This initiative had minimized burning of hot coke, hence, the<br />

reduction in ash content and improvement in coke strength. Reduction in overall<br />

cycle time had contributed significantly in maintaining a higher empty oven<br />

temperature (gone up from 650-950 to 930-1050 o C or even more) prior to<br />

charging. All these have contributed towards increasing the coke quality,<br />

productivity and consistency.<br />

7. Conclusion<br />

Beehive coke oven management system was developed and implemented at<br />

various beehive coke ovens batteries at Dhanbad and Ramgarh district of<br />

Jharkhand, India which were contracted for coal to coke conversion for Tata<br />

Steel. Significant improvements in coke quality in terms of coke CSR, moisture<br />

and undersize have been achieved from beehive coke ovens by means of various<br />

improvement initiatives discussed in the present paper.<br />

The above work helped in fulfilling the blast furnace requirement from beehive<br />

coke in terms of quality by giving more focus on process improvement, people<br />

development and without any major investment. This has ensured the<br />

procurement of good quality of coke through beehive coke conversion route<br />

which is also the cheapest source available as compared to other sources like<br />

import.<br />

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