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Philippines<br />

Antonio Bravo<br />

This report outlines the field testing of the<br />

Waterloo handpump in the Philippines from<br />

January 1980 to May 1982.<br />

The project sought to attain the following<br />

four objectives: (1) to field test the Waterloo<br />

handpump in the rural areas; (2) to evaluate<br />

the technical viability of the handpump by<br />

assessing its operational performance in terms<br />

of volumetric efficiency, mechanical efficiency,<br />

and ease of usage; (3) to determine problems<br />

related to the operation and use of the pump<br />

and provide solutions for the improvement<br />

in design and reliability of the pump; and<br />

(4) to assess prospects for eventual adoption<br />

of the Waterloo pump in the national program<br />

of handpump development.<br />

In accordance with specifications provided<br />

by the International Development Research<br />

Centre (IDRC), prototypes of the Waterloo<br />

handpump were fabricated and installed in<br />

specific areas in the Philippines. Thirty<br />

handpumps were installed in Laguna, Cavite,<br />

Pangasinan, and Nueva Ecija. The sites<br />

chosen were typical rural communities where<br />

water supply is a problem and where a<br />

minimum of 10-20 users reside.<br />

Periodic visits were made to the pump sites<br />

to monitor the performance of the pumps.<br />

Employing a monitoring format agreed upon<br />

by the representatives of the countries<br />

involved in the network project during a<br />

meeting held in Malaysia in the latter part<br />

of 1980, various parameters were observed<br />

and measured.<br />

Pump Design and Construction<br />

Below-ground components<br />

The project team used a 3-inch (7.5-cm)<br />

diameter polyvinyl chloride (PVC) pipe for<br />

the well casing, which also functions as the<br />

pump cylinder. Pipes, 10 feet (3 m) long,<br />

were joined using PVC solvent cernent and<br />

PVC couplings. The nominal pipe dimensions<br />

were 88.7 mm OD x 79.26 mm ID. The piston<br />

was machined from solid PVC stock. Two<br />

polyethylene rings each with a diameter of<br />

3 inches (76.5 mm) and a thickness of 5116<br />

inch (7.93 mm) were used. The first (upper)<br />

piston ring was 5/9 inch (14.2 mm) wide<br />

whereas the lower one was 0.25 inch<br />

(6.35 mm). Eight 0.25-inch (6.35-mm) holes<br />

were drilled in the piston (Fig. lA).<br />

The project team decided to use an irrecoverable<br />

foot valve. Both piston and foot<br />

valve were basically similar except that the<br />

foot valve had larger holes than the piston<br />

(0.5 inch; 12.7 mm) (Fig. 1B). The foot valve<br />

was redesigned therefore, and, instead of two<br />

polyethylene rings, a rubber gasket (ID 2.34<br />

inch and OD 3.5 inch; 59.5 and 88.9 mm)<br />

was used.<br />

The foot valve was further modified by<br />

incorporating a brass spring. The valve seat<br />

was also chamfered to prevent sand particles<br />

from wedging between the flapper valve and<br />

the base (Fig. 2).<br />

PVC pipes (OD 1.06 inch and ID 0.81 inch;<br />

26.8 and 20.5 mm) were used as piston rods.<br />

These were 10 feet (3 m) long and were<br />

joined using PVC couplings and PVC solvent<br />

cement. A PVC screen filter (about 10 feet,<br />

3 m, long) was incorporated in several pumps<br />

during installation. This PVC screen and<br />

sandtrap was improvised by cutting slots<br />

diagonally along a section of PVC pipe with<br />

a hacksaw. These slots were 0.25 inch (6 mm)<br />

apart and 1 inch (2.5 cm) long across the<br />

pipe. The end of the filter was cut and bent to<br />

give it a conical shape.<br />

Above-ground components<br />

The above-ground components consisted<br />

of a wooden handle assembly, metal yoke, a<br />

concrete pedestal, and a concrete platform<br />

reinforced by 0.5-inch (1.25-cm) steel reinforcement<br />

bars. The wooden handle was<br />

originally connected to the piston rod by a<br />

metal flange. This flange was connected by<br />

a bolt to a steel block into which a brass<br />

fitting connected to the piston rod was<br />

screwed. A problem in the design of this<br />

linkage caused the piston rod to buckle during<br />

operation. This was remedied by using a solid<br />

iron rod for the upper portion of the piston<br />

rod (Fig. 3). The pedestal for the pump was<br />

33

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