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NAVY ENGINEERING BULLETIN AUGUST 2002<br />
45<br />
then to ensure reasonable motoring<br />
capability during its operation in the<br />
event of an emergency shutdown, the<br />
need for sustaining HP air was<br />
uncompromising.A fall back option<br />
was then to cross-connect the<br />
electric diving air Baueras to the HP<br />
air wingman, however this was shortlived<br />
as in order to maintain diving<br />
air quality the operation of the<br />
Bauers mandated the use of the<br />
associated Securus moisture and<br />
contaminant filters. The performance<br />
of these filters under continuous use<br />
was below that expected and hence<br />
the change out rate was such that<br />
after only 72 hours, the full<br />
complement of Securus filters was<br />
consumed. HP air availability was<br />
now mission critical as GT mode<br />
relied upon it. To exacerbate matters<br />
our remaining diesel engine mode<br />
(starboard ECO) was also faltering as<br />
it has since leaving Australia owing to<br />
unreliable power transmission<br />
through a fluid coupling which was<br />
slipping. Command’s propulsion<br />
flexibility was now well under threat<br />
as reliable diesel propulsion and GT<br />
sprint availability could not be<br />
guaranteed. Throughout all of this,<br />
ANZAC still represented as the only<br />
viable interception vessel in the NAG<br />
at a time of heightened oil smuggling<br />
activity out of Iraq.<br />
With little options remaining, the<br />
emergency diesel Bauer had to be<br />
connected in some way to the HP air<br />
system. Although not normally used<br />
with the ship’s fixed HP system but<br />
with a little ingenuity it was crossconnected<br />
to the breathing air<br />
system via the re-compression<br />
connection in the forward part of the<br />
hanger. Running the diesel Bauer in<br />
the hanger however posed some very<br />
real safety concerns particularly<br />
noting the intense aviation activity<br />
during the deployment. A makeshift<br />
exhaust trunk was established taking<br />
the diesel fumes from the Bauer to<br />
the flight-deck, but noting the<br />
distance and the slow exhaust flow, a<br />
DC ram fan was needed to assist in<br />
the extraction. All was set to ensure<br />
that at the very least GT mode could<br />
now be relied upon with the<br />
availability of a continuous HP air<br />
supply. However noting the lowpressure<br />
discharge of the diesel<br />
Bauer, it required to be run<br />
continuously to ensure the<br />
appropriate HP air in the GT air start<br />
bottles.This led to further needs such<br />
as watchkeepers (on a department<br />
already heavily burdened with<br />
contributions to boarding parties,<br />
security teams, steaming parties and<br />
not to mention continuous corrective<br />
maintenance on other systems) and<br />
vigilant monitoring and correction of<br />
the HP air system to ensure there<br />
was no loss to system leaks.<br />
The final blow came when the ram<br />
fan used for extraction seized. With<br />
only four carried on board, of which<br />
one was already unserviceable,<br />
another was required for heat<br />
extraction from the crane HPU<br />
compartment (another mission<br />
critical equipment for RHIB<br />
operations) and now a third having<br />
seized, the sole remaining ram fan<br />
was brought into use. With the port<br />
diesel engine down, the starboard<br />
diesel engine performance made<br />
unreliable because of a slipping fluid<br />
coupling and GT mode reliant on<br />
reduced HP air availability,<br />
Command’s propulsion flexibility and<br />
redundancy was severely degraded<br />
and down to effective dependence<br />
on a single DC ram fan.<br />
The situation was bleak. However the<br />
engineering resilience and<br />
determination to ensure HP air<br />
production, coupled with the<br />
continual ‘handraulic’ intervention in<br />
operating the starboard fluid<br />
coupling, meant that the ship could<br />
remain on station for a further three<br />
days until relieved by a US destroyer<br />
and hence completing the required<br />
patrol period. Meanwhile, the strip<br />
down of the HPAC and the insulation<br />
and cladding on the port diesel<br />
engine progressed in readiness for<br />
the imminent and much needed<br />
rectification period alongside Bahrain<br />
prior to a return to patrol.<br />
Good Dit But So What!<br />
The above is not recited to showcase<br />
our particular tenacity in ANZAC, for it<br />
is certain that similar stories can be<br />
told across the fleet in all ships. I tell<br />
it here as a poignant illustration of<br />
how the need to bear engineering<br />
skill, determination, persistence,<br />
flexibility, adaptability and solutions is<br />
very real at sea today as it has<br />
always been. The implicit<br />
understanding by engineers of the<br />
Command requirements and to<br />
focus engineering effort accordingly,<br />
and conversely the tactical<br />
adjustments by warfare officers to<br />
compensate for technical limitations,<br />
is what made ANZAC able to fulfil its<br />
obligation and maintain true to its<br />
mission. The fear is not in our will to<br />
do so, although much could be said<br />
about the feelings of some whom<br />
question that will, but in our<br />
remaining ability to carry out such<br />
actions and hence to meet our<br />
combat readiness even in the face of<br />
such adversity. Despite the smart<br />
technology, the embedded design<br />
redundancy and the sophistication of<br />
the ANZAC propulsion control<br />
system, the example demonstrates<br />
that total reliability will always<br />
depend on applied engineering and<br />
technical leadership at sea, to