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TEXT FPO - Driving Sports TV

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First, we had a whole set of gauges from autoM-<br />

eter. They had sent us their nexus gauges, which are<br />

fully electronic, color shifting and really cool. We had<br />

made some gauge pods for it, but had not wired or<br />

installed them. The reason for this was that we were<br />

planning on also installing an aeM standalone system.<br />

however, with little time remaining, we decided<br />

to leave this and install it later. We did not want to install<br />

the gauges twice since wiring in the aeM would<br />

mean rewiring the gauges, so the gauges sat in their<br />

pods dormant. In the meantime, a Perfect Power 6<br />

would have to do for engine management.<br />

at this time we also installed seats from a 2005<br />

2.5Rs. We also installed a leather shift boot and new<br />

shift knob. What we were lacking was a paint job, and<br />

with only a week to go, I decided I would spray the<br />

car in my garage.<br />

The less that is said about this paint job, the better.<br />

but to illustrate just how wrong things had gone,<br />

it was now 40 degrees Fahrenheit in my garage, I had<br />

never painted a car before, and I had never mixed<br />

paint. It did not go well. between all the runs, orange<br />

peel and other flaws, the car looked bad to say the<br />

least. but it had to get to seMa. so with the paint this<br />

side of dry, I hopped in and drove to Fleet signs and<br />

Graphics, so that they could install 48 hours worth of<br />

stickers in just under 12. We added a few touches to<br />

the stickers along the way to try to hide the hideous<br />

paint job. This did not work out so well.<br />

In the end, the truck driver loading the car onto<br />

his truck would prevent the car going to seMa 2006<br />

when he rammed the front lip into a winch on his<br />

truck. This was a blessing in disguise, as the car clearly<br />

was not ready for the show.<br />

however, the story does not end here. Just after<br />

38 July 2008<br />

The knocking that we heard turned<br />

out to be a broken cam-cap bolt.<br />

seMa 2006 was the first running of subiefest, where<br />

the car sat on display in all its home-painted and<br />

broken nose glory. While the plan was to run the car<br />

around the track, there were a few problems with this.<br />

First was the fact that the monster 18-inch Konigs<br />

wrapped in 235-wide nitto race rubber was in no<br />

way going to fit under the slab-sided fenders. two, a<br />

freak crash closed the track before the car could turn<br />

a wheel. This was also a blessing in disguise, at least<br />

for the ill-fated Legacy, as on the way home from the<br />

track the car started making an ominous knocking<br />

sound. normally when something like this happens,<br />

you pull over, shut down and call aaa. however, I was<br />

at least 100 miles from home, and it was night with no<br />

aaa, so I had to press on. early the following Monday<br />

I drove the car back to Rallitek for a diagnosis. sure<br />

enough, the car was knocking; no, they could not pinpoint<br />

it; yes, the motor would have to come out.<br />

With a heavy heart I drove the car, gingerly,<br />

up to the barn/shop of Mazdasport editor Jeff<br />

Zurschmeide, where I would pull the motor to send it<br />

back to Crawford for analysis. This I did with a severe<br />

sinus infection, not fun when trying to work on a car.<br />

still, I made it through with a mix of advil and cold<br />

beer at the end of the day. a cold beer makes a great<br />

ice pack when you are trying to relieve the pressure<br />

on your head; plus, it has the added effect of getting<br />

you good and drunk so that you can pass out. O.K.,<br />

it isn’t the healthiest way of beating the flu, but it<br />

worked.<br />

With the motor out and the engine back at Crawford,<br />

there wasn’t much I could do, and the car sat<br />

while other projects got priority and the engine was<br />

torn down, inspected and rebuilt.<br />

The knocking that we heard turned out to be a<br />

broken cam-cap bolt. apparently these can break<br />

from time to time, and we just happened to have one<br />

of those engines. Further digging found that a tuning<br />

issue we had been having had washed the cylinders<br />

with fuel and the rings had scuffed the bores; not<br />

good. Further more, the oil pickup tube had a hole<br />

in it and was not getting sufficient oil to the bearings

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