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settlement_of_shallow_foundations_on_granular_soils (Lutenegger ang DeGroot)

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Sutherland (1963) compared the results of this procedure with a number of reported case

histories in which the results of plate bearing tests were available and found that this procedure

provided an improvement over the original Terzaghi and Peck procedure, however, it still tended

to overestimate settlement since it appeared that the allowable bearing pressure was underestimated

by almost 40%.

5.2.6 AI pan (1964)

Another settlement method based primarily on the Terzaghi and Peck (1948) method was

presented by Alpan (1964). This method indirectly uses a corrected blowcount to evaluate a modulus

of sub grade reaction from a plate loading test.

The method assumes that the settlement response of a shallow footing resting on sands will

be linear in the range of allowable bearing pressures (i.e., qu 1 /2.5) and is given as:

s = S 0

[2B/(B+ I )] 2 mCw

[5.23]

where:

s =settlement (in inches)

S 0 =settlement of a 1 ff plate (in inches)

B =footing width (in ft.)

m = shape correction factor

Cw = water table correction factor

= 2.0 = 0.5 (D/B) ,; 2.0 for water located immediately

below the footing

[5.24]

The settlement of the 1 ff plate is given as:

S 0

= aqB

[5.25]

where:

q = footing stress (in tst)

0'. = a constant (dependent upon the corrected blowcount N,)

The blowcount value at the foundation level is first used to estimate the relative density of

the sand, Dn using the suggestions of Gibbs and Holtz (1957) which was put into a more convenient

form by Coffman (1960) as shown in Figure 5.5. The correction factor, a, is shown in graphical

form in Figure 5.6. Note that two charts are suggested by Alp an (1964); one for corrected blowcount

values between 5 and 50; and another for corrected blowcount values between 25 and 80.

65

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