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4.2 Inspection of the old pipeline<br />

and determination of its state<br />

As in any trenchless replacement operation,<br />

the pipeline to be replaced was subjected to a<br />

thorough examination.<br />

Even while the pits were being dug, the sections<br />

of pipeline which were cut out in the course of<br />

this were examined for their degree of fouling,<br />

the properties of their material and their residual<br />

load-bearing capacity. This latter one was<br />

particularly significant for the subsequent procedure.<br />

Whether the pipeline needed further<br />

strengthening before the replacement depended<br />

on it. The pipeline which had been cut open was<br />

also subjected to a visual inspection, the path<br />

followed by it was documented and the positions<br />

of valves and other installed items were<br />

established from drawings. All these had to be<br />

removed as otherwise there would have been an<br />

uncontrolled rise in the tractive force.<br />

4.3 Preparation of the old pipeline<br />

It was found that the load-bearing capacity<br />

was not in fact high enough for the intended<br />

replacement technique. It was very likely that<br />

the walls of the pipes would collapse as the<br />

pipeline was being pressed out and would<br />

therefore make continued pressing impossible.<br />

The installing company therefore decided to<br />

undertake retrospective strengthening.<br />

For this purpose, a DN 150 PVC pipe for connecting<br />

to sewers was slid concentrically into<br />

the old pipe on spacers. The annular gap around<br />

7 cm wide which was created in this way was<br />

then grouted with a special mortar. This mortar<br />

was notable for its good flowability, and its<br />

high capacity for swelling and resistance to<br />

compression. The curing time of the mortar was<br />

five days. The nominal size of the PVC pipe was<br />

firstly intended to produce as large an annular<br />

gap as possible and hence as large as possible<br />

a cross-section for the concrete. Secondly the<br />

140 mm diameter traction string had to fit into<br />

it.<br />

4.4 Installation of the machinery<br />

After the preparatory work on the old pipeline,<br />

the installation of the machinery could begin. A<br />

rail-type supporting structure on which the soil<br />

removal equipment would slide freely and the<br />

new pipes could be assembled was installed in<br />

the launch pit (Fig. 8).<br />

Fig. 8:<br />

The launch or assembly pit<br />

The traction machine and its front frame were<br />

lowered into the target pit. They were both<br />

braced against the shoring formed by the<br />

concrete thrust block already cast. The front<br />

frame served more than one purpose. Firstly the<br />

bursting mandrel for splitting open the old pipeline<br />

could be accommodated there and secondly<br />

the space was needed for pulling the new pipeline<br />

into the target pit. The traction string was<br />

slid into the old pipeline, i.e. into the PVC pipe.<br />

The press-pull head, followed by the system for<br />

Fig. 9:<br />

Assembly of the first pipe to the reamer<br />

DUCTILE IRON PIPE SYSTEMS 55

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