13.07.2015 Views

DateLaboratory Testing of Portland Cement Concrete Patch Material ...

DateLaboratory Testing of Portland Cement Concrete Patch Material ...

DateLaboratory Testing of Portland Cement Concrete Patch Material ...

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Table 1. Rapid Setting <strong>Concrete</strong> <strong>Patch</strong> <strong>Material</strong> RequirementsWisDOT REQUIREMENTTESTED ASTM TEST 2001 WisDOT APPROVED DBR WARRANTY SPECIFICATIONPROPERTY PROCEDURE PRODUCTS LIST ITEM 416.0623.S (2004)Compressive Strength ASTM C 392000 psi @ 2 hours4000 psi @ 7 days3000 psi @ 3 hoursFreeze/Thaw Durability minimum durability factor minimum durability factor(w/ 5% sodium chloride solution) ASTM C 666 <strong>of</strong> 90% after 300 cycles <strong>of</strong> 90% after 300 cycles(using Procedure B) (using Procedure A)Initial Time <strong>of</strong> Set ASTM C 266 minimum <strong>of</strong> 15 minutes no requirementLinear Shrinkage ASTM C 531 maximum <strong>of</strong> 0.100% @ 3 days maximum <strong>of</strong> 0.100% @ 3 daysAlthough the three aforementioned patch materials met WisDOT's requirements in 2001,within one year they all showed signs <strong>of</strong> early distress on STH 13. All <strong>of</strong> the test sectionsconstructed with either Tamms Speed Crete 2028 or Mn/DOT 3U18 mix exhibitedmicrocracking and/or debonding, most likely caused by shrinkage (see Figure 1 below). Thedistresses observed in the Mn/DOT 3U18 test sections were the most severe.Figure 1. <strong>Patch</strong> <strong>Material</strong> Distress on STH 13MICROCRACKDEBONDINGDEBONDING FROM THETRANSVERSE EDGESOF THE SLOTSThe Mn/DOT 3U18 test sections exhibited both debonding and microcracking in some areas (left).Less severe debonding <strong>of</strong> the patch material, from the transverse edges <strong>of</strong> the dowel bar slots, wasobserved in the Tamms Speed Crete 2028 test sections (right).Since the Mn/DOT 3U18 patch material was significantly less expensive than the TammsSpeed Crete 2028 (approximately 1/10 th the cost) and its components were readily available,WisDOT deemed it worthwhile to seek an inexpensive way to improve the performance <strong>of</strong>the material. This study tested and evaluated various modified Mn/DOT 3U18 mixes in anattempt to prevent patch material shrinkage, and any associated cracking and debonding.The objective <strong>of</strong> this research was to find a cost-effective method <strong>of</strong> modifying the Mn/DOT2

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