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In Situ Francis Turbine Blade Replacement due to Gross Cavitation

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<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> <strong>Turbine</strong> <strong>Blade</strong><br />

<strong>Replacement</strong> <strong>due</strong> <strong>to</strong> <strong>Gross</strong> <strong>Cavitation</strong><br />

Author: Mr. Steven R. Potter, Sales Manager/ Welding Engineer<br />

Voith Hydro Services <strong>In</strong>c., 2885 Olympic Street,<br />

Springfield, OR 98478, USA. Tel: 541-868-1831<br />

Email:<br />

steven.potter@voith.com<br />

Presenter: Steven R. Potter, Sales Manager/Welding Engineer<br />

Voith Hydro Services, Western Region<br />

Original Presentation at 2012 HydroVision, Louisville KY<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

1


A brief explanation!<br />

<strong>In</strong> 2011, when this project, paper and presentation were<br />

started, Peak Hydro Services was a wholly owned<br />

subsidiary of Voith Hydro <strong>In</strong>c.<br />

Today Peak Hydro Services is proudly renamed<br />

Voith Hydro Services.<br />

No longer a subsidiary company; is an integral part of<br />

Voith Hydro <strong>In</strong>c.’s After Market Business group<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

2


<strong>In</strong> This Presentation<br />

• Project Facts and His<strong>to</strong>ry<br />

• Elements and Considerations of the business case<br />

• Powerhouse and Unit Description<br />

• Technical Aspects of Repair<br />

• Removal and <strong>Replacement</strong> of blades<br />

• Results and Conclusions<br />

• Acknowledgements<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

3


Project Facts and His<strong>to</strong>ry<br />

• Pointe du Bois, Mani<strong>to</strong>ba, Canada – Approximately 95 miles<br />

(150 kilometers) North East of Winnipeg, Mani<strong>to</strong>ba, Canada<br />

• On the Winnipeg River<br />

• First Unit in Service: 1911<br />

• Construction Completed: 1926<br />

• Construction Cost: $3.25 Million<br />

• Station Capacity: 78 MW<br />

• Average Annual Generation: 599 kWh<br />

• Waterfall Drop: 45 feet (14 Meters)<br />

• Powerhouse Length: 440 feet (135 Meters)<br />

• <strong>Turbine</strong> Genera<strong>to</strong>rs: 15 Double horizontal shaft <strong>Francis</strong><br />

<strong>Turbine</strong> Camelback units and 1 Straflo unit<br />

• Project Acquired by Mani<strong>to</strong>ba Hydro in 2002<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

4


Project Facts and His<strong>to</strong>ry<br />

• Mani<strong>to</strong>ba Hydro is the electric power and natural gas utility in<br />

the province of Mani<strong>to</strong>ba, Canada<br />

• Founded in 1961, as a provincial Crown Corporation<br />

• Operates 15 interconnected hydro generating stations<br />

• 527,000 electric power /263,000 natural gas cus<strong>to</strong>mers<br />

• Acquired Pointe du Bois in 2002; it is the oldest generating<br />

station; began operations in 1911<br />

• <strong>In</strong>itiated plans for $800 million Pointe du Bois modernization in<br />

2007<br />

• Approved <strong>to</strong> replace the 78MW powerhouse, dam and spillway<br />

with a 120-MW powerhouse<br />

• Construction projected <strong>to</strong> take six years with a planned inservice<br />

date of 2015<br />

• This plan was withdrawn in 2011<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Elements and Considerations of the Business Case<br />

• Fac<strong>to</strong>rs discussed are not definitive of Mani<strong>to</strong>ba Hydro’s<br />

business position - represented as some of the project<br />

considerations<br />

• With the Powerhouse replacement project cancelled – a<br />

smaller project was envisaged<br />

• Business case prepared <strong>to</strong> repair/res<strong>to</strong>re limited units<br />

• Several runners are grossly cavitated and some with partial<br />

loss of blades/band damage<br />

• Several units were shut down for safety<br />

• Some units partially disassembled and or being repaired<br />

• Refurbishment is a multiple year multiple unit project including<br />

mechanical, electrical and structural elements<br />

• The business case focused on Unit 13<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Elements and Considerations of the Business Case<br />

• Unit 13 is a double runner horizontal shaft <strong>Francis</strong> <strong>Turbine</strong>. The<br />

turbine casing consists of two cast iron halves<br />

• Station sees significant seasonal temperature changes which<br />

causes rise and fall of the structure and unit alignment issues<br />

• Mani<strong>to</strong>ba Hydro elected not <strong>to</strong> separate the casing on Unit 13<br />

• <strong>In</strong>itially attempted cavitation and other repairs in situ using in<br />

house employees and internal procedures<br />

• Results and progress resulted in reassessment<br />

• Decided <strong>to</strong> contract repairs <strong>to</strong> OEM’s in combination with,<br />

specialty hydro repair service providers, MH’s in house labor,<br />

engineering and project management teams<br />

• Both Unit 13 turbine runners exhibited extensive and gross<br />

cavitation<br />

• Upstream cavitation is worse (all units)<br />

• Runner bands were intact except for cavitation damage<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

8


Pointe du Bois Powerhouse Cross Section<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Elements and Considerations of the Business Case<br />

• Voith Hydro Canada’s Mississauga Ontario division were<br />

contracted with Peak Hydro Services (then a wholly owned<br />

subsidiary of Voith Hydro), now Voith Hydro Services<br />

• Peak (Voith) Hydro Services has more than twenty seven (27)<br />

years dedicated <strong>to</strong> Hydro Field Machining and Welding<br />

Services – Voith Hydro 135 years<br />

• Concluded the downstream runner of Unit 13 was salvageable<br />

• Upstream runner was in worse condition (true of all upstream<br />

runners at the plant)<br />

• Several blades exhibited gross cavitation with multiple through<br />

holes<br />

• <strong>Cavitation</strong> so deep preparation <strong>to</strong> clean sound parent metal not<br />

possible<br />

• Determined that a minimum of three (3) blades would need <strong>to</strong><br />

be replaced<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

10


Powerhouse Section and Pho<strong>to</strong>s<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Summary of the Business Case<br />

• Unit 13 Repair versus Replace<br />

• With significant repair work already performed, completing the<br />

runner repairs was substantially less cost than <strong>to</strong> replace<br />

• Repair lead time would be approximately half the replacement<br />

time<br />

• Return <strong>to</strong> service in approximately 14 months<br />

• ROI and time <strong>to</strong> breakeven were favorable<br />

• Successful repair would demonstrate viability of repairing other<br />

units and contribute <strong>to</strong> continuing station operations<br />

• Expected <strong>to</strong> extend unit operating life twenty (20) years<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Overhead view of typical unit with gates in place<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Typical Unit Cross Section<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Runner and Distribu<strong>to</strong>r Ring<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Technical Aspects of Repair<br />

• Unit 13 has two Horizontal <strong>Francis</strong> runners, each 99 inches<br />

diameter<br />

• Both upstream and downstream runners have thirteen (13)<br />

blades<br />

• Each blade had over its life time been repaired multiple times<br />

• Some areas of prior weld repairs were undermined (weld metal<br />

not adhering <strong>to</strong> base metal) <strong>due</strong> <strong>to</strong> improper preparation<br />

• ‘Foreign’ material (rebar) had been included as filler<br />

• All blades were severely cavitated<br />

• Major areas of cavitation on the suction side (typical) of the<br />

blades<br />

• Runner band cavitated adjacent <strong>to</strong> blade fillets<br />

• Two blades considered unrepairable, a third was marginal<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Typical condition of blades and band<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Technical Aspects of Repair<br />

• Metallurgical samples from runner crowns, bands and blades<br />

revealed chemistry similar <strong>to</strong> ASTM A27 Grade 70-36<br />

• Highly variable carbon content – classified as Medium Carbon<br />

Steel - Carbon Equivalent (CE) determines weldability<br />

• Repairs costs for in situ cavitation and blade replacements<br />

estimated <strong>to</strong> be substantially less than replacement runners<br />

• Return the unit <strong>to</strong> service one year earlier<br />

• Determined that the most cost effective and least risk repair<br />

was removal of three (3) blades by casting replacements<br />

• <strong>Blade</strong>s were 3D Laser Scanned<br />

• Data translated in<strong>to</strong> a CAD model and drawings from which<br />

blades were cast<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> prepared for Laser Scan<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Technical Aspects of Repair<br />

• Material and type dependent, castings are readily weldable<br />

• Casting structures of this era (1900-1920) are particularly<br />

prone <strong>to</strong> variable chemistry and are very porous<br />

• Water immersion of the components allows moisture <strong>to</strong> migrate<br />

throughout the casting filling those voids and pores<br />

• Moisture in the substrate not conducive <strong>to</strong> high quality defect<br />

free welding product<br />

• Trapped water pockets will flash <strong>to</strong> steam at exposure <strong>to</strong> the<br />

extreme temperatures of fusion welding<br />

• Gases become entrapped in the weld metal<br />

• Concern with the presence of entrapped water is the<br />

probability of hydrogen embrittlement of the material<br />

• Moisture must be removed<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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• Under magnification the<br />

structure can in places be seen<br />

<strong>to</strong> be a loosely joined series of<br />

voids<br />

• When submerged are<br />

eventually filled with water.<br />

• The Pointe du Bois runner<br />

castings contain gas pockets,<br />

pores, voids and casting dross<br />

(impurities)<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Technical Aspects of Repair<br />

• Primary welding process for all areas was Flux Core Arc<br />

Welding (FCAW), a derivative process of GMAW (MIG) welding<br />

• Repairs abutting prior repair zones required special<br />

consideration as they contain surface and subsurface<br />

discontinuities<br />

• Random discontinuities found at repair margins<br />

• Selectively used Gas Tungsten Arc Welding process (GTAW)<br />

• The skills applied by the welders proved very successful<br />

eliminating defects and providing acceptable repairs<br />

• Acceptance criteria established by Voith Hydro and Mani<strong>to</strong>ba<br />

Hydro for the new repairs<br />

• <strong>In</strong> process inspections using liquid dye penetrant<br />

• Linear indications subject <strong>to</strong> Magnetic Particle <strong>In</strong>spection<br />

• All inspections were witnessed by Mani<strong>to</strong>ba Hydro<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Technical Aspects of Repair<br />

• <strong>Blade</strong>s measure 46” inches long by 16” wide<br />

• Thickness approximately 0.75” inches at leading and trailing<br />

edges; 1.25” at middle sections<br />

• Average repaired area 160 square inches some exceeding 250<br />

square inches<br />

• <strong>Cavitation</strong> generally exceeded 0.300” deep<br />

• Some areas greater than 1.00” deep<br />

• <strong>Blade</strong>s mapped prior <strong>to</strong> repair (as found condition)<br />

• Mapped repairs (as left condition) and pho<strong>to</strong>graphed<br />

• <strong>Blade</strong> vent openings measured before and after welding<br />

• Band gap clearance and run out was measured<br />

• Unit 13 downstream runner repaired while replacement blades<br />

for the upstream runner were being cast<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Typical ‘as found’ condition<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Typical ‘as left’ condition<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Removal and <strong>Replacement</strong> of blades in situ<br />

• Upstream cavitation repair before replacement blades<br />

• During repairs it was decided that one of the three (3) blades<br />

identified for replacement was actually salvageable<br />

• Substantial time, discussion and engineering was expended<br />

prior <strong>to</strong> any site work in order <strong>to</strong> plan methods <strong>to</strong> remove,<br />

replace and inspect the blades<br />

• Peak Hydro determined the best solution was using butt weld<br />

preparations as opposed <strong>to</strong> the natural fillet conjunction of<br />

band, crown and the blades in the ‘as cast’ configuration<br />

• Post weld inspection (using ultra sound) of fillets would detect<br />

anomalies inherent <strong>to</strong> the casting<br />

• Butt joints are easier <strong>to</strong> prepare for weld processing and<br />

provide a ‘cleaner’ inspection zone<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Prior repair at <strong>Blade</strong>/Band fillet<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Gouging of fillet reveals voids<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Removal and <strong>Replacement</strong> of blades in situ<br />

• Repair and overlay was completed in four junction zones;<br />

suction and pressure sides of fillets at band and crown<br />

• A lifting plan was prepared (safe work plan)<br />

• Each section of blade being removed/replaced weighed<br />

approximately 200 Lbs.<br />

• Chain blocks and restraining/locating plinths were welded <strong>to</strong><br />

adjacent blades <strong>to</strong> ensure that when cut free the blade would<br />

not slip out of position<br />

• <strong>Blade</strong>s were plasma cut and lowered from the 6 O’clock<br />

position<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> prepared for removal<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> fillets repaired<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> Removal and replacement<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> is lowered from runner<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Old/New blades compare and trim<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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<strong>Blade</strong> removed<br />

Presentation name | place or presenter | YYYY-MM-DD<br />

36


Removal and <strong>Replacement</strong> of blades in situ<br />

• <strong>Blade</strong> stubs were prepared with a double V weld preparation<br />

geometry and inspected prior installation<br />

• The replacement blades were fitted in place and welded<br />

according <strong>to</strong> qualified sequence and weld procedures<br />

• Subjected <strong>to</strong> ultrasonic inspections by a third party inspection<br />

company<br />

• Three of four (3 of 4) welds passed 1 st inspection<br />

• One of four (1 of 4) required repair before being accepted <strong>to</strong><br />

ASME VIII standards on re-inspection<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Prepare stubs for replacement blade<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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New blade being installed<br />

Presentation name | place or presenter | YYYY-MM-DD<br />

39


Ultra Sonic <strong>In</strong>spection of replacement blades<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Repair Results and Conclusions<br />

• Welding repairs <strong>to</strong> both downstream and upstream runners<br />

have proven very successful res<strong>to</strong>ring structure integrity, blade<br />

thickness, profile and fairness<br />

• While still a blend of old and new repairs, the surface area of<br />

quality weld material has substantially increased particularly in<br />

areas prone <strong>to</strong> cavitation<br />

• All major structural defects have been repaired<br />

• All cavitation has been removed<br />

• The removal and replacement of blades worked according <strong>to</strong><br />

planned procedure without issues<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Repair Results and Conclusions<br />

• Vent openings measured between each blade set<br />

• Hydraulic Balance measured as percentage from nominal<br />

• ‘As Found’ measurements not considered reliable <strong>due</strong> <strong>to</strong> the<br />

poor condition of the blade surfaces<br />

• Averaged 0.85% for the downstream and -0.36% for the<br />

upstream<br />

• ‘As Left’ measurements reveal hydraulic balance has improved<br />

<strong>to</strong> 0.08% downstream and -0.05% upstream<br />

• The two blades replaced in situ were subjected <strong>to</strong> full NDT<br />

examination in addition <strong>to</strong> dimensional checks and found <strong>to</strong> be<br />

acceptable <strong>to</strong> ASME VIII standards<br />

• Runner integrity, hydraulic balance and fairness are all<br />

substantially improved<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Acknowledgements:<br />

The following persons all made major contributions <strong>to</strong> the<br />

success of the Pointe du Bois project:-<br />

Mani<strong>to</strong>ba Hydro:<br />

Messrs. Jules Gareau, Jeff Marshall,<br />

Dan Nahuliak, Rejan Sayak<br />

Voith Hydro Services: Messrs. Samuel Perry, Steven Potter<br />

Chris<strong>to</strong>pher Vaughan, Michael Norris<br />

Voith Hydro Canada: Messrs. Richard Deboo,<br />

Charles Gagnon, Mehrzad Shahouei<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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Thanks for your attention<br />

Voith Hydro Services<br />

<strong>In</strong> <strong>Situ</strong> <strong>Francis</strong> turbine <strong>Blade</strong> <strong>Replacement</strong> | NWHA Hood River| 2013-05-23<br />

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