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Oklahoma Gas & Electric Muskogee Generating Station Best ...

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<strong>Oklahoma</strong> <strong>Gas</strong> & <strong>Electric</strong><br />

<strong>Muskogee</strong> <strong>Generating</strong> <strong>Station</strong> – BART Determination<br />

May 28, 2008<br />

Table 3-2 continued<br />

Control Technology<br />

Controlled NOx<br />

Emission Rate<br />

(lb/mmBtu)<br />

In Service on<br />

Existing PC<br />

Boilers<br />

21<br />

In Service on<br />

Other<br />

Combustion<br />

Sources?<br />

Technically Feasible on<br />

<strong>Muskogee</strong> Units 4 & 5?<br />

Rotamix (SNCR) NA X Yes Rotamix control systems have been<br />

demonstrated on small coal-fired<br />

boilers. However, there are several<br />

currently unresolved technical<br />

difficulties associated with<br />

applying SNCR-type systems on a<br />

large subbituminous coal-fired<br />

boiler. Therefore, Rotamix is not<br />

considered an available retrofit<br />

control technology for <strong>Muskogee</strong><br />

Units 4 & 5.<br />

Pahlman Process NA X No Bench- and pilot-scale testing has<br />

been conducted on coal-fired<br />

boilers, however, there is limited<br />

data available assessing the<br />

technical feasibility of this system<br />

on large coal-fired boilers.<br />

Wet NOx Scrubbing NA X Yes The system has been used on<br />

refinery fluid catalytic cracking<br />

units and small coal-fired boilers,<br />

but has not been used on large<br />

coal-fired boilers. Wet NOx<br />

scrubbing systems are not<br />

commercially available or<br />

technically feasible for <strong>Muskogee</strong><br />

Units 4 & 5.

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