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System 112A - The Black Vault

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B E lle.#~ CmOUTlOI<br />

SECRET<br />

--------------------------------------------------~..<br />

1<br />

second runs; the other has completed five 160-second<br />

runs. Severe tube leakage occurred du.l'ing the testing<br />

of the second thrust chamber. This was due to an<br />

injector discrepancy. In accordance with these results,<br />

recommendations have been made to cut all<br />

new thrust chambers with throat plugs.<br />

A test program is being conducted to det\-l ­<br />

mine the effect of between-run servicing procedures<br />

on thrust chamber durability and the adequacy of performing<br />

such operations on the test stand or motor<br />

mount. <strong>The</strong> major items involved are the nushing<br />

of the regenerative coolant tubes and the application<br />

and baking of the ceramic thrust chamber linell. <strong>The</strong><br />

first chamber in this program had a life of eleven 160­<br />

second runs at 500 psig chamber pressure. <strong>The</strong><br />

chamber was removed from the test stand, waterflushed,<br />

dried, recoated with ceramlc,and baked in an<br />

oven prior to each run. For succeeding chambers<br />

this procedure will be varied and methylene cloride<br />

will be used as a flushing ageilt.<br />

As a result of the success of the Linde Flame<br />

Plating process on the 4000-lb drilled-aluminum<br />

thrust chamber, the pos81b1l1ty of plating the COnvergent<br />

and throat sections of the tubular thrust chamber<br />

is being investigated. It is believed that, if 0.003 in.<br />

of tungsten carbide could be applied in the throat area<br />

of the tube bundle, the thrust chamber durabUitywould<br />

be increased.<br />

b. Drilled-Aluminum Thrust Chambers<br />

Drawings were released to fabricate three<br />

drilled thrust chambers of 5052 aluminum alloy. <strong>The</strong>se<br />

will be used to evaluate chamber erosion of aluminum<br />

when copper and silicon are not present in the alloy,<br />

and when coatings such as Hardkote, tungstenca.rbide,<br />

and microme are appUed to chamber walls of this<br />

alloy.<br />

Activity on the drilled aluminum thrust<br />

chamber during this quarter was again largely confined<br />

to injector evaluation. This phase of the program is<br />

covered in section 2, d, of this report.<br />

Two thrust chambers with tungsten-carbidecoated<br />

chamber sections were fire-tested to compare<br />

the durab1l1ty of the coating utilizing chrome r.1ckel as<br />

a bi;tder with that employing a cobalt binder. <strong>The</strong><br />

thrust chamber with the chrome nickel binder exceeded<br />

engine qualification .. equirements by a considerable<br />

mugln. Testing on the chamber withthe cobalt binder<br />

was concluded after six 160-second runs when the regenerative<br />

coolant pasBages were exposed. However,<br />

this testing was not considered conclusive because the<br />

cobalt binder coating was accidentally scored during<br />

machining and failure occurred at this point. At<br />

least one additional chamber With each coating Will be<br />

fire-tested to confirm these results.<br />

c. Refractory Coatings<br />

A drilled aluminum chamber coated with<br />

Norton Company flame-sprayed zirCOnia (Rokide "Z")<br />

was evaluated by firing a coated chamber on a test<br />

stand. <strong>The</strong> coating was .moderately durable, but<br />

spilled neu the nozzle end of the chamber. A second<br />

chamber Is being coated; the coating thickness will be<br />

held to a maximum of 0.010 In. to reduce the spall1ng<br />

tendency.<br />

d. Fuel Injectors<br />

During this quarter, 29 injectorsfor the 75L*<br />

thrust chamber assemblies were tested and accepted.<br />

To date, 264 units of this configuration have passed<br />

preliminary acceptance tests. Nine lI,d.dit:t.onal1nj~ctOI'l'<br />

of the same configuration were ACcepted for<br />

future assembly of test engines.<br />

Other steel injector testsincluded the evaluation<br />

of the effects of redueing the fuel-dome-injeetor<br />

fuel valve seal area to accommodate the self-contained<br />

injector fuel valve. No performance or heat<br />

rejection differences were noted as a result of this<br />

change.<br />

Testing of injectors for use on drilledaluminum<br />

thrust chambers continued during thilf.<br />

quarter with durabllity tests on both "doublf!t" and<br />

standard stainless steel injectors. This program has<br />

been separated into two phases and may be classified<br />

as follows: .<br />

(1) To develop a coating for the aluminum<br />

chamber which wlll allow extended operation<br />

with standard production injector<br />

using inhibited acid.<br />

(2) To develop an injector which will be<br />

compatible with the present Aiumillte<br />

Hardkote thrust chamber, also using<br />

inhibited acid.<br />

Testing on the phase I program was continued<br />

With the evaluation of an additional tungstencarbide-coated<br />

chamber. T'nis chamber was the first<br />

tested using a chrome-nickel binder for the tungsten<br />

ca.rbide coating. <strong>The</strong> injector used was a standard 72­<br />

pair caunterbored injector. '<strong>The</strong> chamber was tested<br />

over a total duration of 3320 seconds at which time a<br />

gouge appeared in the chamber Wlfll and invalidated<br />

further testing. Operation af thilll unit included 17<br />

full-duration tests conducted at rated thrustconditions<br />

and ambient propellant temperatures. One hot test<br />

28<br />

SECRET<br />

.~ . . _---­

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