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VOL 71 No4 - Navy League of Australia

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ENGINES<br />

The airship was powered by two Wolseley engines, each <strong>of</strong> which<br />

developed 180 horse-power. They were eight cylinder, water cooled<br />

vertical engines designed to deliver maximum power at 1 ,000 rpm. As<br />

originally designed the forward engine drove two propellers through<br />

bevel gearing at 500 rpm. In an attempt to lighten and re-balance the<br />

ship in August 1911, the two gondolas' positions were exchanged.<br />

'AVIONICS'<br />

The 'wireless telegraphy' installation was specially prepared for R1<br />

after a number <strong>of</strong> experiments. It was powered by an alternator driven<br />

by the after engine delivering three kilowatts, 350 cycles, 200 volts<br />

and was expected to have a range <strong>of</strong> about 600 nautical miles. The<br />

transmitter spark was 'quenched' to reduce the risk <strong>of</strong> igniting hydrogen<br />

and light metal screens surrounded the equipment to eliminate the<br />

risk completely. The receiver was a modified Marconi with a 'pericon'<br />

detector using a 1 ,000 ft five-stranded copper wire aerial suspended<br />

below the ship in flight.<br />

FIRST 'FLOAT'<br />

At last, on Monday 22 May 1911 inflation was complete and the airship<br />

was lowered onto the water in its shed ready for basin trials. Boats<br />

were secured either side <strong>of</strong> the gondolas and padding was fixed to<br />

the shed doors which were only inches wider than the airship itself.<br />

An elaborate plan had been prepared for extracting it and she was<br />

walked aft by 300 sailors and marines pulling on ropes carefully until<br />

the nose was clear and then towed to the centre <strong>of</strong> Cavendish Dock<br />

where she was attached to a mooring pontoon secured there. At first a<br />

wind baffle was attached to the mast but this caused the airship to yaw<br />

violently and so it was removed, curing the problem. The nose mooring<br />

arrangement, subsequently used by all airships, proved successful.<br />

Designed to withstand a 'pull ' <strong>of</strong> up to four tons, the recorded 'pull ' in a<br />

17 knot breeze was only 5301bs. While she rode out at the mast, a crew<br />

<strong>of</strong> nine remained on board and carried out a range <strong>of</strong> acceptance trials<br />

although engine runs were cut short by problems with the radiators.<br />

On 23 May she rode out a gale <strong>of</strong> wind estimated at up to 45 knots<br />

successfully and searchlights were played on the ship from HERMIONE<br />

during the two nights she was out to make sure that all was well with<br />

her. She floated but was too heavy to lift and, because the gas bags<br />

leaked at the rate <strong>of</strong> about 1% per day, replacement hydrogen had to<br />

be brought out to her in cylinders carried in a naval cutter. Getting<br />

her back into the shed on 25 May turned out to be more difficult than<br />

extracting her because <strong>of</strong> a slight cross-wind. The whole evolution took<br />

1 00 minutes and resulted in one side being rubbed against the door <strong>of</strong><br />

the shed and two sailors falling into the dock. She looked beautiful with<br />

her silver grey and yellow hull and had cost £41 ,000 to date. Despite<br />

her nickname, R1 was hailed as a success by the press.<br />

Back in the shed, the airship 'floated ' at a height <strong>of</strong> three feet without<br />

crew, tools, wireless set, hawsers, petrol or ballast Captain Sueter had<br />

refused to accept her and drastic alterations had to be undertaken if<br />

she was to fly. The ship was slung from the ro<strong>of</strong> once more and the<br />

outer skin was peeled <strong>of</strong>f and the gas bags deflated and removed. Then<br />

the water-trimming device was taken out together with the keel , cabin<br />

and any equipment intended for non-flying use. The heavier gondola<br />

was moved from aft to forward and the control car was lightened and<br />

moved aft. By July R1 was still unable to lift itself and the Advisory<br />

Committee for Aeronautics was asked for advice. They recommended<br />

the insertion <strong>of</strong> an extra bay with 40 ,000 cubic feet <strong>of</strong> gas, a solution<br />

that was to be applied to R1 01 by a later generation to cure a similar<br />

problem. The Admiralty declined such a drastic solution immediately<br />

because the shed would have to be rebuilt to take the lengthened ship<br />

and it was hoped that the weight reduction programme would at least<br />

allow a limited trials programme before the end <strong>of</strong> 1911 . After three<br />

years work, the <strong>Navy</strong> wanted results.<br />

Another inflation and weighing on 17 August showed that she was still<br />

too heavy and a further 1, 1951bs <strong>of</strong> equipment was removed after she<br />

was again deflated. The forward propeller was reduced to 1 0 feet so<br />

that it could be driven directly from the engine without a gearbox and<br />

holes were drilled in the engine control levers to lighten them . Tool<br />

boxes were replaced by fabric bags and the crew made and installed<br />

a canvas water-ballast trimming system. On 22 September 1911 she<br />

was inflated for what proved to be the last time, using 1, 762 cylinders <strong>of</strong><br />

The stern lifted as it was blown away from the dock wall.

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