24.01.2015 Views

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

State Study 111 - Polymer Modified Hot Mix Asphalt Field Trial.pdf

SHOW MORE
SHOW LESS
  • No tags were found...

You also want an ePaper? Increase the reach of your titles

YUMPU automatically turns print PDFs into web optimized ePapers that Google loves.

ASPHALT INSPECTORS DAILY REPORT<br />

Lot No. 127 Date 07/09/1996 Project No. 59-0055-03-070-10 County Grenada and Yalobusha<br />

Contractor Lehman-Roberts Producer of <strong>Mix</strong> Lehman-Roberts <strong>Mix</strong> Design Lab No. 9638310<br />

Type Plant Batch-Drum Binder MODIFIER KRATON Source of AC ERGON<br />

(Outside Lane)<br />

EXTRATIONS (MT-30) SAMPLE NUMBER 1<br />

Time 9:30 Time 9:30<br />

Temperature 174 C Temperature 163 C<br />

Sample Wt. (W) 1896.5 Air Wt. 1190.8<br />

Weight of Moist (M) 0.8 Water Wt. 682.8<br />

Dry Sample Wt. (Ws) 1895.7 Characteristics SSD Wt. 1192.1<br />

Corr. AC % 4.68 of Laboratory Volume 509.3<br />

Total Ext. Wt. (W1) 1807 Compacted Sp. Grav. 2.338<br />

Job Sieve Weight % Dev. Spec. Specimens Voids 3.4<br />

<strong>Mix</strong> Size Grams Passing Tol. (MT-34&MT-35) VMA 14<br />

1 1/2" 6 Dial 262<br />

100 1" 0 100 0 6 Stability 3486<br />

99 3/4" 18.6 98.9 0.1 6 Flow 16<br />

79 1/2" 263.9 85.4 6.4 6 <strong>Asphalt</strong> Content Guage (MT-6) 4.72<br />

65 3/8" 590 67.3 2.3 6 Moisture Sample Wt. 501.8<br />

42 #4 1062.9 41.2 0.8 5 Correction Wt. Water 0.2<br />

28 #8 1289.1 28.7 0.7 5 (AASHTO: T110) % Moisture 0.04<br />

#16 5 Corrected <strong>Asphalt</strong> Content 4.68<br />

16 #30 1509 16.5 0.5 4 Sample Wt. 1896.2<br />

7 #50 1670.3 7.6 0.6 4 Maximum Cal. Wt. 7514<br />

3.9 #200 1731.6 4.2 0.3 1.5 Specific Gravity Final Wt. 8627.1<br />

TEST STRIP OR ROADWAY DENSITY (TMD-22-06-00-000) (AASHTO: T209) Volume 783.1<br />

Sublot No. 1 2 3 4 5 Max. Sp.Grav. 2.421<br />

Station 577+35 583+74 590+30 593+01 600+33<br />

Location 0.61 m 0.61 m 3 m 2.4 m 2.4 m Crush Count %<br />

Thickness 51 mm 38 mm 38 mm 41 mm 41 mm Limestone Retained on #4 Sieve %<br />

Air Wt. 843.8 620.6 563.8 540.6 636.7 Agg. Bulk Sp. Grav. 2.59<br />

Water Wt. 474.5 356 321.7 311.4 363.2 Job <strong>Mix</strong> AC% 4.8<br />

CORE SSD Wt. 845.4 621.5 565.7 541.9 638.7 VMA = 14.7 Minimum = 13<br />

DENSITY Volume 370.9 365.5 244 230.5 275.5<br />

Sp. Gravity 2.275 2.337 2.311 2.345 2.311 Average<br />

Max. Sp. Gravity 2.421 Density<br />

% Density 94 96.5 95.5 96.9 95.5 95.7<br />

80

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!