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17 29‐Jun‐11 17481 27936 WAT ECoR At 23.40 hrs LP informed to CC/VSKP that Cab‐2 heavy air leaking from<br />
BP angle cock vent hole after EOT. C&W staffs attended but not<br />
succeed. Li PMV Diwaker attended with mechanics but not rectified.<br />
Advised to arrange relief power. At 00.15hrs L/27936(WAT) detached<br />
from train and L/21240(AJJ) given bar line and EOT done at 00.30 hrs<br />
and BP ready and departure at 00.40 hrs.<br />
STEAM SHED: Loco was checked found exhaust port leakage from<br />
cab‐2 BP angle cock. BP angle cock was changed.Defective angle cock<br />
was opened and found its valve seat (Gasket) was damaged<br />
condition. Due to damage of the valve seat, BP angle cock EP leakage<br />
was expd during open condition.On 28/06/11 external pressure<br />
checking was done. During testing (cab2) efficiency test was done<br />
from rear cab‐1.External pressure testing was done by Sri Ganga Rao,<br />
Gr.I, T.No.269.<br />
Pneumatic Valves Bad Mant.(Shed) ECoR<br />
1 05.06.11 BSCS 31283 BIA SECR Train controlled at CDMR.On starting, BP dropped. LP reported that<br />
MCB 100 tripped and CP not working. LP reset MCB 100 but CP not<br />
working. Then put electronics off & on and found normal. Gave ready<br />
at 04:50. Train left at 05:10. Train arrived in SEB loop at 08:50. LP<br />
reported MCB 100 tripped again & again and Battery charger not<br />
working. Loco failed at 09:15.<br />
2 05.06.11 12301 30282 GZB NR Train passed CDMR at 00:33. Loco tripped at 00:39 and not resumed.<br />
Message displayed‐SS01 0109 P1 Main power assistant winding over<br />
current. As per DDS BUR max.current 039/012. Train arrived GAQ at<br />
00:45 in coasting. LP put electronics off & on and found loco normal.<br />
ELS/GMO checked ‐ MCB 100 tripped & BA charger not working. BUR2<br />
BUR3 ‐ WRE module interchanged then loco became OK.<br />
Train left at 00:51. At MGS LI V.B.Pathak checked and found<br />
normal.Loco made over to NCR working the same train.<br />
3 Ph FR Case ECR<br />
3 Ph FR Case ECR<br />
3 05.06.11 GHTL 28062 SIV‐<br />
Hirect MPCS‐<br />
Steslite<br />
ASN ER Train stopped bet RFJ‐DEO RD due to loco tripped and message givenfault<br />
in diagonestic control system. LP tried but loco not<br />
closed.L/31254 arrived site & onload in front at 05:00, pressure ready<br />
at 05:15 and train left at 05:20. .<br />
4 09.06.11 53612 22804 MGS ECR Trainarrived KCKI and SIV autometically off & LSCHBA glowing. Internal<br />
fault lamp glowing also. LP tried to rectifie but not success. So, loco<br />
failed.<br />
5 15.06.11 03127/spl 27522<br />
STC‐AAL<br />
6 17.06.11 PNP 27505<br />
SIV‐Siemens<br />
MGS ECR Train stopped between PKA‐DHN due to DJ tripped via QSIT and QSIT<br />
became permanent. LP put HBA OFF & ON & isolated block‐1 then left<br />
site at 19:09. Train arrived DHN at 20:00 with same trouble occurred<br />
again & again. Another loco 24017 O/L in front of dead loco‐27522 at<br />
20:20, P/R at 20:30, left DHN at 20:54.<br />
CNB NCR Train arrived GAYA without pre‐information about defects that BA<br />
charger not working.LP reported that DJ tripped & QSIT dropped and<br />
external fault lamp glowing. So loco made dead by LP and wait for<br />
some times then tried to energise but not success. Another loco 27242<br />
O/L train left 8:10 with dead loco 27505.<br />
ELS/MGS checked ‐ Battery no. 8 showing reverse polarity. Same<br />
battery changed then OK.<br />
ELS/GMO checked‐ SIV blower over heated and not working as its<br />
delevary hole chocked. Firm (Simens) staff attended and given fit.<br />
ELS/MGS checked ‐ MVSL1 bonded & open circuited. MVSL1 changed.<br />
(Make‐HBB, R/W on 10.08.06 at KPA, DO O/H‐ 26.11.09, DOF‐<br />
04.01.10)<br />
ELS / MGS checked in put insulator terminal flashed and cut & other<br />
same wire also cut Loco directed to base shed due to firm staff has<br />
not agree to attended at MGS asout of warranty Make siemence.<br />
Battery FR Case ECR<br />
SIV Material Failure ECR<br />
Aux. Mach Elect Material Failure ECR<br />
SIV FR Case ECR<br />
7 18.06.11 12024 22311 HWH ER Train arrived JAJ LP reported that flashing from BA charger but BA<br />
voltage showing 100 V.Loco checked by LI & M/Staff TFP cable which<br />
come in BA charger flashed and cable open out and CHBA not<br />
working.Another loco 24408/BL O/L in front of dead loco P/R left<br />
15:20<br />
8 18.06.11 NE 27993 SIV ‐<br />
HIRECT<br />
9 19.06.11 PKW (Sangam) 28284 SIV‐<br />
Hirect)<br />
CNB NCR Train stopped between JPL‐HDN due to DJ tripped via QSIT . LP made<br />
loco dead & put HBA OFF & ON then DJ closed and left site but again<br />
stopped between KVQ‐MDJ due to QSIT dropped & DJ tripped ,<br />
message given rectifier over temp and internal fault lamp glowing.Asstt<br />
loco 27034 arrived & O/L in rear of MT & left site by pushing at 0:15,<br />
arrived MDJ at 0:45. Then 27034 detached from rear & O/L in front of<br />
dead loco left 1:45.<br />
MGS ECR Train stopped in main line PRY at 14:08 due to loco tripped on<br />
coasting. On checking found QOP‐2 & QE dropped with smoke from<br />
SIV. Loco failed at 14:30. Multi loco 28284 + 24019 onload at 18:30,<br />
pressure ready at 18:45 and train left PRY at 19:10.<br />
Loco Jointly checked at ASN shed by CLI/UDL & JE/ASN<br />
BA charger 2 nos tap lead of charger tranformer was cut from<br />
lug.same attended.<br />
AS per CT LC/MGS loco will go to bash shed as dead SIV deft. Make<br />
HIRECT<br />
CHBA FR Case ECR<br />
SIV FR Case ECR<br />
ELS/MGS checked cotactor C‐145 Arc‐ chute burnt and C‐145 flashed.C‐ Contactor Material Failure ECR<br />
145 & its Arc‐chute changed. Make‐ CLW commissioning 04.02.11