24.01.2015 Views

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

SHOW MORE
SHOW LESS
  • No tags were found...

You also want an ePaper? Increase the reach of your titles

YUMPU automatically turns print PDFs into web optimized ePapers that Google loves.

ASPHALT INSPECTORS DAILY REPORT<br />

Lot No. 173 Date 08/01/1996 Project No.59-0055-03-070-10 County Grenada and Yalobusha<br />

Contractor Lehman-Roberts Producer of <strong>Mix</strong> Lehman-Roberts <strong>Mix</strong> Design Lab No. 9639914<br />

Type Plant Batch-Drum Surface MODIFIER SEAL-O-FLEX Source of AC ERGON<br />

(Inside Lane)<br />

EXTRATIONS (MT-30) SAMPLE NUMBER 1 2<br />

Time 3:45 Time 3:45<br />

Temperature 182 C Temperature 163 C<br />

Sample Wt. (W) 1614.1 Air Wt. 1209.3<br />

Weight of Moist (M) 0.6 Water Wt. 676.1<br />

Dry Sample Wt. (Ws) 1603.5 Characteristics SSD Wt. 1210.8<br />

Corr. AC % 5.21 (84.1) of Laboratory Volume 534.7<br />

Total Ext. Wt. (W1) 1529.4 Compacted Sp. Grav. 2.262<br />

Job Sieve Weight % Dev. Spec. Specimens Voids 4.6<br />

<strong>Mix</strong> Size Grams Passing Tol. (MT-34&MT-35) VMA 15.8<br />

1 1/2" 6 Dial 343<br />

1" 6 Stability 4361<br />

100 3/4" 0 100 0 6 Flow 20<br />

97 1/2" 83.2 94.6 2.4 6 <strong>Asphalt</strong> Content Guage (MT-6) 5.25<br />

87 3/8" 215.2 85.9 1.1 6 Moisture Sample Wt. 500.8<br />

55 #4 715.4 53.2 1.8 5 Correction Wt. Water 0.2<br />

37 #8 972.8 36.4 0.6 5 (AASHTO: T110) % Moisture 0.04<br />

#16 5 Corrected <strong>Asphalt</strong> Content 5.21<br />

20 #30 1223.6 20 0 4 Sample Wt. 2013.1<br />

11 #50 1381.2 9.7 1.3 4 Maximum Cal. Wt. 7514<br />

5.4 #200 1454.5 4.9 0.5 1.5 Specific Gravity Final Wt. 8678.3<br />

TEST STRIP OR ROADWAY DENSITY (TMD-22-06-00-000) (AASHTO: T209) Volume 848.9<br />

Sublot No. 1 2 3 4 5 Max. Sp.Grav. 2.371<br />

Station 55+86 66+66 69+46 80+40 81+30<br />

Location 3 m 3 m 1.8 m 1.2 m 2.4 m Crush Count %<br />

Thickness 38 mm 38 mm 32 mm 38 mm 32 mm Limestone Retained on #4 Sieve %<br />

Air Wt. 582.5 538.9 470.2 594.7 458.4 Agg. Bulk Sp. Grav. 2.545<br />

Water Wt. 324.9 300.5 262.2 332.1 252.8 Job <strong>Mix</strong> AC% 5.2<br />

CORE SSD Wt. 586.6 543.7 474.5 599.3 463.2 VMA = 15 Minimum = 14<br />

DENSITY Volume 261.7 243.2 212.3 267.2 210.4<br />

Sp. Gravity 2.226 2.216 2.215 2.226 2.179 Average<br />

Max. Sp. Gravity 2.371 Density<br />

% Density 93.9 93.5 93.4 93.9 91.9 93.3<br />

106

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!