24.01.2015 Views

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

SHOW MORE
SHOW LESS
  • No tags were found...

You also want an ePaper? Increase the reach of your titles

YUMPU automatically turns print PDFs into web optimized ePapers that Google loves.

ASPHALT INSPECTORS DAILY REPORT<br />

Lot No. 169 Date 07/30/1996 Project No.59-0055-03-070-10 County Grenada and Yalobusha<br />

Contractor Lehman-Roberts Producer of <strong>Mix</strong> Lehman-Roberts <strong>Mix</strong> Design Lab No. 9639914<br />

Type Plant Batch-Drum Binder MODIFIER SEAL-O-FLEX Source of AC ERGON<br />

(Outside Lane)<br />

EXTRATIONS (MT-30) SAMPLE NUMBER 1 2<br />

Time 7:45 Time 7:45<br />

Temperature 160 C Temperature 160 C<br />

Sample Wt. (W) 1842.2 Air Wt. 1191.7<br />

Weight of Moist (M) 0.6 Water Wt. 682.4<br />

Dry Sample Wt. (Ws) 1841.6 Characteristics SSD Wt. 1193.5<br />

Corr. AC % 4.77 (87.8) of Laboratory Volume 511.1<br />

Total Ext. Wt. (W1) 1753.8 Compacted Sp. Grav. 2.332<br />

Job Sieve Weight % Dev. Spec. Specimens Voids 3.4<br />

<strong>Mix</strong> Size Grams Passing Tol. (MT-34&MT-35) VMA 14.3<br />

1 1/2" 6 Dial 306<br />

100 1" 0 100 0 6 Stability 4071<br />

99 3/4" 0 100 1 6 Flow 20<br />

83 1/2" 339 80.7 2.3 6 <strong>Asphalt</strong> Content Guage (MT-6) 4.83<br />

68 3/8" 567 67.7 0.3 6 Moisture Sample Wt. 502.9<br />

42 #4 1031.1 41.2 0.8 5 Correction Wt. Water 0.3<br />

28 #8 1262.5 28 0 5 (AASHTO: T110) % Moisture 0.06<br />

#16 5 Corrected <strong>Asphalt</strong> Content 4.77<br />

16 #30 1457.3 16.9 0.9 4 Sample Wt. 1827.2<br />

7 #50 1611 8.1 1.1 4 Maximum Cal. Wt. 7514.4<br />

3.9 #200 1674.3 4.5 0.6 1.5 Specific Gravity Final Wt. 8584.9<br />

TEST STRIP OR ROADWAY DENSITY (TMD-22-06-00-000) (AASHTO: T209) Volume 756.7<br />

Sublot No. 1 2 3 4 5 Max. Sp.Grav. 2.415<br />

Station<br />

Location Crush Count %<br />

Thickness 38 mm 44 mm 38 mm 44 mm 41 mm Limestone Retained on #4 Sieve %<br />

Air Wt. 584.7 693.3 563.2 703.8 657.3 Agg. Bulk Sp. Grav. 2.59<br />

Water Wt. 320.8 387.7 305.4 394.3 364.7 Job <strong>Mix</strong> AC% 4.8<br />

CORE SSD Wt. 587.2 696 565.3 705.8 659 VMA = 14.7 Minimum = 13<br />

DENSITY Volume 266.4 308.3 258.9 311.5 294.3<br />

Sp. Gravity 2.195 2.249 2.175 2.259 2.233 Average<br />

Max. Sp. Gravity 2.415 Density<br />

% Density 90.9 93.1 90.1 93.5 92.5 92<br />

104

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!