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7 27‐Jun‐11 KCC/N LD:<br />
42/2390 T<br />
28086 ANGL ECoR After passing DSPT (Danishpet) @ 19.20 hrs, LP reported DJ tripped Stesalit make RSI, 6 tell tale fuses melted and D9 diode punctured. RSI Firm‐Stesalit SR<br />
through QLM & QRSI‐1 acted. Found RSI‐1 block 6 tell/tale fuses<br />
melted, isolated RSI‐1, energized loco and asked R/E since gradient 1 in<br />
100 R.<br />
1 03/06/11 12737 22744 LGD SCR Smoke from Gear case‐4. Relief engine given. At ELS/LGD, checked and found TM4 pinion end bearing seized and<br />
deflector came out,. Bearing make NSK/Japan, DOC;16.07.05<br />
Traction Motor Material/Unavoidable. SCR<br />
2 6/4/2011 12625 22654 ED SR VCB tripped as SIV not picking up and internal fault lamp glowing.<br />
Relief engine given.<br />
At ELS/ED, found SIV W‐phase GDU card defective. Same replaced. SIV<br />
make AAL kit‐3.<br />
SIV<br />
Material/Unavoidable<br />
Advised to SR for<br />
necessary remedial<br />
action<br />
SCR<br />
3 14/06/11 12861 23638 ET WCR DJ tripped due to heavy air leakage from SMGR filter union pipe.<br />
Worked up to CLE (chintalapalli) with manual operation of GR. At CLE<br />
Relief engine given.<br />
At ELS/KZJ, checked and found SMGR ceramic air filter incoming pipe<br />
line nipple collar worn out and came out from union caused air<br />
leakage due to improper securing of ZSMGR pannel. Pipe line<br />
replaced.<br />
Pneumatic pipe line<br />
Defective Maintenance<br />
/ Avoidable.<br />
Advised to WCR for<br />
necessary remedial<br />
action<br />
SCR<br />
1 6/18/2011 N/ ASN<br />
27974/ 27958 /<br />
WAG7<br />
BNDM<br />
SER<br />
2 6/17/2011 BOBR/BTPC 27742+27301 KZJ SCR<br />
3 6/24/2011 12801 (PUI‐<br />
NDLS Exp)<br />
20626 / WAM4 TATA SER<br />
L/Loco 27974 tripped on 18th notch. On checking found while closing<br />
BLVMT, STC not pick up & DJ tripped,<br />
T/ loco 27301 tripped with jerk. Checked & found QRSI -<br />
1+2 and QOP 1+2 dropped. On further checking found J-2<br />
not in proper direction. So J/(1+2) manually operated few<br />
times & reset the relays first time. Tested individually from<br />
T/loco 27301, having the same problem. So loco marked<br />
TR. Ld: 60/148½=5235T<br />
Tripped with detonating sound & S/E from HT compt. CLI/ADTP<br />
attended, found ICDJ, GR was operated manually few times & found DJ<br />
closed. Started from spot at 7:07hr again experienced DJ tripped with<br />
detonating sound & S/E from CGR‐1. Ld: 8/16=360TDriver‐<br />
K.Raju/ CKP<br />
SIV was tripping with glowing of external fault LED and display of<br />
SER<br />
'Earth fault' as MVRH winding burnt & earth, IR value of all phases '0'<br />
AUX/E<br />
mega ohm. Sr. no.‐ M0712789, Make‐ BBL, Type‐ MZ20M438, Mfg. yr.‐<br />
MFG/TRADE<br />
12/2007, DOC‐ 23.05.08<br />
Checked at ELS/TATA found Loco-27742 SL-1 earth, and SL MATERIAL SER<br />
in Loco-27301 TM-1&2 isolated as their IP armature<br />
became earth. Loco has been directed to ELS/KZJ for<br />
further attention.<br />
ELS/TATA ‐ Checked and found tracking took place CGR top insulating<br />
plate fixation bolt with connecting short link of CGR‐3 to RGR. CGR 1,2<br />
and 3 checked and found normal.Smoke noticed on GR horizontal<br />
shaft and vertical shaft beval gear. GR contact No.10 and 12 end<br />
portion flashed. GR vertical insulator IR value '0' .<br />
Details of GR‐ Srl.No.‐IB 304864430, Make : ABB ‐ RH done by<br />
M/s.BTI in Dec‐2010. Commissioned in L/20626 during IOH<br />
Dt.21.03.11.<br />
GR/SMGR<br />
MFG/TRADE<br />
SER<br />
18617 (HWH‐<br />
4 6/24/2011 RNC Intercity<br />
Exp)<br />
20651 / WAM4 TATA SER<br />
5 6/26/2011 Tiger BCN/E 24044 / WAG5 JHS NCR<br />
Tripping through QOP‐2 & S/E from under gear. Suspected S/E from<br />
TM‐6. So HQOP‐2 & Block‐2 kept isolated & started the train. Again<br />
same trouble between ULB – BSBP & S/E from U/Gear. Used F/Ex’R. On<br />
arrival at KGP loco detached. Ld: 12/24=600T Driver‐P.K.Shetty<br />
/ TATA<br />
After passing N/S bet DTV‐JSG exp, DJ closed but after 2‐3min suddenly<br />
tripped with QLM alone dropped & TFP oil splashed.<br />
Checked at ELS/TATA & found TM‐6 armature badly burnt, Mica came<br />
out. After dismantling found armature power coil fully stripped<br />
condition. Initially armature coil bonded. Further coil burnt due to<br />
HQOP‐2 off.<br />
Details of TM : Stator No. 092‐3419, LR/TATA 30.09.10, Arm. No.<br />
5753, FRW/TATA ‐ 15.09.10, LOD‐01.11.10.<br />
QLM dropped & TFP oil splashed. Directed to ELS/JHS for further<br />
attention.<br />
JE/SDL checked at SDL & found three nos. power cable of TFP is<br />
1 6/3/2011 18508 22034 GZB NR<br />
LP informed that loco tripped between MDXR‐GGT, checked &<br />
burnt & its insulation also burnt. (TFP cable between TFP to RSI<br />
found in HT compartment heavy smoke & burning smell, used<br />
burst) As per LP, loco tripped with QOP‐2 dropping and smoke<br />
F/extinguisher and checked found power cable near TFP is burnt<br />
& flame in TFP compartment. hence loco marked TR & directed<br />
condition.<br />
to home shed.<br />
LP reported that in loco no. 27165 ICDJ. LI/RIG Shri S. Parida<br />
2 6/3/2011 N/KDLP 27232/27165 BNDM SER<br />
attended at RIG and found DJ closing slightly, UA deviating and<br />
Suspected DJ closing contact inside VCB chamber not<br />
ARNO attempting to start then DJ trips.HQCVAR kept on 'O' but<br />
maintaining. so loco marked TR. BNDM shed report : VCB<br />
trouble could not be rectified. VCB pressure found 5.7 Kg/cm2<br />
interupter burst, (Areva make) VCB changed.<br />
was reduced to 5.5 Kg/cm2 but eventhough trouble could not<br />
be rectified.<br />
TM<br />
TFP<br />
HT\LT cables<br />
Vacuum Circuit<br />
Breaker (VCB)<br />
MATERIAL<br />
MATERIAL<br />
Bad Maintanance<br />
Shed<br />
Bad Maintanance<br />
Shed<br />
SER<br />
SER<br />
SECR<br />
SECR