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MONTHLY PROGRESS REPORT - SHORT FORM<br />

Report Dates: October 1, <strong>2000</strong> to October 31, <strong>2000</strong> Hard Copies Distributed to:<br />

Contract No.: N62470-97-D-5000 COTR:<br />

Karen Wilson<br />

(757)322-4817<br />

Order No.: 0014<br />

Wilsonke@efdlant.navfac.navv.mil<br />

I<br />

Pr-,ect No.: 920764<br />

RAC CM:<br />

(757)396-5121<br />

Greg Hedley<br />

Project Name: Hadnot Point Fuel Farm Hedlevqs@efdlant.navfac.navy.mil ext. 383<br />

Project Location: MCB Camp Lejeune, NC Project Controls Manager:<br />

Linda Barberousse<br />

(757)363-7190<br />

Project Manager: James A. Dunn, Jr., P.E.<br />

Lbarberousse@theitqroup.com<br />

Project Description: Contract Files<br />

Construction and Operation of Biosparging, Air Sparging, and Soil Vapor<br />

Extraction Systems with aggressive fluid vapor recovery at Hadnot Point<br />

Fuel Farm/Building 1115.<br />

Scheduled Web Site Posting Date:<br />

Original Contract Start Date:<br />

Original Contract Completion Date:<br />

Current Contract Completion Date:<br />

O&M Completion Date:<br />

Current Projected Completion Date:<br />

Current TO Ceiling:<br />

Total $ to Date:<br />

Remaining Funds:<br />

Estimated Report Period:<br />

Forecast @ Completion:<br />

2,826,904.00<br />

2,012,115.00<br />

814,789.OO<br />

70,696.OO<br />

2,822,147.00<br />

Ht a i extraction wells recovered 61 gals. of product. Normal O&M of the SE system resulted in recovery of 52,227 Ibs. of<br />

hydrocarbons. Continued daily gauging of wells and Buildings 1101 and 1068 at HPFF and twice weekly checking of all twelve<br />

buildings. Re-caulked buildings 1108, 1115 and 1068 to close potential vapor pathways. Conducted 6 AFVR events on various<br />

Current schedule attached.<br />

None.<br />

Orig<br />

Provide RA for Hadnot Point Fuel Farm bldg.<br />

1115, Camp Lejeune, NC.<br />

06/30/98 07122199 $1,483,522.00 $58,413.00 $1,541,935.00<br />

1 Additional 12 months of O&M through 8/31/00 05128199 08/31 /OO $214,989.00 $11,525.00 $226514.00<br />

2<br />

Install trench at East end of Bldg 1101 and<br />

install blower.<br />

12129199 08/01 /OO $0.00 $0.00 $0.00<br />

3<br />

Scope Change - Completely replace all O&M<br />

for the current period<br />

01/l 3/00 08/01 /OO $0.00 $0.00 $0.00<br />

Prep Work Plans to provide trenching around<br />

4 Bldg. 1101 and trenching at Wells HPFF-28 01/28/00 08/01 /OO $7,122 $431 .oo !§7,553.00<br />

-,m and MW-15<br />

Exploratory Excavation around MW HPFF-28<br />

5<br />

and MW-15 to attempt to determine the<br />

source of free product. Conduct SVE<br />

02/22/00 08/01 /OO $80,848.00 $3,166.00 $84,014.00<br />

influence testing program<br />

6 Seal Bldg. 1101 and conduct test of biosparge 03/01/00 08/01 /OO $28,004.00 $1,219.00 $29,223.00

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