21.01.2015 Views

Implementation Strategy V4 - Unipart Logistics

Implementation Strategy V4 - Unipart Logistics

Implementation Strategy V4 - Unipart Logistics

SHOW MORE
SHOW LESS

Create successful ePaper yourself

Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.

Doncaster Production Business Unit – Bogie Overhaul<br />

Background<br />

In early September 2005 the Bogie Production Unit at Doncaster delivered its first Bogie 1 to<br />

GNER. In 2006, this figure rose to 263, nearly doubling in 2007 to 489.<br />

1 A ‘bogie’ is the name of the chassis unit<br />

which is positioned underneath a train carriage<br />

to support it. Typically a bogie consists of two<br />

axles to which wheels are fixed. The bogie is<br />

allowed to swivel underneath the train carriage<br />

to self align between the rail tracks when the<br />

carriage is in motion.<br />

Identify and understand the Need<br />

Owing to the increase in Customer demand in 2007, further expected increases in 2008 to 570,<br />

and customer requirements for a greater range of bogie types to be overhauled, significant focus<br />

was required.<br />

copyright UGC Limited 2008


Set Objectives<br />

Two main objectives were:<br />

• Increase capacity to meet customer demand<br />

• Maintain a high level of quality to continue to exceed customer expectations.<br />

Grasp the situation<br />

At this stage we wanted to establish the current state of the operations, regardless of the history<br />

or reasons.<br />

Frame Examine<br />

Shot Blast<br />

Strip Area<br />

Process Flow<br />

Bolster Area<br />

Paint<br />

Comm<br />

Cell<br />

Internal<br />

Assembly<br />

Because the process has been broken down into a ‘flow process’ (or Single Piece Flow), our<br />

bogie moves from one stage to the next in a sequence until it has been through all the stages and<br />

is complete. This has a number of benefits, but one of the problems is often how to make this<br />

whole process perform faster (increase our capacity). Think of the analogy of a group of walkers<br />

going on a hike, and for safety reasons they are all joined together by a rope. The speed of the<br />

group is set by the slowest person, and the same is the case for our process. If one of the stages<br />

goes too fast it will run out of parts, and will also produce faster than the next stage requires.<br />

Conversely, if a stage goes too slow, it will stop the next stage through lack of work and the<br />

preceding stage will have finished work with nowhere for the work to go.<br />

Process Mapping of<br />

operations to include all<br />

material and information<br />

flows.<br />

copyright UGC Limited 2008


Grasp the situation (cont’d)<br />

Based on customer demand and available time, Takt = 4hrs (240min)<br />

Having measured the process from end to end the average times for each of the processes were<br />

found to be[figures need adding in here]:<br />

Mins<br />

500<br />

450<br />

400<br />

350<br />

300<br />

250<br />

200<br />

150<br />

100<br />

50<br />

0<br />

Wash<br />

High Level Dismantle<br />

Low Level Dismantle<br />

1<br />

Shot Blast<br />

Paint<br />

2 3<br />

Frame Exam<br />

Baseline<br />

Bolster Assembly<br />

Assy 1<br />

Assy 2<br />

Faro Arm<br />

Press<br />

Final assy<br />

WSP<br />

Process Time<br />

Takt Rqd<br />

It was necessary to target the ‘bottleneck’ processes to achieve the Takt time and customer<br />

demand, These bottleneck processes restrict the flow of work through the overall process, and as<br />

a consequence set the limit on our overall process capacity, as you can only perform as fast as<br />

your slowest process.<br />

By focusing on our bottlenecks this ensured that:<br />

• we would deliver a direct benefit against the objective of improving capacity<br />

• we could focus our limited resources in specific areas to deliver greatest benefit<br />

• we could tackle areas where often inventory is built up prior to the process. Inventory<br />

hides other wastes.<br />

All issues, that were identified during this process, were collated on a fishbone diagram for later<br />

consideration<br />

4<br />

copyright UGC Limited 2008


Issues i<br />

Product<br />

Locate waste and identify solutions<br />

Behaviour<br />

Training<br />

MAN<br />

No problem<br />

solving<br />

activity<br />

Incorrect<br />

Operation<br />

Training<br />

delays/<br />

waiting<br />

Ergonomics<br />

of processes<br />

Line Balance<br />

Takt<br />

METHOD<br />

Planning<br />

Space<br />

Flow<br />

Layout<br />

Locate<br />

Tooling<br />

Fetch Tooling<br />

Disruption<br />

Process<br />

Constraints<br />

Bottleneck<br />

Visibility<br />

Times<br />

Variation<br />

Issues<br />

Load/ Unload<br />

cycle times<br />

Availability<br />

Tooling<br />

Incorrect<br />

tools used<br />

Missing<br />

Locate<br />

correct Parts<br />

fetch<br />

Parts<br />

Overprocess<br />

Cost of<br />

Consumables<br />

New v Refurb<br />

Paint<br />

Gloves<br />

MACHINE<br />

MAT'L<br />

Fishbone Diagram of Identified Issues in Bogie Overhaul<br />

Many of the issues affected all the areas within the Bogie Overhaul Area, so we had to identify<br />

which were the main areas to focus on with the limited resource available. Based on the Baseline<br />

graph (above) it was recognised there were 4 key areas to focus on to achieve the overall<br />

objective of capacity improvement:<br />

1. Shot Blast<br />

2. Frame Exam<br />

3. Bolster assembly<br />

4. Assembly stage 1<br />

copyright UGC Limited 2008


Implement Solutions<br />

1. Shot Blast<br />

Identified Areas for Improvement<br />

380<br />

240<br />

Current<br />

Target<br />

Non-value added activity<br />

• Poor layout<br />

• Inappropriate tooling<br />

• Poor ergonomics<br />

• Poor utilisation of shot<br />

blast facility<br />

• Fetching parts<br />

Shot<br />

Blast<br />

Airbag Jig<br />

Small Parts<br />

Before<br />

After<br />

Improved loading and material handling of parts<br />

copyright UGC Limited 2008


Implement Solutions (cont’d)<br />

2. Frame Exam<br />

Identified Areas for Improvement<br />

456<br />

240<br />

Current<br />

Target<br />

Non-value added activity<br />

• Poor layout<br />

• Inappropriate tooling<br />

• Excessive variation<br />

• Work imbalance<br />

• Fetching parts<br />

Frame<br />

Exam<br />

During the frame examine<br />

process each part needs to<br />

be assessed as OK,<br />

Repair, or Replace<br />

Stock maintained of<br />

repaired parts ready<br />

to replace those<br />

requiring repair<br />

Storage of change parts<br />

& sub assy<br />

Kanban Board<br />

Material storage &<br />

handling<br />

Workplace<br />

Organisation<br />

copyright UGC Limited 2008


Implement Solutions (cont’d)<br />

3. Bolster Assembly<br />

Identified Areas for Improvement<br />

458<br />

Current Non-value added activity<br />

• Poor layout<br />

• Inappropriate tooling<br />

• Poor process for airbags<br />

240<br />

Target<br />

• Hand painting<br />

• Fetching parts<br />

Bolster<br />

Assy<br />

Improve painting process<br />

Improved Refurbishment<br />

Process<br />

Improved Storage<br />

Improved airbag process and pipework processes by:<br />

• Laying out the Airbag process as a ‘U shaped cell’<br />

• Improving the painting process<br />

• Organising the workplace through 5S<br />

copyright UGC Limited 2008


Implement Solutions (cont’d)<br />

4. Assembly Stage 1<br />

Identified Areas for Improvement<br />

382<br />

240<br />

Current<br />

Target<br />

Non-value added activity<br />

• Poor layout<br />

• Inappropriate tooling<br />

• Overprocessing<br />

• Locating correct tools<br />

• Fetching parts<br />

Assy 1<br />

Old Elbow Fitting<br />

New Elbow Fitting<br />

Bought in new parts:<br />

• Cheaper (compared to labour saving)<br />

• Quicker to fit<br />

• Right first time improvement<br />

Shadow boards for tooling<br />

2 Bin Kanban<br />

system for<br />

consumables<br />

copyright UGC Limited 2008


Review Situation and Results<br />

500<br />

450<br />

2<br />

Baseline<br />

3<br />

400<br />

350<br />

1<br />

4<br />

300<br />

Mins<br />

250<br />

200<br />

150<br />

100<br />

50<br />

0<br />

Wash<br />

High Level Dismantle<br />

Low Level Dismantle<br />

Shot Blast<br />

Paint<br />

Frame Exam<br />

Bolster Assembly<br />

Assy 1<br />

Assy 2<br />

Faro Arm<br />

Press<br />

Final assy<br />

WSP<br />

Before<br />

After<br />

Takt Rqd<br />

Improvements made in each of the targeted areas:<br />

1.Shot Blast = 41%<br />

2.Frame Exam = 34%<br />

3.Bolster assembly = 36%<br />

4.Assembly stage 1 = 17%<br />

In addition to the overall process improvements there have been improvements in process<br />

capability as demonstrated by the Frame Examine process variation (below):<br />

Variation<br />

Variation<br />

Improved process stability in Frame Examine Process<br />

copyright UGC Limited 2008


Update Standard Work<br />

Standard Operating<br />

Procedures (SOPs)<br />

were written or updated<br />

to reflect changes in the<br />

process and use of new<br />

tooling and fixtures<br />

Standard Work Layouts were updated for all process stages to establish the ‘standard<br />

condition’, ensure through auditing that the process layout is sustained and also set a benchmark<br />

from which to improve further.<br />

Date<br />

Originator<br />

Area / Team<br />

Ref<br />

Operation<br />

Sequence<br />

27/06/2006<br />

R Woods<br />

From: Bogie High Level Dismantle<br />

To: Bogie Low Level Dismantle<br />

STANDARD PLANNING DOCUMENT<br />

STANDARD WORK LAYOUT<br />

Date: 27/06/2006<br />

Description:<br />

Date<br />

Originator<br />

Area / Team<br />

Ref<br />

Operation<br />

Sequence<br />

27/06/2006<br />

R Woods<br />

From: Bogie High Level Dismantle (27 to 56)<br />

To: Bogie Low Level Dismantle<br />

STANDARD PLANNING DOCUMENT<br />

STANDARD WORK LAYOUT<br />

Date: 27/06/2006<br />

Description:<br />

Work Bench<br />

Tool Cupboard<br />

16<br />

15<br />

SCW<br />

Work Bench<br />

Tool Cupboard<br />

SCW<br />

2<br />

8<br />

17<br />

19 18<br />

20<br />

3<br />

4<br />

25<br />

26<br />

1<br />

38<br />

SCW<br />

Trolley<br />

39 40<br />

41 42<br />

33 29<br />

24<br />

23<br />

9<br />

43<br />

27<br />

32<br />

28<br />

35 34<br />

Shadow Board /<br />

Work Bench<br />

10<br />

14<br />

Scrap<br />

37<br />

36<br />

30<br />

31<br />

5<br />

6<br />

7<br />

Lateral Control<br />

Rack<br />

Scrap<br />

11<br />

13<br />

21<br />

12<br />

22<br />

Quality Check Safey Precaution Std In Process Stock Qty of SIPS Takt Time Cycle Time<br />

Quality Check Safey Precaution Std In Process Stock Qty of SIPS Takt Time Cycle Time<br />

Date Date Date Review Date<br />

Name / Position Name / Position Name / Position Responsibility<br />

Before Improvement<br />

Name / Position<br />

Date Name / Position<br />

Date Name / Position<br />

Date Review Date<br />

After Improvement<br />

Responsibility<br />

copyright UGC Limited 2008


Audit<br />

Having achieved these results it was important to sustain this so that we could improve further.<br />

We did this in a number of ways:<br />

Target Boards – we recognised that the most important part of<br />

all the improvement work was to ensure that we now sustained<br />

it, for a number of reasons;<br />

• We can measure how well the process is being<br />

sustained<br />

• We can measure that we are continuing to gain the<br />

benefits of the improvement<br />

• We can identify further issues (waste) within the<br />

process as the next stage of improvement, and get<br />

better everyday.<br />

Workplace Audit<br />

This ensured we checked the right things and that critical elements of the process were<br />

maintained, for example:<br />

• Checking that all the tooling is present on the shadow board at the end of a shift<br />

• Checking that the Standard Layout is being maintained and any deviations are put on a<br />

3C document<br />

• Checking that the Comm Cell meetings are occurring and questions raised receive<br />

feedback<br />

• Checking whether the Line Manager has visited the area to ‘Go & See’ [Principle 9]<br />

The Communication Centre was set<br />

up to enable effective production<br />

planning processes to be established.<br />

This ensured that all issues affecting<br />

the Bogie Overhaul Facility were<br />

collated in one central location. This is<br />

where support departments<br />

(Maintenance, Quality, Engineering,<br />

Supply Chain) meet with Production<br />

and agree actions in support of the<br />

business objectives.<br />

copyright UGC Limited 2008


Benefits<br />

£100K Benefit<br />

• Increased capacity - 5 bogies week to 7 bogies per week<br />

• Reduced man hours required - 20%<br />

Acknowledgements<br />

A large number of individuals have been fundamental to implementing and continuing the<br />

sustainment of these improvements.<br />

The main team included:<br />

Tony Metcalfe<br />

Ray Herbert<br />

Melissa Freeman<br />

Dave Heaton<br />

Erica King<br />

Mark Hopcraft<br />

Dave Munro<br />

Colin Cunningham<br />

Neil Watson<br />

Robert Davies<br />

Daz Smith<br />

Chris Peach<br />

David Baines<br />

Mark Nogowczyk<br />

For more information, please contact<br />

Mark Nogowczyk<br />

email: mark.nogowczyk@unipartrail.com<br />

copyright UGC Limited 2008

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!