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TECHNOLOGY<br />
FOCUS<br />
Factors<br />
pH<br />
Copper ozJgaL<br />
Exposure time Im<strong>in</strong>.l<br />
I i<br />
I<br />
, .,'<br />
.l I I<br />
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-i I \<br />
Attack<br />
·1 2<br />
., 2<br />
I, Lllvel " "+• Level" ••<br />
10.3<br />
9.9<br />
90<br />
8.6<br />
'6.3<br />
45<br />
F.igure6-Alkalille Strip Experiment<br />
Matrix.<br />
Figu.re 7-PCI- W<strong>in</strong> Probe System..<br />
Figure 8-PCl·<br />
Will Sweep Output.<br />
application method. Based on this resun,.<br />
<strong>the</strong> manufactur<strong>in</strong>g specification was modified<br />
to only require a quick immersion <strong>in</strong><br />
lieu of a four-m<strong>in</strong>ute soak. The practice<br />
was quickly implemented <strong>in</strong> Phase U.<br />
Chemical Attack<br />
Dur<strong>in</strong>g <strong>the</strong> project, a large quantity of<br />
gears were exhibit<strong>in</strong>g a pitted condition at<br />
<strong>the</strong> mach<strong>in</strong><strong>in</strong>g operations <strong>in</strong> various areas.<br />
After metallurgical exam<strong>in</strong>ation, it was<br />
determ<strong>in</strong>ed that <strong>the</strong> pits were a result of<br />
chemical attack/corrosion. S<strong>in</strong>ce <strong>the</strong><br />
machiae cutt<strong>in</strong>g fluids, clean<strong>in</strong>g and<br />
preservation factors had been previously<br />
tested <strong>in</strong> Phase I, <strong>the</strong>y were quickly dismissed<br />
as <strong>the</strong> root cause. This allowed <strong>the</strong><br />
team to focus <strong>the</strong> <strong>in</strong>vestigation <strong>in</strong> <strong>the</strong> plat<strong>in</strong>g<br />
facility. The key factors were identified<br />
through a thought process mapp<strong>in</strong>g exercise.<br />
Possible <strong>in</strong>itiators of <strong>the</strong> attack were<br />
alkal<strong>in</strong>e pH,expos1IIfe time, and <strong>the</strong> ounces<br />
of copper <strong>in</strong> <strong>the</strong> alkal<strong>in</strong>e strip solution. An<br />
experiment was designed. to test <strong>the</strong>se factors<br />
an 9310 steel specimens as shown <strong>in</strong><br />
Figure 6..Analysis of <strong>the</strong> experiment. identified<br />
pH as <strong>the</strong> factor with <strong>the</strong> highest significance.<br />
Data also <strong>in</strong>dicated when <strong>the</strong> pH<br />
level was greater than W, chemical attack<br />
did not occur.<br />
For phase II implementation, <strong>the</strong> team<br />
<strong>in</strong>stalled a controller on <strong>the</strong> alkal<strong>in</strong>e strip<br />
tanks to ma<strong>in</strong>ta<strong>in</strong> <strong>the</strong> tank pH levels above<br />
lO.3, by automatically add<strong>in</strong>g anhydrous<br />
ammonia when <strong>the</strong> pH level dropped<br />
below 10.3, It was noted !hat dur<strong>in</strong>g <strong>the</strong><br />
anhydrous ammonia addition, an. exo<strong>the</strong>rmic<br />
reaction occurred,heat<strong>in</strong>g <strong>the</strong> solution<br />
to temperatures above HJO"F.The problem<br />
identified with <strong>the</strong> elevated temperature<br />
was that when <strong>the</strong> alkal<strong>in</strong>e stripp<strong>in</strong>g SOJIItionreached<br />
temperatures above 77°P, it<br />
became corrosive to carbon steels. The<br />
team <strong>in</strong>stalled a chill<strong>in</strong>g unit <strong>in</strong> <strong>the</strong> stripp<strong>in</strong>g<br />
tanks to stabilize <strong>the</strong> solution temperature<br />
at 60"E After <strong>in</strong>stall<strong>in</strong>g <strong>the</strong> chiller and<br />
ma<strong>in</strong>ta<strong>in</strong><strong>in</strong>g stable pH levels at 10.3-10,7,<br />
no chemical attack on an entire lot of gears<br />
has occurred due to pH imbalance as a root<br />
cause.<br />
Residual Coolant<br />
Early <strong>in</strong>. <strong>the</strong> project, it was determ<strong>in</strong>ed<br />
by extensive laboratory test<strong>in</strong>g that waterbased<br />
mach<strong>in</strong><strong>in</strong>g coolant was an effective<br />
corrosion. <strong>in</strong>hibitor. Low carbon alloy gears<br />
coated with a film of <strong>in</strong>-process coolant did<br />
not corrode after two months <strong>in</strong> <strong>the</strong> high<br />
heat and humidity test chamber.<br />
The results of this test<strong>in</strong>g were:<br />
• Used coolant is not a corrosion enabler,<br />
• The coolant solution's ability to form a<br />
protective film barrier on <strong>the</strong> surface of <strong>the</strong><br />
part determ<strong>in</strong>ed its ability to <strong>in</strong>hibit corrosion.<br />
Whe<strong>the</strong>r this film came (rom virg<strong>in</strong><br />
or <strong>in</strong>-process coolant was irrelevant.<br />
.•If a film was not left on <strong>the</strong> part by <strong>the</strong><br />
coolant after <strong>the</strong> mach<strong>in</strong><strong>in</strong>g operation and<br />
it was not properly treated with a preservative<br />
oil, <strong>the</strong>n corrosion was enabled. Such<br />
corrosion resulted <strong>in</strong> <strong>in</strong>creased manufactur<strong>in</strong>g<br />
costs andlead times.<br />
·401 JULY/AUGUST <strong>2002</strong>' GEAR TECHNOLOGY· www.geartechno/Qgy.com' www.powertransm;ss on. com<br />
• A corrosion-protective film could be<br />
formed after process<strong>in</strong>g through ei<strong>the</strong>r <strong>the</strong><br />
coolam or preservative solution typically<br />
applied dur<strong>in</strong>g <strong>the</strong> msnufacnmng process.<br />
Test results <strong>in</strong>dicated that residua]<br />
coolant would leave a short-term COITOsian<br />
<strong>in</strong>hibit<strong>in</strong>g film an <strong>the</strong> gears similar<br />
to <strong>the</strong> ones result<strong>in</strong>g from immersion ill<br />
an oil bath. This residual film could<br />
reduce <strong>the</strong> <strong>in</strong>cidence of corrosion even if<br />
<strong>the</strong> preservative oil was not applied. If<br />
<strong>the</strong> proper flu.id attributes could be measured<br />
and ma<strong>in</strong>ta<strong>in</strong>ed, not only would<br />
costly corrosion <strong>in</strong>itiation be greatly<br />
reduced, but <strong>the</strong> corrosion prevention<br />
steps (preservative baths) could also be<br />
decreased or elim<strong>in</strong>ated.<br />
On-l<strong>in</strong>e PCI-W<strong>in</strong> Probe<br />
A significant barrier to. rely<strong>in</strong>g on residual<br />
coolant as rut effective short-term COfrosion<br />
:<strong>in</strong>hilbitor is determ<strong>in</strong><strong>in</strong>g if <strong>the</strong><br />
coolant has !he proper attributes. Standard<br />
corrosion test<strong>in</strong>g takes too long to give<br />
usable <strong>in</strong><strong>format</strong>ion ill an Oil-go<strong>in</strong>g production<br />
environment. For example, this test<strong>in</strong>g<br />
procedure would take approximately 48<br />
hours to complete at added cost for coolant<br />
analysis. The team's goal was to f<strong>in</strong>d a tool<br />
to provide real time sump-site test<strong>in</strong>g to'<br />
predict <strong>the</strong> coolant's corrosion <strong>in</strong>hibit<strong>in</strong>g<br />
properties.<br />
After fur<strong>the</strong>r research.<br />
<strong>the</strong> team decided<br />
on !he use of an adapted Digi-Galv prob<strong>in</strong>g<br />
system, PCl-W<strong>in</strong> Probe, similar <strong>in</strong> operat<strong>in</strong>g<br />
pr<strong>in</strong>ciple to <strong>the</strong> one: u ed <strong>in</strong> <strong>the</strong> oil<br />
pipel<strong>in</strong>e monitor<strong>in</strong>g <strong>in</strong>dustry. The probe<br />
has<strong>the</strong> potential to provide quick <strong>in</strong>dicationsof<br />
a coolant's corrosion-<strong>in</strong>hibit<strong>in</strong>g<br />
capabidties.<br />
The PCl-Wm Probe system shown <strong>in</strong><br />
Figure 7, consists of a small test. cell (specimen<br />
hous<strong>in</strong>g and electrode), a digitally<br />
controlled dual range precision <strong>in</strong>strument<br />
unit, and a standard Pentium desktop PC<br />
with <strong>the</strong> AMPLICON PC30AT crud and<br />
associated software <strong>in</strong>stalled. In addition,<br />
three accessories are added: a glass sleeve<br />
sample vessel, a constant temperature<br />
water bath with tub<strong>in</strong>g to allow flow<br />
through <strong>the</strong> glass sleeve, and a pump to<br />
provide circulation of <strong>the</strong> sample. The<br />
accessories create a test<strong>in</strong>g environment<br />
that simulates <strong>the</strong> actual conditions under