The Locomotive - Lighthouse Survival Blog
The Locomotive - Lighthouse Survival Blog
The Locomotive - Lighthouse Survival Blog
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68 THE LOCOMOTIVE. [Mat,<br />
ning, and it continued to run until 3:04. During all this time there had been no sign<br />
of leakage from the girth-joint, except the slightest trace of vapor, which had been<br />
occasionally visible between 12:30 and 2:20, when the air in the boiler-room was still.<br />
At 3:04 the quarry pump was stopped, and after waiting just one minute for the circu-<br />
lation to subside a little, the inspirator was started (see D). <strong>The</strong> boiler promptly rose<br />
until it was at least .28" above the normal position. (<strong>The</strong> pencil, unfortunately, ceased<br />
to mark for a short time, and the dotted part of the record is conjectural.; <strong>The</strong> girthjoint<br />
plainly showed distress, and at 3: 13 (see E) it was leaking water quite freely. At<br />
3:19 (see F) the inspirator was shut off, but still the leak continued, and the boiler<br />
maintained its abnormal position. At about 3:27 (see 67) the quarry pump was started<br />
again, and the resulting circulation speedily equalized the temperature in the boiler so<br />
that at 3: 33 (see H) the boiler was resting on the middle saddle, and the leakage had<br />
entirely disappeared. <strong>The</strong> quarry pump continued running, and at 3:43, when the test<br />
was discontinued, the boiler was still in its normal position.<br />
It was thought that the diagram we have described would suffice to demonstrate<br />
that the chilling action of the feed-water was<br />
responsible for the trouble that the owners of<br />
this boiler experienced, but as it was found im-<br />
practicable to regulate the flow of water from<br />
the bucket satisfactorily, the apparatus was<br />
modified to some extent, and the experiments<br />
were repeated. <strong>The</strong> modification consisted in<br />
the substitution of a clock for the water bucket,<br />
as shown in Fig. 4. <strong>The</strong> face and hands of<br />
the clock were removed, and a carefully-turned<br />
hardwood pulley, 1%" in diameter, was se-<br />
cured to the hour spindle. <strong>The</strong> cord from the movable board was passed completely<br />
around this pulley, and to the end of the cord a weight was attached, which was found<br />
by experiment to be almost sufficient to overcome the friction of the board.<br />
With the modified apparatus a new test was made, substantially as before. Marks<br />
were made on the moving board, at known intervals of time, for the purpose of testing<br />
the regularity of its motion, and it was found that in the improved form of the apparatus<br />
the motion of the board could be considered, without sensible error, to be absolutely uni-<br />
form. <strong>The</strong> lest was begun at 10: 22^ a. m., at which time the quarry pump was running.<br />
At 10:23 the inspirator was started, with the pump still running, and for nine minutes<br />
there was no noticeable effect. <strong>The</strong> water level was purposely carried very high, and at<br />
10:32 the boiler began to rise from the saddle, the circulation apparently being in-<br />
sufficient to take care of the large body of feed that was introduced. <strong>The</strong> inspirator<br />
was stopped at 10 :<br />
34,<br />
Fig. 4.<br />
Re< ordixg Apparatus.<br />
but the boiler continued to rise until about 10 : 36. <strong>The</strong> girth seam<br />
began to leak water about 10:32. and at 10:38, four minutes after the inspirator was<br />
stopped, the circulation seemed to succeed in equalizing the temperature again, for the<br />
boiler went down promptly until it rested on the saddle, and the leak disappeared.<br />
From this time until 10 : 57 the boiler did not leave the saddle by more than the hun-<br />
dredth part of an inch. At 10:57 the quarry pump, which had been running ever since<br />
the experiment began, was stopped, and the boiler began to rise very slowly, and it was<br />
a trifle more than .04" above the saddle at 11:28. It is not easy to say what was the<br />
cause of this slight variation, but as the boiler was uncovered, and the cool, out-door air<br />
blew against the bottom of it through a window, it is possible that the chill so produced<br />
was sufficient to cause the observed rise. At 11 : 28 the inspirator was started, and the<br />
—<br />
Improved Form of the