24.01.2015 Views

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

SHOW MORE
SHOW LESS
  • No tags were found...

You also want an ePaper? Increase the reach of your titles

YUMPU automatically turns print PDFs into web optimized ePapers that Google loves.

ASPHALT INSPECTORS DAILY REPORT<br />

Lot No. 156 Date 07/23/1996 Project No.59-0055-03-070-10 County Grenada and Yalobusha<br />

Contractor Lehman-Roberts Producer of <strong>Mix</strong> Lehman-Roberts <strong>Mix</strong> Design Lab No. 9638314<br />

Type Plant Batch-Drum Binder MODIFIER ULTRAPAVE Source of AC ERGON<br />

(Outside Lane)<br />

EXTRATIONS (MT-30) SAMPLE NUMBER 1 2<br />

Time 8:02 Time 8:02<br />

Temperature 171 C Temperature 163 C 163 C<br />

Sample Wt. (W) 2056 Air Wt. 1186.6 1195.4<br />

Weight of Moist (M) 0.8 Water Wt. 682.4 686.5<br />

Dry Sample Wt. (Ws) 2055.2 Characteristics SSD Wt. 1188 1196.5<br />

Corr. AC % 5.09 (104.6) of Laboratory Volume 505.6 510<br />

Total Ext. Wt. (W1) 1950.6 Compacted Sp. Grav. 2.347 2.344<br />

Job Sieve Weight % Dev. Spec. Specimens Voids 2.8 2.9<br />

<strong>Mix</strong> Size Grams Passing Tol. (MT-34&MT-35) VMA 14<br />

1 1/2" 6 Dial 254<br />

100 1" 0 100 0 6 Stability 3375<br />

99 3/4" 22.2 98.9 0.1 6 Flow 18<br />

83 1/2" 364.6 81.3 1.7 6 <strong>Asphalt</strong> Content Guage (MT-6) 5.13<br />

68 3/8" 635.7 67.4 0.6 6 Moisture Sample Wt. 500.9<br />

42 #4 1134.7 41.8 0.2 5 Correction Wt. Water 0.2<br />

28 #8 1380.7 29.2 1.2 5 (AASHTO: T110) % Moisture 0.04<br />

#16 5 Corrected <strong>Asphalt</strong> Content 5.09<br />

16 #30 1603.4 17.8 1.8 4 Sample Wt. 1813.1<br />

7 #50 1791.3 8.2 1.2 4 Maximum Cal. Wt. 7514.4<br />

3.9 #200 1863.7 4.5 0.6 1.5 Specific Gravity Final Wt. 8576.5<br />

TEST STRIP OR ROADWAY DENSITY (TMD-22-06-00-000) (AASHTO: T209) Volume 751<br />

Sublot No. 1 2 3 4 5 Max. Sp.Grav. 2.414<br />

Station 792+44 799+45 807+03 812+46 820+40<br />

Location 2.1 m 0.6 m 1.8 m 0.6 m 0.9 m Crush Count 94.2%<br />

Thickness 38 mm 44 mm 38 mm 41 mm 41 mm Limestone Retained on #4 Sieve %<br />

Air Wt. 629.9 704 627.8 694.5 692.4 Agg. Bulk Sp. Grav. 2.59<br />

Water Wt. 361.4 397.7 356.7 387.2 395.5 Job <strong>Mix</strong> AC% 4.8<br />

CORE SSD Wt. 630.4 705.2 628.8 696.4 693.7 VMA = 14.7 Minimum = 13<br />

DENSITY Volume 269 307.5 272.1 309.2 298.2<br />

Sp. Gravity 2.342 2.289 2.307 2.246 2.322 Average<br />

Max. Sp. Gravity 2.414 Density<br />

% Density 97 94.8 95.6 93 96.2 95.3<br />

97

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!