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22 6/22/2011 N/BTMT 24552/24551 BIA<br />
BIA shed report: BA voltage in 24552, 24 V and hence both<br />
While starting LP exp DJ closing but STC not picking up. LP tried loco DJ not closing from 24552. But from loco no 24551 DJ<br />
SECR to rectify by keeping HBA off, but trouble not rectified.R/loco closing but not closing in 24552. Loco BA discharge in yard.<br />
demanded. So loco marked TR.<br />
Battery charger working checked found normal. Battery Make‐<br />
EXIDE<br />
M/staff attended but could not rectify and advised LP that loco<br />
23 6/22/2011 N/KRPH 27055 MGS ECR<br />
O/G‐ LP reported that while taken over charge of LE. poor brake has to go to pit to attend, brake power adjusted in pit and<br />
power.<br />
given fit. LP reported TLC at 23.30 hrs that no information by<br />
I/C LP.<br />
24 6/27/2011 12860 22504 SRC SER<br />
LP informed that QOP‐II permanently dropped so block‐II AT Igatpuri M/staff found J‐2 drum contact badly flashed.and<br />
isolated and worked the train up to DGG. At DGG another loco TM‐4,5 & 6 badly flashed.SRC shed report: TM‐4 & TM‐5<br />
27934(VSKP) attached on top.<br />
commutator brush box flashed so Both TMs changed.<br />
25 6/30/2011 12860 22586 SRC SER<br />
1 11/6/2011 12253 22372 HWH ER<br />
1 04.06.11 12833<br />
AD‐HWH<br />
2 14.06.11 2962<br />
IND‐BCT<br />
3 15.06.11 12953<br />
BCT‐NZM<br />
LP reported that TLTE between JMG‐KRL, checked Q‐51, Q‐52,<br />
GR pressure found normal then try with EEC but unsuccess.<br />
CLI/ RIG‐ N Sahoo cleaned the Q‐52 relay and gently tapped<br />
and try to take 4‐5 notches found no trouble but R/loco already<br />
attached in front so as per advice of Sr. DEE (OP) allowed that<br />
24414/BZA ( 80 kmph ) + wkg loco in dead. SRC Shed report: Q‐<br />
52 defective. same changed.<br />
Battery<br />
Bogie & its Mech.<br />
Equipments<br />
Traction Motor<br />
Relay<br />
Mal Operation by<br />
crew<br />
Bad Maintanance<br />
Shed<br />
Bad Maintanance<br />
Shed<br />
Bad Maintanance<br />
Shed<br />
Suddenly pressure dropped at YPR station due to FP pipe already Suddenly pressure dropped at YPR station due to FP pipe already<br />
SWR<br />
broken and damaged due to CRO in BZA division, found BP also cracked broken and damaged due to CRO in BZA division, found BP also Pn. Pipeline<br />
Misc<br />
from neck portion.<br />
cracked from neck portion.<br />
22601 SRC SER LP INFORMED DJ OPEN ON STANDING W/O TARGET , CHECKED FOUND MICROPROCESSOR PT WAS OPEN CIRCUITED RESULTING INTO MICROPROCESSOR SRC/SER WR<br />
SMOKE NEAR BV BOX. FRESH LOCO PROVIDED.<br />
QCVAR NOT ENERGISING & R118 OVER HEATED. LOCO SENT DEAD TO<br />
HOME SHED.<br />
22542 BRC WR AFTER PASSING SBPJ DJ TRIPPED, CHECKED FOUND X'MER OIL SPREAD SECTION CLEAR AND FRESH LOCO PROVIDED. X'MER BRC<br />
WR<br />
OUT AND OIL LEVEL MINIMUM.<br />
SHED<br />
30025 GZB NR TRAIN STOPPED AS TWO FAULT EXPEERIENCE BY LOCO PILOT F0201P1 IN RTM SHED FOUND TM 1 JAMMED.HENCE STARS (GEAR) TM END &<br />
i.e. DISTURBANCE IN CONVERTOR NO.1 AND F0201P2 i.e.EARTH FAULT GEAR CASE UNCOUPLED & SR‐1 ISOLATED BY GZB STAFF. LOCO SENT<br />
IN CONVERTOR NO.1 . AND SMOKE NOTICED FROM TM‐1.<br />
LELA WITH SR. 90 KMPH TO HOME SHED.<br />
THREE PHASE<br />
GZB<br />
NR<br />
SECR<br />
SECR<br />
SECR<br />
SECR<br />
WR<br />
4 29.06.11 GM/KWI<br />
43/3960<br />
2 03.06.11 23024+24459<br />
BL/WR(DEAD)<br />
23089 TKD WCR TRAIN STOPPED AT KM 286/20 DUE TO DJ TRIP BY QSIT WHILE BLDJ<br />
PRESSED WITH MESSAGE "INVERTER FAULTY". HBA KEPT OFF, HSIV<br />
KEPT ON "0" BUT NOT SUCCEEDED. FRESH LOCO 24528 PROVIDED.<br />
SI‐AAL, MICROPROCESSOR‐STESALIT.<br />
ET WCR LOCO WAS ORDERED EX ELS/ET. AFTER EOL LP NOT START &<br />
REPORTED QRSI‐2 DROPPING ON 4tH NOTCH HENCE LINE CLEAR<br />
CANCELLED. ELS STAFF REACHED ON LOCO & GIVEN READY AFTER<br />
INCREASING SETTING OF QRSI & TRAIN LEFT EX ET YARD. LP AGAIN<br />
REPORTED EX ET THAT QRSI‐2 DROPPING ON 800 AMP. LATER TRAIN<br />
PASSED BNI VIA LOOP LINE WITH BANKER LOCO 23817/NR BUT<br />
STOPPED NEAR ADVANCE STARTER DUE TO QRSI‐2 DROPPING HENE<br />
TRAIN BACK TO BNI LOOP LINE DUE TO GRADIENT AHEAD & LOCO<br />
FAILED & SENT TO T/S ET.<br />
AT BRC SHED JOINTLY CHECKED WITH AAL REPRESENTATIVE AND<br />
FOUND "IGDU‐VFD" RECORDED IN FAULT MEMORY OF SIV. ON<br />
FURTHER CHECKING FOUND V‐PHASE LEFT SIDE IGBT SHORT<br />
CIRCUITED. LOCO UNDER OBSERVATION AFTER IGBT CARD<br />
REPLACEMENT.<br />
SI UNIT<br />
LOCO JOINTLY CHECKED BY SLI & JE & REPORTED 01 CT (CURRENT<br />
TFP) USING AS RSI‐LM TWO CT, ONE USED IN THIS LOCO WHICH IS<br />
PARALLEL CONNECTED (ONE CT IN RSI‐2 BLOCK & ONE ADDITIONAL<br />
CT USE IN BA‐3 PANEL BETWEEN WIRE NO. A‐274 & A‐275 CAUSING<br />
QRSI‐2 DROPPING ON 800 AMPS.<br />
RESPONSIBILITY BAD WORKMANSHIP OF ELS/ET DURING<br />
UNSCHEDULE REPAIR & WRONG CONNECTION MADE TWO CT OF RSI‐<br />
2. ELS/ET REPORT‐ LOCO CHECKED AT T/S ET & FOUND QRSI‐2<br />
DROPPING ON 3rd NOTCH AT 700 AMPS CURRENT. QRSI‐2 RELAY COIL<br />
WIRE NO. A/274 & A/275 SHOWING SHORTED, EVEN AFTER BOTH<br />
SIDE CONNECTION WAS REMOVED. FURTHER DURING CHECKING<br />
FOUND 02 NOS CT IS EXISTING IN RSI‐2, WHILE IN BA‐2 & 3 02 NOS RSI<br />
CT WAS ALSO EXISTING, WHICH RESULTED TOTAL CURRENT IN QRSI<br />
RELAY INCREASED. RSI WAS LAST CHANGED ON 02.06.11.<br />
RSI MAINT WCR<br />
TKD<br />
WCR<br />
WR