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Report Investigation of gas blowout on Snorre A - Well Integrity ...

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another sign that the casing spear did not have the necessary seals, or that the seals were<br />

defective, i.e. the circulati<strong>on</strong> went through the casing spear and not through the scab-liner.<br />

They observed that the well took mud, i.e. that the volume balance in the well seemed<br />

satisfactory and just as much mud went into the well as came out.<br />

During further pulling <str<strong>on</strong>g>of</str<strong>on</strong>g> the scab-liner they were repeated forced, for various reas<strong>on</strong>s, to use<br />

overpull. This means that the tracti<strong>on</strong> used was greater than the weight <str<strong>on</strong>g>of</str<strong>on</strong>g> the scab-liner.<br />

At 0500 hours, the top <str<strong>on</strong>g>of</str<strong>on</strong>g> the scab-liner was under the BOP. Before the drilling crew pulled<br />

this through the BOP, they stopped and observed to check for changes in the well volume<br />

(flowcheck). The well did not exhibit any changes in volume. The scab-liner was pulled <strong>on</strong><br />

through the BOP and blocked the cut and hold functi<strong>on</strong>.<br />

At 0700-0715 hours <strong>on</strong> 28 November 2004, the crew changed from night to day shift.<br />

During the period 0800 – 1530 hours, the day shift c<strong>on</strong>tinued to pull the scab-liner. Swabbing<br />

with altogether approx. 4 m 3 volume increase was observed, and mud loss equivalent to 31 m 3<br />

was also observed. During this period, the operati<strong>on</strong> was observed for flowcheck for both<br />

brief and l<strong>on</strong>ger periods. Again, the well was regarded as being stable, and the drilling crew<br />

c<strong>on</strong>tinued to pull the scab-liner after each flowcheck.<br />

During the course <str<strong>on</strong>g>of</str<strong>on</strong>g> the day, the drilling supervisor maintained c<strong>on</strong>tinuous c<strong>on</strong>tact with the<br />

OIM and the drilling operati<strong>on</strong>s supervisor <strong>on</strong> duty <strong>on</strong> land, in order to inform them about<br />

developments in the well.<br />

3.3 Third part: the well c<strong>on</strong>trol situati<strong>on</strong> develops<br />

At 1530 hours <strong>on</strong> the same day, the annular preventer <str<strong>on</strong>g>of</str<strong>on</strong>g> the BOP stack was closed, for the<br />

first time, due to influx. This type <str<strong>on</strong>g>of</str<strong>on</strong>g> valve was the <strong>on</strong>ly <strong>on</strong>e <str<strong>on</strong>g>of</str<strong>on</strong>g> three types <str<strong>on</strong>g>of</str<strong>on</strong>g> safety valves<br />

that could be utilized in the BOP. A Kelly cock was installed and the top drive was screwed<br />

in.<br />

After a brief period <str<strong>on</strong>g>of</str<strong>on</strong>g> pressure increase, the well started to lose pressure. At about 1630<br />

hours, the annular preventer was opened again, to pump mud to <str<strong>on</strong>g>of</str<strong>on</strong>g>fset for the mud loss. A<br />

total <str<strong>on</strong>g>of</str<strong>on</strong>g> about 25 m 3 <str<strong>on</strong>g>of</str<strong>on</strong>g> drilling mud was pumped into the work string and annulus. Attempts<br />

were made to circulate the well, but no mud was returned. Up until 1800 hours, the well was<br />

observed and an additi<strong>on</strong>al loss totaling 13 m 3 was ascertained and noted in the drilling report.<br />

The increasing problems with well P-31A throughout the afterno<strong>on</strong> were the topic <str<strong>on</strong>g>of</str<strong>on</strong>g><br />

discussi<strong>on</strong> at the regular platform management meeting at 1700 hours. The planned<br />

emergency preparedness drill was cancelled because <str<strong>on</strong>g>of</str<strong>on</strong>g> the situati<strong>on</strong>.<br />

At about 1800 hours, after an attempt was made to reverse-circulate the well (down the<br />

annulus and up the work string), a backflow <str<strong>on</strong>g>of</str<strong>on</strong>g> well liquids was observed, which developed in<br />

an undesirable manner. Once again, the annulus safety value was closed in the BOP. The<br />

instability in the well proved to be <strong>on</strong> the rise, with a str<strong>on</strong>g pressure increase to approx. 130<br />

bar in the course <str<strong>on</strong>g>of</str<strong>on</strong>g> 2 hours.<br />

17

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