TEXT FPO - Driving Sports TV
TEXT FPO - Driving Sports TV
TEXT FPO - Driving Sports TV
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First, we had a whole set of gauges from autoM-<br />
eter. They had sent us their nexus gauges, which are<br />
fully electronic, color shifting and really cool. We had<br />
made some gauge pods for it, but had not wired or<br />
installed them. The reason for this was that we were<br />
planning on also installing an aeM standalone system.<br />
however, with little time remaining, we decided<br />
to leave this and install it later. We did not want to install<br />
the gauges twice since wiring in the aeM would<br />
mean rewiring the gauges, so the gauges sat in their<br />
pods dormant. In the meantime, a Perfect Power 6<br />
would have to do for engine management.<br />
at this time we also installed seats from a 2005<br />
2.5Rs. We also installed a leather shift boot and new<br />
shift knob. What we were lacking was a paint job, and<br />
with only a week to go, I decided I would spray the<br />
car in my garage.<br />
The less that is said about this paint job, the better.<br />
but to illustrate just how wrong things had gone,<br />
it was now 40 degrees Fahrenheit in my garage, I had<br />
never painted a car before, and I had never mixed<br />
paint. It did not go well. between all the runs, orange<br />
peel and other flaws, the car looked bad to say the<br />
least. but it had to get to seMa. so with the paint this<br />
side of dry, I hopped in and drove to Fleet signs and<br />
Graphics, so that they could install 48 hours worth of<br />
stickers in just under 12. We added a few touches to<br />
the stickers along the way to try to hide the hideous<br />
paint job. This did not work out so well.<br />
In the end, the truck driver loading the car onto<br />
his truck would prevent the car going to seMa 2006<br />
when he rammed the front lip into a winch on his<br />
truck. This was a blessing in disguise, as the car clearly<br />
was not ready for the show.<br />
however, the story does not end here. Just after<br />
38 July 2008<br />
The knocking that we heard turned<br />
out to be a broken cam-cap bolt.<br />
seMa 2006 was the first running of subiefest, where<br />
the car sat on display in all its home-painted and<br />
broken nose glory. While the plan was to run the car<br />
around the track, there were a few problems with this.<br />
First was the fact that the monster 18-inch Konigs<br />
wrapped in 235-wide nitto race rubber was in no<br />
way going to fit under the slab-sided fenders. two, a<br />
freak crash closed the track before the car could turn<br />
a wheel. This was also a blessing in disguise, at least<br />
for the ill-fated Legacy, as on the way home from the<br />
track the car started making an ominous knocking<br />
sound. normally when something like this happens,<br />
you pull over, shut down and call aaa. however, I was<br />
at least 100 miles from home, and it was night with no<br />
aaa, so I had to press on. early the following Monday<br />
I drove the car back to Rallitek for a diagnosis. sure<br />
enough, the car was knocking; no, they could not pinpoint<br />
it; yes, the motor would have to come out.<br />
With a heavy heart I drove the car, gingerly,<br />
up to the barn/shop of Mazdasport editor Jeff<br />
Zurschmeide, where I would pull the motor to send it<br />
back to Crawford for analysis. This I did with a severe<br />
sinus infection, not fun when trying to work on a car.<br />
still, I made it through with a mix of advil and cold<br />
beer at the end of the day. a cold beer makes a great<br />
ice pack when you are trying to relieve the pressure<br />
on your head; plus, it has the added effect of getting<br />
you good and drunk so that you can pass out. O.K.,<br />
it isn’t the healthiest way of beating the flu, but it<br />
worked.<br />
With the motor out and the engine back at Crawford,<br />
there wasn’t much I could do, and the car sat<br />
while other projects got priority and the engine was<br />
torn down, inspected and rebuilt.<br />
The knocking that we heard turned out to be a<br />
broken cam-cap bolt. apparently these can break<br />
from time to time, and we just happened to have one<br />
of those engines. Further digging found that a tuning<br />
issue we had been having had washed the cylinders<br />
with fuel and the rings had scuffed the bores; not<br />
good. Further more, the oil pickup tube had a hole<br />
in it and was not getting sufficient oil to the bearings