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15 21.06.11 11071 18B 21931 KYN CR<br />
16 21.06.11 12810 24B 22879 SRC SER<br />
DS tripped with converter faulty and train stopped at km 51/01. train F‐3 fuse blown off since GTO shorted. Original GTO received with SI<br />
engine of N‐NGSM(DSL) at KYN given as A/Eng<br />
unit of 1997 make.<br />
QOP‐1, QRSI‐1 and QLM dropped and smoke from HT compartment CTF‐1 contact flashed , its commom bus bar insulation burnt. TM‐1,2<br />
near RSI‐1. Train backed to GAO after isolating RSI‐1. Loco failed and and 3 IR value zero. Firm has been advised to attend the loco.<br />
another loco given<br />
Warranty failure<br />
17 24.06.11 12138 22701 BRC WR<br />
Train stopped after passing starter signal at Dongargaon & then backed<br />
to DGN main line. LP rep while approaching DGN H/signal QOP‐2 , QRSI‐Loco became normal after isolating TM‐6 & worked 5 TM upto IGP.<br />
2 dropped, tried by isolating TM‐4,5 & 6 one by one but not succeed. TM‐6 badly flashed and IR value found '0'. TM‐6 isolated and given fit<br />
HQOP‐2 kept OFF but smoke noticed from under truck. Same loco on 5 TM. Crew took more time to isolate def TM<br />
worked further on 5 TM.<br />
LP reported train stopped at km 785/7, FO702P1 auxilary convertor‐2<br />
18 27.06.11 N‐KNW 43=3831 31278 AQ CR<br />
isolated and also bogie‐1 isolated Due to rising gradient train stopped. In Traction converter no‐1 MPH incomming cable no. 1134 from SB<br />
Train backed to Wagholi on 3 TM and then failed. Section blocked for board(BUR O/P cable) parted from lug due to poor crimping by CLW.<br />
1'11".<br />
19 29.06.11<br />
Smoke noticed from under track w/o QOP target. Driver stopped the TM‐5 deflector came out. This is initial stage of TM bearing seizure<br />
N/BDI<br />
27685 LDH NR train to check loco and rfound burning smell near TM‐5. loco detached case. Pinion removed and loco will will be given fit on 5 TM for<br />
60=59.5=5325<br />
and placed in siding.<br />
H/Shed<br />
1 01.06.11 MTPS 27821+ 27819 BIA SECR Rear loco no 27821 suddenly tripped & not energised due to SIV not M/Staff Mr. S.C.Gorai + LI/UDL M.Roy reported SIV not pick up after<br />
pick up.<br />
pressing BLRDJ 30 Sec.M/staff & LI escorted the rear loco to clean the<br />
load by pressing BLRDJ. Again rear loco tripped & notch not<br />
progressing by manual control also. Banking loco attached on rear &<br />
clear the section SMGR type ‐ ABB<br />
2 02.06.11 2307 UP 22863 HWH ER Train stopped at Km 249/19 due to DJ trip. Message given “ DJ trip via<br />
DJ feed back failure.<br />
3 12.06.11 EC/ BAD 23754 GZB NR After passing CRJ Starter signal loco trip through QOA. On checking<br />
found S/E from MVRH.<br />
4 17.06.11 EC/TNEB 27372 NKJ WCR After passing 'N' sec between KQU‐BRPA while closing DJ loco tripped<br />
through QOA & QOA(P).<br />
5 19.06.11 12988 22071 GZB NR Loco trip through QOA (P) LP isolated HQOA but found all auxiliary not<br />
working. On checking found CCA was melting. LP isolated HOBA &<br />
worked the train up to SDAH.<br />
6 20.06.11 18616 DN 22271 SRC SER Train detained at KAN (8:32 – 9:09 hrs) due to pressure trouble.<br />
Arrived BWN by manual control.<br />
7 20.06.11 12340 DN 22752 MGS ECR After start RNG MVRH abnormal sound. Then HVRH Pos ‘0’ & arrived at<br />
UDL by 5 th notch. LI & M/staff checked & found MVRH impeller<br />
broken.<br />
8 24.06.11 6310 DN 22327 HWH ER Train stopped in bet TTN‐JSME due to BP pressure dropped. On<br />
checking found Both CP not working.<br />
1 1‐Jun‐11 2839 22368 SRC SER Train JEN through passed at 5.15 hrs and stopped at Km no 357/10 due<br />
to TLTE on run at 5.22 hrs. On checking found GR not progressing with<br />
LSB glowing. On checking LP found CTF‐3 automatically goes to braking<br />
condition even if MP on "0". So LP tied CTF‐3 on traction position and<br />
started the train at 5.45 hrs.<br />
2 1‐Jun‐11 E/MGPV‐37 27606 NKJ WCR LP informed at 6.00 hrs from JKPR that GR not progressing. On<br />
checking he found SMGR pressure showing 9.0 Kg/Cm2. Same was<br />
informed to TLC/KUR & suspecting trouble in SMGR reducing valve,<br />
message given to ELS/ANGL for supplying of the same. But due to<br />
unavailability of SMGR reducing Valve loco directed to ELS/VSKP after<br />
marking TR .<br />
On checking found at HWH shed MPCS (Steslite) unit defective,<br />
changed by firm<br />
LI Ram Babu gone to site reported that S/E from MVRH. Loco checked<br />
at ASN shed & found S/E from MVRH .Loco sent to base shed<br />
CLI/B.K.Saha Roy /BWN & JE/BWN Manas Chakraborty arrived at BRPA<br />
on checking found no fire extinguisher used, there was no roof<br />
leakage.HVSL1,HVSL2,HPH competely burnt condition, suspected sort<br />
circuit.Loco sent to base shed.<br />
On checking at NKG found RPQOA resistance burnt.CCA melted due to<br />
wire no.420 in bet SB‐1 (Cab1) panel to SB2 (Cab2) panel bonded.<br />
QOA permanent TFWA meggaring value of a 0 & a 1 bushing is<br />
showing<br />
JE/BWN Bhowmik checked the loco & found after cooler pipe crack.<br />
Air leakage from after cooler joint also. Same attended & given fit.<br />
BWN arrived at 9:35 hrs, Departure at 10:17 hrs =42”<br />
On checking at HWH shed found TM6 slight flash mark. Impeller of<br />
MVRH 4 nos of bolt open condition.<br />
Loco checked at ELS/ASN on 24.06.11 .On checking found no supply<br />
in cable no G‐100 at cab1 SB supply checked at BD found normal.<br />
Fresh cable lay out done from BD to SB‐1 & found both CP working<br />
normal. Conclusion‐ No continuity was in cable no G‐100 from BD to<br />
SB‐1<br />
ELS/SRC:Coupler cables (3 Sq cm) cab‐2 from MP to SB‐2,one cable cut<br />
and three cable insulation damaged due to severe sulphation.<br />
ELS/VSKP: SMGR reducing valve changed(Shavo make).Old valve was<br />
having over sized.<br />
SIV Material CR<br />
CTF Warranty failue (Firm) CR<br />
TM + Crew ( Shri<br />
S.P.Bhakare)<br />
Material<br />
CR<br />
HV cable Maint/Shop CR<br />
TM Bearing Material CR<br />
SIV<br />
MPCS<br />
Aux motor Elect<br />
Misc/loco<br />
Pn pipe line<br />
Aux motor Elect<br />
Cable<br />
Material failure<br />
Firm<br />
Material failure<br />
Bad maint/WCR<br />
Mal opration by Dr.<br />
Material failure<br />
Material failure<br />
Material failure/ POH<br />
KPA.<br />
HT/LT Cables Defective Material ECoR<br />
SMGR Defective Material ECoR<br />
ER<br />
ER<br />
ER<br />
ER<br />
ER<br />
ER<br />
ER<br />
ER