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E&R - eLocoS

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17 29‐Jun‐11 17481 27936 WAT ECoR At 23.40 hrs LP informed to CC/VSKP that Cab‐2 heavy air leaking from<br />

BP angle cock vent hole after EOT. C&W staffs attended but not<br />

succeed. Li PMV Diwaker attended with mechanics but not rectified.<br />

Advised to arrange relief power. At 00.15hrs L/27936(WAT) detached<br />

from train and L/21240(AJJ) given bar line and EOT done at 00.30 hrs<br />

and BP ready and departure at 00.40 hrs.<br />

STEAM SHED: Loco was checked found exhaust port leakage from<br />

cab‐2 BP angle cock. BP angle cock was changed.Defective angle cock<br />

was opened and found its valve seat (Gasket) was damaged<br />

condition. Due to damage of the valve seat, BP angle cock EP leakage<br />

was expd during open condition.On 28/06/11 external pressure<br />

checking was done. During testing (cab2) efficiency test was done<br />

from rear cab‐1.External pressure testing was done by Sri Ganga Rao,<br />

Gr.I, T.No.269.<br />

Pneumatic Valves Bad Mant.(Shed) ECoR<br />

1 05.06.11 BSCS 31283 BIA SECR Train controlled at CDMR.On starting, BP dropped. LP reported that<br />

MCB 100 tripped and CP not working. LP reset MCB 100 but CP not<br />

working. Then put electronics off & on and found normal. Gave ready<br />

at 04:50. Train left at 05:10. Train arrived in SEB loop at 08:50. LP<br />

reported MCB 100 tripped again & again and Battery charger not<br />

working. Loco failed at 09:15.<br />

2 05.06.11 12301 30282 GZB NR Train passed CDMR at 00:33. Loco tripped at 00:39 and not resumed.<br />

Message displayed‐SS01 0109 P1 Main power assistant winding over<br />

current. As per DDS BUR max.current 039/012. Train arrived GAQ at<br />

00:45 in coasting. LP put electronics off & on and found loco normal.<br />

ELS/GMO checked ‐ MCB 100 tripped & BA charger not working. BUR2<br />

BUR3 ‐ WRE module interchanged then loco became OK.<br />

Train left at 00:51. At MGS LI V.B.Pathak checked and found<br />

normal.Loco made over to NCR working the same train.<br />

3 Ph FR Case ECR<br />

3 Ph FR Case ECR<br />

3 05.06.11 GHTL 28062 SIV‐<br />

Hirect MPCS‐<br />

Steslite<br />

ASN ER Train stopped bet RFJ‐DEO RD due to loco tripped and message givenfault<br />

in diagonestic control system. LP tried but loco not<br />

closed.L/31254 arrived site & onload in front at 05:00, pressure ready<br />

at 05:15 and train left at 05:20. .<br />

4 09.06.11 53612 22804 MGS ECR Trainarrived KCKI and SIV autometically off & LSCHBA glowing. Internal<br />

fault lamp glowing also. LP tried to rectifie but not success. So, loco<br />

failed.<br />

5 15.06.11 03127/spl 27522<br />

STC‐AAL<br />

6 17.06.11 PNP 27505<br />

SIV‐Siemens<br />

MGS ECR Train stopped between PKA‐DHN due to DJ tripped via QSIT and QSIT<br />

became permanent. LP put HBA OFF & ON & isolated block‐1 then left<br />

site at 19:09. Train arrived DHN at 20:00 with same trouble occurred<br />

again & again. Another loco 24017 O/L in front of dead loco‐27522 at<br />

20:20, P/R at 20:30, left DHN at 20:54.<br />

CNB NCR Train arrived GAYA without pre‐information about defects that BA<br />

charger not working.LP reported that DJ tripped & QSIT dropped and<br />

external fault lamp glowing. So loco made dead by LP and wait for<br />

some times then tried to energise but not success. Another loco 27242<br />

O/L train left 8:10 with dead loco 27505.<br />

ELS/MGS checked ‐ Battery no. 8 showing reverse polarity. Same<br />

battery changed then OK.<br />

ELS/GMO checked‐ SIV blower over heated and not working as its<br />

delevary hole chocked. Firm (Simens) staff attended and given fit.<br />

ELS/MGS checked ‐ MVSL1 bonded & open circuited. MVSL1 changed.<br />

(Make‐HBB, R/W on 10.08.06 at KPA, DO O/H‐ 26.11.09, DOF‐<br />

04.01.10)<br />

ELS / MGS checked in put insulator terminal flashed and cut & other<br />

same wire also cut Loco directed to base shed due to firm staff has<br />

not agree to attended at MGS asout of warranty Make siemence.<br />

Battery FR Case ECR<br />

SIV Material Failure ECR<br />

Aux. Mach Elect Material Failure ECR<br />

SIV FR Case ECR<br />

7 18.06.11 12024 22311 HWH ER Train arrived JAJ LP reported that flashing from BA charger but BA<br />

voltage showing 100 V.Loco checked by LI & M/Staff TFP cable which<br />

come in BA charger flashed and cable open out and CHBA not<br />

working.Another loco 24408/BL O/L in front of dead loco P/R left<br />

15:20<br />

8 18.06.11 NE 27993 SIV ‐<br />

HIRECT<br />

9 19.06.11 PKW (Sangam) 28284 SIV‐<br />

Hirect)<br />

CNB NCR Train stopped between JPL‐HDN due to DJ tripped via QSIT . LP made<br />

loco dead & put HBA OFF & ON then DJ closed and left site but again<br />

stopped between KVQ‐MDJ due to QSIT dropped & DJ tripped ,<br />

message given rectifier over temp and internal fault lamp glowing.Asstt<br />

loco 27034 arrived & O/L in rear of MT & left site by pushing at 0:15,<br />

arrived MDJ at 0:45. Then 27034 detached from rear & O/L in front of<br />

dead loco left 1:45.<br />

MGS ECR Train stopped in main line PRY at 14:08 due to loco tripped on<br />

coasting. On checking found QOP‐2 & QE dropped with smoke from<br />

SIV. Loco failed at 14:30. Multi loco 28284 + 24019 onload at 18:30,<br />

pressure ready at 18:45 and train left PRY at 19:10.<br />

Loco Jointly checked at ASN shed by CLI/UDL & JE/ASN<br />

BA charger 2 nos tap lead of charger tranformer was cut from<br />

lug.same attended.<br />

AS per CT LC/MGS loco will go to bash shed as dead SIV deft. Make<br />

HIRECT<br />

CHBA FR Case ECR<br />

SIV FR Case ECR<br />

ELS/MGS checked cotactor C‐145 Arc‐ chute burnt and C‐145 flashed.C‐ Contactor Material Failure ECR<br />

145 & its Arc‐chute changed. Make‐ CLW commissioning 04.02.11

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